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Difference between revisions of "34-059-23869"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-059-23869
 
| Well ID: 34-059-23869
 +
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.92026376, -81.54253969 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| County: [[Guernsey County, Ohio|Guernsey]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[BUCKEYE OIL PRODUCING CO]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date: 1996-08-03
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing:
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations:
+
| Violations: 0
 
|-
 
|-
| Latitude:
+
| Latitude: 39.92026376
 
|-
 
|-
| Longitude:
+
| Longitude: -81.54253969
 
|-
 
|-
 
|}
 
|}
Line 42: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 950.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 349.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 2974.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1156.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 2540.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 446.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 1273.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 860.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 1679.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 635.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 2472.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 380.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 2937.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 574.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 3616.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 430.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 3885.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 293.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 2113.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 202.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 25.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 63: Line 157:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1138711108
 
| 1138711108
 
| 2006-01-30
 
| 2006-01-30
|
+
|  
 
| TIMCO RIG ON HOLE. UNABLE TO SEAT PACKER. WILL HAVE TO PULL TUBING AND STEAM SAME, PERFORATE LIME, SUSPECTED HOLE IN CASING, GO BACK IN WITH TUBING AND SET BOTTOM AND LIME PLUGS THRU TUBING.
 
| TIMCO RIG ON HOLE. UNABLE TO SEAT PACKER. WILL HAVE TO PULL TUBING AND STEAM SAME, PERFORATE LIME, SUSPECTED HOLE IN CASING, GO BACK IN WITH TUBING AND SET BOTTOM AND LIME PLUGS THRU TUBING.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1138970235
 
| 1138970235
 
| 2006-02-02
 
| 2006-02-02
|
+
|  
 
| STILL UNABLE TO BREAK RODS FREE. 6 GAL. SOLVENT PUT DOWN HOLE, LET SIT OVERNIGHT, 2000' RODS PULLED FROM TUBING. RIG WILL BE MOVED OFF HOLE AND SOLVENT WILL BE PLACED DOWNHOLE DAILY UNTIL RODS CAN BE PULLED THEN RIG WILL BE BROUGHT BACK TO WORK ON THE TUBING.
 
| STILL UNABLE TO BREAK RODS FREE. 6 GAL. SOLVENT PUT DOWN HOLE, LET SIT OVERNIGHT, 2000' RODS PULLED FROM TUBING. RIG WILL BE MOVED OFF HOLE AND SOLVENT WILL BE PLACED DOWNHOLE DAILY UNTIL RODS CAN BE PULLED THEN RIG WILL BE BROUGHT BACK TO WORK ON THE TUBING.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1143640357
 
| 1143640357
 
| 2006-03-28
 
| 2006-03-28
|
+
|  
 
| TIMCO RIG ON HOLE, STARTED 1/30/2006. PULLING RODS, RODS HUNG, AT THAT POINT STARTED PUTTING ACID IN HOLE. 6 GALLONS PER DAY DOWN TUBING.STILL COULDN'T MOVE RODS INSIDE TUBING.ATTEMPTED SEVERAL TIMES TO START MOVING RODS WITH ACID IN TUBING, WOULD NOT MOV
 
| TIMCO RIG ON HOLE, STARTED 1/30/2006. PULLING RODS, RODS HUNG, AT THAT POINT STARTED PUTTING ACID IN HOLE. 6 GALLONS PER DAY DOWN TUBING.STILL COULDN'T MOVE RODS INSIDE TUBING.ATTEMPTED SEVERAL TIMES TO START MOVING RODS WITH ACID IN TUBING, WOULD NOT MOV
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1149700857
 
| 1149700857
 
| 2006-06-07
 
| 2006-06-07
|
+
|  
 
| FINAL RESTORATION
 
| FINAL RESTORATION
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1289i13951635
 
| 1289i13951635
 
| 2001-04-19
 
| 2001-04-19
|
+
|  
 
| PRELIMENARY RESTORATION COMPLETE.
 
| PRELIMENARY RESTORATION COMPLETE.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2039289299
 
| 2039289299
 
| 2006-01-31
 
| 2006-01-31
|
+
|  
 
| timco rig on hole unable to unseat packer.PULL RODS OUT, RUN RODS IN, APPEARS TO BE HUNG IN HOLE SOMEWHERE DOWN HOLE.
 
| timco rig on hole unable to unseat packer.PULL RODS OUT, RUN RODS IN, APPEARS TO BE HUNG IN HOLE SOMEWHERE DOWN HOLE.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 215671055
 
| 215671055
 
| 2006-02-01
 
| 2006-02-01
|
+
|  
 
| TIMCO RIG STILL UNABLE TO UNSEAT PACKER. RIG SHUT DOWN. GETTING HEADS TOGETHER FOR PLANS.
 
| TIMCO RIG STILL UNABLE TO UNSEAT PACKER. RIG SHUT DOWN. GETTING HEADS TOGETHER FOR PLANS.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:20, 14 July 2015

Well Details

Well ID: 34-059-23869
Loading map...
County: Guernsey
Municipality:
Operator Name: BUCKEYE OIL PRODUCING CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1996-08-03
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.92026376
Longitude: -81.54253969

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1996-0 950.0 349.0
1997-0 2974.0 1156.0
1998-0 2540.0 446.0
1999-0 1273.0 860.0
2000-0 1679.0 635.0
2001-0 2472.0 380.0
2002-0 2937.0 574.0
2003-0 3616.0 430.0
2004-0 3885.0 293.0
2005-0 2113.0 202.0
2006-0 0.0 25.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1138711108 2006-01-30 TIMCO RIG ON HOLE. UNABLE TO SEAT PACKER. WILL HAVE TO PULL TUBING AND STEAM SAME, PERFORATE LIME, SUSPECTED HOLE IN CASING, GO BACK IN WITH TUBING AND SET BOTTOM AND LIME PLUGS THRU TUBING.
1138970235 2006-02-02 STILL UNABLE TO BREAK RODS FREE. 6 GAL. SOLVENT PUT DOWN HOLE, LET SIT OVERNIGHT, 2000' RODS PULLED FROM TUBING. RIG WILL BE MOVED OFF HOLE AND SOLVENT WILL BE PLACED DOWNHOLE DAILY UNTIL RODS CAN BE PULLED THEN RIG WILL BE BROUGHT BACK TO WORK ON THE TUBING.
1143640357 2006-03-28 TIMCO RIG ON HOLE, STARTED 1/30/2006. PULLING RODS, RODS HUNG, AT THAT POINT STARTED PUTTING ACID IN HOLE. 6 GALLONS PER DAY DOWN TUBING.STILL COULDN'T MOVE RODS INSIDE TUBING.ATTEMPTED SEVERAL TIMES TO START MOVING RODS WITH ACID IN TUBING, WOULD NOT MOV
1149700857 2006-06-07 FINAL RESTORATION
1289i13951635 2001-04-19 PRELIMENARY RESTORATION COMPLETE.
2039289299 2006-01-31 timco rig on hole unable to unseat packer.PULL RODS OUT, RUN RODS IN, APPEARS TO BE HUNG IN HOLE SOMEWHERE DOWN HOLE.
215671055 2006-02-01 TIMCO RIG STILL UNABLE TO UNSEAT PACKER. RIG SHUT DOWN. GETTING HEADS TOGETHER FOR PLANS.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.