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Difference between revisions of "34-019-22375"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-019-22375
 
| Well ID: 34-019-22375
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.6472986683, -80.9480131712 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.64729867, -80.94801317 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Carroll County, Ohio|Carroll]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[CHESAPEAKE EXPLORATION LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2013-05-17
 
| Spud Date: 2013-05-17
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.6472986683
+
| Latitude: 40.64729867
 
|-
 
|-
| Longitude: -80.9480131712
+
| Longitude: -80.94801317
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2014-1
 +
| style="text-align:right;" | 39677.0
 +
| style="text-align:right;" | 36.0
 +
|
 +
|
 +
| style="text-align:right;" | 455.0
 +
| style="text-align:right;" | 36.0
 +
|-
 +
|-
 +
| 2014-2
 +
| style="text-align:right;" | 127496.0
 +
| style="text-align:right;" | 84.0
 +
|
 +
|
 +
| style="text-align:right;" | 1066.0
 +
| style="text-align:right;" | 84.0
 +
|-
 +
|-
 +
| 2014-3
 +
| style="text-align:right;" | 127690.0
 +
| style="text-align:right;" | 92.0
 +
|
 +
|
 +
| style="text-align:right;" | 621.0
 +
| style="text-align:right;" | 92.0
 +
|-
 +
|-
 +
| 2014-4
 +
| style="text-align:right;" | 105624.0
 +
| style="text-align:right;" | 92.0
 +
|
 +
|
 +
| style="text-align:right;" | 475.0
 +
| style="text-align:right;" | 92.0
 +
|-
 +
|-
 +
| 2015-1
 +
| style="text-align:right;" | 109675.0
 +
| style="text-align:right;" | 90.0
 +
|
 +
|
 +
| style="text-align:right;" | 642.0
 +
| style="text-align:right;" | 90.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 103:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -655220258
 
| 2013-05-17
 
|
 
| I was onsite to check the status of the drilling of the 17.5" surface casing hole. They are currently at 669' and are taking on 150 barrels of water with a chlorides level of 2800. They are concerned whether or not to set casing at their current location in the Big Injun due to the on take of water. Brett Farnsworth and Supervisor Tom Hill were contacted and decided to set casing at 885 feet, 15 feet short of the 900' permitted depth. The cement job should occur later tonight/mourning.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1316841479
 
| 1316841479
 
| 2013-05-17
 
| 2013-05-17
|
+
|  
| I was onsite to witness the cementing of the 13 3/8" casing set to 883 feet. The well was taken on large amounts of water during drilling but the hole was well conditioned before the cement was pumped by increasing circulation time and adding floseal. The job was pumped as planned with the cement weighed at 15.6ppg. There was a total of 45 barrels of cement returned to surface and the floats held at 875psi for 5 minutes with little fluid coming back. They are going to set their 9 5/8" casing around 1500'.
+
| I was onsite to witness the cementing of the 13 3/8 casing set to 883 feet. The well was taken on large amounts of water during drilling but the hole was well conditioned before the cement was pumped by increasing circulation time and adding floseal. The job was pumped as planned with the cement weighed at 15.6ppg. There was a total of 45 barrels of cement returned to surface and the floats held at 875psi for 5 minutes with little fluid coming back. They are going to set their 9 5/8 casing around 1500'.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1369760847
 
| 1369760847
 
| 2013-05-24
 
| 2013-05-24
|
+
|  
 
| I was at the site checking the drilling progress and obtaining cementing paperwork from the surface and intermediate cementing operations.  I met with Larry Williamson, drilling consultant.  The rig was in the process of drilling the curve at a total measured depth of 7,555' KB at 12:15 pm.
 
| I was at the site checking the drilling progress and obtaining cementing paperwork from the surface and intermediate cementing operations.  I met with Larry Williamson, drilling consultant.  The rig was in the process of drilling the curve at a total measured depth of 7,555' KB at 12:15 pm.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1370538125
 
| 1370538125
 
| 2013-05-29
 
| 2013-05-29
|
+
|  
 
+
| I went to the site to witness the cementing of the production casing.  The drilling contractor, Nomac 43, drilled an 8.75 diameter hole from beneath the base of the intermediate casing at 1622
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -655220258
 +
| 2013-05-17
 +
|
 +
| I was onsite to check the status of the drilling of the 17.5 surface casing hole. They are currently at 669' and are taking on 150 barrels of water with a chlorides level of 2800. They are concerned whether or not to set casing at their current location in the Big Injun due to the on take of water. Brett Farnsworth and Supervisor Tom Hill were contacted and decided to set casing at 885 feet, 15 feet short of the 900' permitted depth. The cement job should occur later tonight/mourning.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:25, 14 July 2015

Well Details

Well ID: 34-019-22375
Loading map...
County: Carroll
Municipality:
Operator Name: CHESAPEAKE EXPLORATION LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2013-05-17
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 40.64729867
Longitude: -80.94801317

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2014-1 39677.0 36.0 455.0 36.0
2014-2 127496.0 84.0 1066.0 84.0
2014-3 127690.0 92.0 621.0 92.0
2014-4 105624.0 92.0 475.0 92.0
2015-1 109675.0 90.0 642.0 90.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1316841479 2013-05-17 I was onsite to witness the cementing of the 13 3/8 casing set to 883 feet. The well was taken on large amounts of water during drilling but the hole was well conditioned before the cement was pumped by increasing circulation time and adding floseal. The job was pumped as planned with the cement weighed at 15.6ppg. There was a total of 45 barrels of cement returned to surface and the floats held at 875psi for 5 minutes with little fluid coming back. They are going to set their 9 5/8 casing around 1500'.
1369760847 2013-05-24 I was at the site checking the drilling progress and obtaining cementing paperwork from the surface and intermediate cementing operations. I met with Larry Williamson, drilling consultant. The rig was in the process of drilling the curve at a total measured depth of 7,555' KB at 12:15 pm.
1370538125 2013-05-29 I went to the site to witness the cementing of the production casing. The drilling contractor, Nomac 43, drilled an 8.75 diameter hole from beneath the base of the intermediate casing at 1622
-655220258 2013-05-17 I was onsite to check the status of the drilling of the 17.5 surface casing hole. They are currently at 669' and are taking on 150 barrels of water with a chlorides level of 2800. They are concerned whether or not to set casing at their current location in the Big Injun due to the on take of water. Brett Farnsworth and Supervisor Tom Hill were contacted and decided to set casing at 885 feet, 15 feet short of the 900' permitted depth. The cement job should occur later tonight/mourning.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.