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Difference between revisions of "34-105-23724"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-105-23724
 
| Well ID: 34-105-23724
 +
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.12701854, -81.92074853 | width=100% | height=100% }}
 
|-
 
|-
| County:
+
| County: [[Meigs County, Ohio|Meigs]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[RAINBOW OIL & GAS]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date: 2013-07-16
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing:
+
| Well Status: Producing
 
|-
 
|-
| Violations:
+
| Violations: 0
 
|-
 
|-
| Latitude:
+
| Latitude: 39.12701854
 
|-
 
|-
| Longitude:
+
| Longitude: -81.92074853
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 63: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1086764085
 
| -1086764085
 
| 2013-12-19
 
| 2013-12-19
|
+
|  
 
| Check on annular disposal. Surface casing visible, lines hooked up and watertight.
 
| Check on annular disposal. Surface casing visible, lines hooked up and watertight.
|
+
|  
|
+
|  
|
+
| Field Visit or Inspection
 
|-
 
|-
 
|-
 
|-
 
| -1213926962
 
| -1213926962
 
| 2013-12-19
 
| 2013-12-19
|
+
|  
 
| Inspected the annular disposal connections with Inspector Josh Garland. Jeff Burke (well owner) was on site as well. All connections are water tight. No leaks were observed during inspection.
 
| Inspected the annular disposal connections with Inspector Josh Garland. Jeff Burke (well owner) was on site as well. All connections are water tight. No leaks were observed during inspection.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| -1874430466
 
| 2014-08-19
 
|
 
| Preliminary restoration requirments have been met.
 
|
 
|
 
|
 
|-
 
|-
 
| -315012153
 
| 2013-12-24
 
|
 
| Follow up to -693532978 and complaint #4560. A functioning pop-off had been installed at the separator.
 
|
 
|
 
|
 
|-
 
|-
 
| -693532978
 
| 2013-12-12
 
|
 
| Landowner had complained of a smell of gas. I met with Jeff Burke of Rainbow Oil & Gas at the well site. Owner was venting gas into the 100 Barrel steel tank and allowing it to be released from the manhole in the tank. Owner stated the lines had not yet been laid due to right of way issues with the adjacent landowners. He stated work laying the line would begin early next week. All gas vented to the atmosphere must be flared, with the exception of gas released by a properly functioning relief device and gas released by controlled venting for testing, blowing down and cleaning out wells. Unlawful venting shall cease immediately and releif devise or flare must be installed if venting is to continue.
 
|
 
| 9-9-05(B)
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1231047577
 
| 1231047577
 
| 2013-09-05
 
| 2013-09-05
|
+
|  
| Log suite ran. Cement op on backside of 4 1/2" production casing was1373 , Berea Sandstone from 1684-1694, perforated from 1684-1688 with 10 shots.
+
| Log suite ran. Cement op on backside of 4 1/2 production casing was1373 , Berea Sandstone from 1684-1694, perforated from 1684-1688 with 10 shots.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1241571933
 
| 1241571933
 
| 2013-12-30
 
| 2013-12-30
|
+
|  
 
| Follow up to -693532978 and complaint #4560. Lines laid and meter box being connected. Well is to be in production later today.
 
| Follow up to -693532978 and complaint #4560. Lines laid and meter box being connected. Well is to be in production later today.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1373400870
 
| 1373400870
 
| 2013-07-09
 
| 2013-07-09
|
+
|  
 
| Building location and digging pits.
 
| Building location and digging pits.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1374594658
 
| 1374594658
 
| 2013-07-22
 
| 2013-07-22
|
+
|  
| Witnessed surface cement job. 3 centralizers were ran at 64', 224', and at 352'. 417 feet of new 7" surface casing was set in 430 feet of 9 7/8" hole with 125 sacks of Class A cement with 1% gel, 100% excess used. Hole conditioned and good circulation established before cement pumped. During cement mix the pressures at the pump truck reached 500 psi and Formation cement shut down truck. Pressure was bled off the lines and the pipe was pulled a few feet out of the hole. Lines reconnected and circulation established immediately, continued on with job. The pressures reached 500 psi and the pipe began to move up out of the hole again, before the displacement was run. Again the pressure was released and the pipe pulled, now 10-15 feet out of hole. The job was restarted and cement returns were seen at the surface, before the displacement was ran, with less than 1 Bbl of returns. Pressured up for the third time and the well was shut in with casing full of cement. Company plans to cut off surface casing at ground level and drill out cement.
+
| Witnessed surface cement job. 3 centralizers were ran at 64', 224', and at 352'. 417 feet of new 7 surface casing was set in 430 feet of 9 7/8 hole with 125 sacks of Class A cement with 1% gel, 100% excess used. Hole conditioned and good circulation established before cement pumped. During cement mix the pressures at the pump truck reached 500 psi and Formation cement shut down truck. Pressure was bled off the lines and the pipe was pulled a few feet out of the hole. Lines reconnected and circulation established immediately, continued on with job. The pressures reached 500 psi and the pipe began to move up out of the hole again, before the displacement was run. Again the pressure was released and the pipe pulled, now 10-15 feet out of hole. The job was restarted and cement returns were seen at the surface, before the displacement was ran, with less than 1 Bbl of returns. Pressured up for the third time and the well was shut in with casing full of cement. Company plans to cut off surface casing at ground level and drill out cement.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1374603088
 
| 1374603088
 
| 2013-07-23
 
| 2013-07-23
|
+
|  
 
| The cement had fallen back about a foot. It will be topped off with a sack of redi-mix. .
 
| The cement had fallen back about a foot. It will be topped off with a sack of redi-mix. .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1375130319
 
| 1375130319
 
| 2013-07-29
 
| 2013-07-29
|
+
|  
| Drilling cement out of 7" surface casing and equalizing fluid in hole to get ready for casing pressure test.
+
| Drilling cement out of 7 surface casing and equalizing fluid in hole to get ready for casing pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1375219858
 
| 1375219858
 
| 2013-07-30
 
| 2013-07-30
|
+
|  
| Administered Annular Disposal surface casing integrity test. 370 psi was held on 404' of 7" surface casing for 15 minutes with 10 psi loss. Test passed. No Tanks.
+
| Administered Annular Disposal surface casing integrity test. 370 psi was held on 404' of 7 surface casing for 15 minutes with 10 psi loss. Test passed. No Tanks.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1376317744
 
| 1376317744
 
| 2013-08-12
 
| 2013-08-12
|
+
|  
 
| Currently drilling at  1400 feet, down below the Injun Sand.
 
| Currently drilling at  1400 feet, down below the Injun Sand.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1377008100
 
| 1377008100
 
| 2013-08-20
 
| 2013-08-20
|
+
|  
| Currently drilling at 1800'. Berea Sandstone encountered at roughly 1740'. 4 1/2" casing being delivered today.
+
| Currently drilling at 1800'. Berea Sandstone encountered at roughly 1740'. 4 1/2 casing being delivered today.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1378222918
 
| 1378222918
 
| 2013-09-03
 
| 2013-09-03
|
+
|  
| Witnessed longstring cement job. 1837' of 4 1/2" casing set in 1840' of 6 1/4" borehole with 33 sacks EA type II cement with expanders. Pressure test ran at 900 psi and pipe passed.
+
| Witnessed longstring cement job. 1837' of 4 1/2 casing set in 1840' of 6 1/4 borehole with 33 sacks EA type II cement with expanders. Pressure test ran at 900 psi and pipe passed.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1388771081
 
| 1388771081
 
| 2013-12-31
 
| 2013-12-31
|
+
|  
 
| Associated with complaint # 4560 and inspection -693532978 . Received call from producer letting me know the lines have been completely connected.
 
| Associated with complaint # 4560 and inspection -693532978 . Received call from producer letting me know the lines have been completely connected.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1389200013
 
| 1389200013
 
| 2014-01-08
 
| 2014-01-08
|
+
|  
 
| Witnessed Longstring cement job. 1806 feet of new 4 1/2 casing set in 1810 feet of 6 1/4 inch borehole with 29 sacks of Class A cement. Circulation established. Casing pressure test administered with no loss of pressure over the required time.
 
| Witnessed Longstring cement job. 1806 feet of new 4 1/2 casing set in 1810 feet of 6 1/4 inch borehole with 29 sacks of Class A cement. Circulation established. Casing pressure test administered with no loss of pressure over the required time.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 18251560
 
| 18251560
 
| 2013-07-16
 
| 2013-07-16
|
+
|  
| 21 feet of 10" drive pipe was set to hold unconsolidated surface materials. Review of drilling rules with producer.
+
| 21 feet of 10 drive pipe was set to hold unconsolidated surface materials. Review of drilling rules with producer.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1874430466
 +
| 2014-08-19
 +
|
 +
| Preliminary restoration requirments have been met.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1900512462
 
| 1900512462
 
| 2013-09-06
 
| 2013-09-06
|
+
|  
 
| Witnessed partial hydraulic frac job. Berea Sandstone shot from 1684 - 1688 with 10 shots. Formation treated with 45305 gallons fresh water and 140 sacks 20/40 sand. Breakdown 2249 psi, with and average pressure of 1958 psi.
 
| Witnessed partial hydraulic frac job. Berea Sandstone shot from 1684 - 1688 with 10 shots. Formation treated with 45305 gallons fresh water and 140 sacks 20/40 sand. Breakdown 2249 psi, with and average pressure of 1958 psi.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 226985605
 
| 226985605
 
| 2013-12-18
 
| 2013-12-18
|
+
|  
| Follow up to -693532978 and complaint #4560. Laying 2" line today.
+
| Follow up to -693532978 and complaint #4560. Laying 2 line today.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -315012153
 +
| 2013-12-24
 +
|
 +
| Follow up to -693532978 and complaint #4560. A functioning pop-off had been installed at the separator.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -693532978
 +
| 2013-12-12
 +
|
 +
| Landowner had complained of a smell of gas. I met with Jeff Burke of Rainbow Oil & Gas at the well site. Owner was venting gas into the 100 Barrel steel tank and allowing it to be released from the manhole in the tank. Owner stated the lines had not yet been laid due to right of way issues with the adjacent landowners. He stated work laying the line would begin early next week. All gas vented to the atmosphere must be flared, with the exception of gas released by a properly functioning relief device and gas released by controlled venting for testing, blowing down and cleaning out wells. Unlawful venting shall cease immediately and releif devise or flare must be installed if venting is to continue.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 695402086
 +
| 2014-10-15
 +
|
 +
| Asked to check on well by Supervisor. No noted violations.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 784577963
 
| 784577963
 
| 2013-07-30
 
| 2013-07-30
|
+
|  
| Administered surface casing integrity pressure test. 404' of 7" surface casing held required 370 psi for 30 minutes with 20 psi loss. Test passed.
+
| Administered surface casing integrity pressure test. 404' of 7 surface casing held required 370 psi for 30 minutes with 20 psi loss. Test passed.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:52, 14 July 2015

Well Details

Well ID: 34-105-23724
Loading map...
County: Meigs
Municipality:
Operator Name: RAINBOW OIL & GAS
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-07-16
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.12701854
Longitude: -81.92074853

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1086764085 2013-12-19 Check on annular disposal. Surface casing visible, lines hooked up and watertight. Field Visit or Inspection
-1213926962 2013-12-19 Inspected the annular disposal connections with Inspector Josh Garland. Jeff Burke (well owner) was on site as well. All connections are water tight. No leaks were observed during inspection.
1231047577 2013-09-05 Log suite ran. Cement op on backside of 4 1/2 production casing was1373 , Berea Sandstone from 1684-1694, perforated from 1684-1688 with 10 shots.
1241571933 2013-12-30 Follow up to -693532978 and complaint #4560. Lines laid and meter box being connected. Well is to be in production later today.
1373400870 2013-07-09 Building location and digging pits.
1374594658 2013-07-22 Witnessed surface cement job. 3 centralizers were ran at 64', 224', and at 352'. 417 feet of new 7 surface casing was set in 430 feet of 9 7/8 hole with 125 sacks of Class A cement with 1% gel, 100% excess used. Hole conditioned and good circulation established before cement pumped. During cement mix the pressures at the pump truck reached 500 psi and Formation cement shut down truck. Pressure was bled off the lines and the pipe was pulled a few feet out of the hole. Lines reconnected and circulation established immediately, continued on with job. The pressures reached 500 psi and the pipe began to move up out of the hole again, before the displacement was run. Again the pressure was released and the pipe pulled, now 10-15 feet out of hole. The job was restarted and cement returns were seen at the surface, before the displacement was ran, with less than 1 Bbl of returns. Pressured up for the third time and the well was shut in with casing full of cement. Company plans to cut off surface casing at ground level and drill out cement.
1374603088 2013-07-23 The cement had fallen back about a foot. It will be topped off with a sack of redi-mix. .
1375130319 2013-07-29 Drilling cement out of 7 surface casing and equalizing fluid in hole to get ready for casing pressure test.
1375219858 2013-07-30 Administered Annular Disposal surface casing integrity test. 370 psi was held on 404' of 7 surface casing for 15 minutes with 10 psi loss. Test passed. No Tanks.
1376317744 2013-08-12 Currently drilling at 1400 feet, down below the Injun Sand.
1377008100 2013-08-20 Currently drilling at 1800'. Berea Sandstone encountered at roughly 1740'. 4 1/2 casing being delivered today.
1378222918 2013-09-03 Witnessed longstring cement job. 1837' of 4 1/2 casing set in 1840' of 6 1/4 borehole with 33 sacks EA type II cement with expanders. Pressure test ran at 900 psi and pipe passed.
1388771081 2013-12-31 Associated with complaint # 4560 and inspection -693532978 . Received call from producer letting me know the lines have been completely connected.
1389200013 2014-01-08 Witnessed Longstring cement job. 1806 feet of new 4 1/2 casing set in 1810 feet of 6 1/4 inch borehole with 29 sacks of Class A cement. Circulation established. Casing pressure test administered with no loss of pressure over the required time.
18251560 2013-07-16 21 feet of 10 drive pipe was set to hold unconsolidated surface materials. Review of drilling rules with producer.
-1874430466 2014-08-19 Preliminary restoration requirments have been met.
1900512462 2013-09-06 Witnessed partial hydraulic frac job. Berea Sandstone shot from 1684 - 1688 with 10 shots. Formation treated with 45305 gallons fresh water and 140 sacks 20/40 sand. Breakdown 2249 psi, with and average pressure of 1958 psi.
226985605 2013-12-18 Follow up to -693532978 and complaint #4560. Laying 2 line today.
-315012153 2013-12-24 Follow up to -693532978 and complaint #4560. A functioning pop-off had been installed at the separator.
-693532978 2013-12-12 Landowner had complained of a smell of gas. I met with Jeff Burke of Rainbow Oil & Gas at the well site. Owner was venting gas into the 100 Barrel steel tank and allowing it to be released from the manhole in the tank. Owner stated the lines had not yet been laid due to right of way issues with the adjacent landowners. He stated work laying the line would begin early next week. All gas vented to the atmosphere must be flared, with the exception of gas released by a properly functioning relief device and gas released by controlled venting for testing, blowing down and cleaning out wells. Unlawful venting shall cease immediately and releif devise or flare must be installed if venting is to continue.
695402086 2014-10-15 Asked to check on well by Supervisor. No noted violations.
784577963 2013-07-30 Administered surface casing integrity pressure test. 404' of 7 surface casing held required 370 psi for 30 minutes with 20 psi loss. Test passed.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.