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== Well Details == | == Well Details == | ||
{| class="wikitable" width="95%" | {| class="wikitable" width="95%" | ||
− | | Well ID: 131-20092 | + | | Well ID: 42-131-20092 |
| style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.421225, -76.03905 | width=100% | height=100% }} | | style="width: 50%; height=100%; align=center" rowspan="14" | {{#display_map: 41.421225, -76.03905 | width=100% | height=100% }} | ||
|- | |- |
Well ID: 42-131-20092 | ![]() Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. Sorry, we have no imagery here. ![]() |
County: Wyoming | |
Municipality: Monroe Township | |
Operator Name: CARRIZO (MARCELLUS) LLC | |
Farm/Lease Name: SHIELDS 1V | |
First Permit Date: 2010-09-14 | |
Last Permit Date: 2010-09-14 | |
Spud Date: 2011-01-06 | |
Unconventional: Yes | |
Horizontal: No | |
Producing: No | |
Violations: 3 | |
Latitude: 41.421225 | |
Longitude: -76.03905 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID |
---|---|---|---|---|
1941183 | 2011-01-06 | No Violations Noted | ||
1944789 | 2011-01-24 | No Violations Noted | ||
1946683 | 2011-01-24 | No Violations Noted | UDI- Rig 46. Company Man Scott Schultz. Crew assembling 11 3/4 casing and running in hole upon arrival. DEP stayed on site to observe cement job. At @ 23:30, BJ Services begin pumping cement. 15.4 wt/ Y - 1.23/ 0.5% gasblok. 540 sks gastite cement. Had 55 bbls returns. Casing set at 716'. Final weight of cement on flow line was checked with mud scale= 14.5. Plug landed at 01:45, float held. WOC 8 hrs. | |
1946716 | 2011-01-26 | Viol(s) Noted & Immediately Corrected | Scott Schultz- Co. Man. FUI on spill of drill cuttings/mud. Solids handling contractor penetrated bottom of open-top mud tub with excavator teeth while mixing solids. Lost a reported 50 bbls of drill cuttings/mud onto plastic under tub. Spilled material was immediately cleaned up and disposed of. Tub was emptied and hole in bottom of tub was patched. Spill occurred @05:00 on 1/25/11. Reported by Gary Byron from carizzo. | 603844 |
1946992 | 2011-02-02 | No Violations Noted | I received analysis results for the methane sampling suite. The results indicated a detection for methane (0.0163 mg/L). I compared this with pre-drill test results provided by Carizzo Marcellus. The pre-drill results indicated no detection of methane. I collected another sample from the residence to determine if the installation of the casing at the well has remediated the problem. I informed Gary Byron, consultant for Carizzo, that I was collecting another sample and of the results of the methane sample. | |
1950891 | 2011-02-18 | Violation(s) Noted | 605069 | |
1954330 | 2011-03-03 | No Violations Noted | ||
1961133 | 2011-03-17 | No Violations Noted | Received and reviewed landowner's requests for restoration plan. | |
1985100 | 2011-06-30 | No Violations Noted | Well has been plugged. | |
1998265 | 2011-08-24 | No Violations Noted | ||
2005104 | 2011-09-26 | No Violations Noted | ||
2010585 | 2011-09-07 | Pending | ||
2062442 | 2012-04-26 | Violation(s) Noted | Well was plugged on 2/9/2011 and Drilling Permit had expired on 9/14/2011. The operator has failed to terminate the ESCGP and is in violation of 102.7.
|
637794 |
2079799 | 2012-06-29 | No Viols - Permanently Shut Down | Reviewed Well Site Restoration Report. |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2011-1 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
2010-2 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 | 0.0 |
PERIOD | TYPE | QUANTITY | UNITS | DISPOSAL METHOD | WASTE FACILITY PERMIT ID | WASTE FACILITY NAME | FACILITY CITY | FACILITY STATE |
---|---|---|---|---|---|---|---|---|
2011-1 | DRILLING FLUID WASTE | 2679.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | WMGR119 | EUREKA RESOURCES (WILLIAMSPORT WATER TREATMENT) | WILLIAMSPORT | PA |
2011-1 | DRILL CUTTINGS | 597.0 | Tons | LANDFILL | NY31346244 | HAKES LANDFILL | PAINTED POST | NY |
2011-1 | DRILLING FLUID WASTE | 454.0 | Bbl | CENTRALIZED TREATMENT PLANT FOR RECYCLE | PA0102784 | WASTE TREATMENT CORPORATION | WARREN | PA |