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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-081-61062 | | Well ID: 34-081-61062 | ||
+ | | style="height=100%; align=center" rowspan="15" | {{#display_map: 40.50765086, -80.6912731 | width=100% | height=100% }} | ||
|- | |- | ||
− | | County: | + | | County: [[Jefferson County, Ohio|Jefferson]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[FIRSTENERGY GENERATION LLC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
− | | Spud Date: | + | | Spud Date: |
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: | + | | Latitude: 40.50765086 |
|- | |- | ||
− | | Longitude: | + | | Longitude: -80.6912731 |
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|} | |} | ||
== Inspection Data == | == Inspection Data == | ||
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!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
+ | |- | ||
+ | | 1030951423 | ||
+ | | 2013-10-24 | ||
+ | | | ||
+ | | I was on location for this well. The well was logged by Appalachian Services and shot off the 6.625 casing 200' down hole where free pipe was shown. 2 3/8 tubing was going to be run into 502' but the hole bridged off around 180'. We had to pull out of the hole, and put a cut collar on the tubing to allow us to wash it down. We had to pump on the hole for sometime before we circulated out the bridge. We were able to run down to 502' and set a 150 sack surface cement plug. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1678127553 | ||
+ | | 2015-03-18 | ||
+ | | | ||
+ | | On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B). | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
|- | |- | ||
| -874968115 | | -874968115 | ||
| 2013-10-23 | | 2013-10-23 | ||
− | | | + | | |
− | | I was on location with Inspector Lowdur to witness the pulling of the 2 | + | | I was on location with Inspector Lowdur to witness the pulling of the 2 tubing and the setting of the first cement plug. There was a delay in pulling the tubing as the rods parted inside the tubing and had to be cut off with each joint. A 145 sack cement plug was set and will checked tomorrow. |
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|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-081-61062 | Loading map...
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County: Jefferson | |
Municipality: | |
Operator Name: FIRSTENERGY GENERATION LLC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 40.50765086 | |
Longitude: -80.6912731 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1030951423 | 2013-10-24 | I was on location for this well. The well was logged by Appalachian Services and shot off the 6.625 casing 200' down hole where free pipe was shown. 2 3/8 tubing was going to be run into 502' but the hole bridged off around 180'. We had to pull out of the hole, and put a cut collar on the tubing to allow us to wash it down. We had to pump on the hole for sometime before we circulated out the bridge. We were able to run down to 502' and set a 150 sack surface cement plug. | ||||
1678127553 | 2015-03-18 | On the date of inspection I am accompanied by SE Regional Manager Brent Bear to inspect the plugged and abandoned well for Final Restoration. The well passes Final Restoration per ORC 1509.072(B). | ||||
-874968115 | 2013-10-23 | I was on location with Inspector Lowdur to witness the pulling of the 2 tubing and the setting of the first cement plug. There was a delay in pulling the tubing as the rods parted inside the tubing and had to be cut off with each joint. A 145 sack cement plug was set and will checked tomorrow. |
For data sources see[1]