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Difference between revisions of "34-073-22954"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-073-22954
 
| Well ID: 34-073-22954
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.5438384929, -82.3330353952 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.54383849, -82.3330354 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Hocking County, Ohio|Hocking]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[SCHMELZER PLUGGING LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1984-05-31
 
| Spud Date: 1984-05-31
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 2
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.5438384929
+
| Latitude: 39.54383849
 
|-
 
|-
| Longitude: -82.3330353952
+
| Longitude: -82.3330354
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 1551.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 889.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 2399.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 507.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 2300.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 330.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 259.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 180.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 118.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 365.0
 +
|
 +
|
 +
| style="text-align:right;" | 154.0
 +
| style="text-align:right;" | 365.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 130:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1339803441
 
| 2007-09-20
 
|
 
| An administrative inspection revealed that the well is in-compliance..
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1004468912
 
| 1004468912
 
| 2006-08-09
 
| 2006-08-09
|
+
|  
 
| An inspection revealed that the well is idle.  Production records show 1987 as the last year of production.  Mr. Michael Tucker states that both Sater wells need new pumps.  New identification will also be needed.
 
| An inspection revealed that the well is idle.  Production records show 1987 as the last year of production.  Mr. Michael Tucker states that both Sater wells need new pumps.  New identification will also be needed.
|
+
|  
| 9-9-05(A)10
+
|  
|
+
| Phone Call
|-
 
|-
 
| 1004468912
 
| 2006-08-09
 
|
 
| An inspection revealed that the well is idle.  Production records show 1987 as the last year of production.  Mr. Michael Tucker states that both Sater wells need new pumps.  New identification will also be needed.
 
|
 
| NONE E
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1176740427
 
| 1176740427
 
| 2007-04-11
 
| 2007-04-11
|
+
|  
 
| A telephone conversation held with Mr. Michael Tucker on 4/11/2007 revealed that the well was not in-compliance.
 
| A telephone conversation held with Mr. Michael Tucker on 4/11/2007 revealed that the well was not in-compliance.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1246291248
 
| 1246291248
 
| 2007-06-06
 
| 2007-06-06
|
+
|  
 
| An inspection revealed non-compliance.
 
| An inspection revealed non-compliance.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1339803441
 +
| 2007-09-20
 +
|
 +
| An administrative inspection revealed that the well is in-compliance..
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1465361632
 
| 1465361632
 
| 2007-08-13
 
| 2007-08-13
|
+
|  
 
| An attempt to contact Mr. Michael Tucker by telephone was not successful.  Mr. Dale Tucker states that the engine work has been completed on the Sater well.  He states that he will have Michael Tucker return my call.  An interview will be conducted with the landowner to see if house gas is now being received from these wells.
 
| An attempt to contact Mr. Michael Tucker by telephone was not successful.  Mr. Dale Tucker states that the engine work has been completed on the Sater well.  He states that he will have Michael Tucker return my call.  An interview will be conducted with the landowner to see if house gas is now being received from these wells.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 476604083
 
| 476604083
 
| 2007-07-17
 
| 2007-07-17
|
+
|  
 
| A follow-up inspection revealed that the 100 bbl tank has been replaced.  The previous tank contained large hole at top of tank.  The engine for P#2873 is being reparied by Ohio Pump and Supply according to Mr. Michael Tucker.  He states that the electric motor from P#2954 will be placed on this well.  The engine will be placed on the P#2954.  A new gas line is being ran to residential dwelling.  Mr. Michael Tucker provided a run ticket from Ohio Oil Gathering Corporation showing commerical production from the Sater #1 & Sater #2 wells (common tank battery) on 7/3/2007.  Records indicate that the last year of production was 1999.
 
| A follow-up inspection revealed that the 100 bbl tank has been replaced.  The previous tank contained large hole at top of tank.  The engine for P#2873 is being reparied by Ohio Pump and Supply according to Mr. Michael Tucker.  He states that the electric motor from P#2954 will be placed on this well.  The engine will be placed on the P#2954.  A new gas line is being ran to residential dwelling.  Mr. Michael Tucker provided a run ticket from Ohio Oil Gathering Corporation showing commerical production from the Sater #1 & Sater #2 wells (common tank battery) on 7/3/2007.  Records indicate that the last year of production was 1999.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 753353878
 
| 753353878
 
| 2007-08-27
 
| 2007-08-27
|
+
|  
 
| A follow-up inspection revealed that an engine has been placed on this well.  Identification was not observed and is required.  An interview with the landowner, confirmed that gas is not being received from either of the Sater wells.  The gas line is still disconnected.  Mr. Michael Tucker, the well owner, has not returned any phone calls.
 
| A follow-up inspection revealed that an engine has been placed on this well.  Identification was not observed and is required.  An interview with the landowner, confirmed that gas is not being received from either of the Sater wells.  The gas line is still disconnected.  Mr. Michael Tucker, the well owner, has not returned any phone calls.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 755077191
 
| 755077191
 
| 2007-01-04
 
| 2007-01-04
|
+
|  
 
| A follow-up inspection conducted on 1/4/2007 revealed that the well is still idle. The owner, Mr. Michael Tucker, stated that both the Sater #1 and #2 wells have bad pumps.  Mr. Tucker also stated that the landowner, at one time was receiving house gas from these wells.  An interview conducted with the landowner, on 1/4/2007 confirmed that no house gas is being received.  The landowner stated that they are utilizing propane to heat their house.  The gas line from the well to the house has been cut.  Also, noted was that a 110bbl tank contained a hole near the top of the tank, the electrical box was lying on the ground and a power line, in the pasture, was low.  Identification has been provided for both Sater#1 and Sater #2 wells.  This case will be handed over to management.
 
| A follow-up inspection conducted on 1/4/2007 revealed that the well is still idle. The owner, Mr. Michael Tucker, stated that both the Sater #1 and #2 wells have bad pumps.  Mr. Tucker also stated that the landowner, at one time was receiving house gas from these wells.  An interview conducted with the landowner, on 1/4/2007 confirmed that no house gas is being received.  The landowner stated that they are utilizing propane to heat their house.  The gas line from the well to the house has been cut.  Also, noted was that a 110bbl tank contained a hole near the top of the tank, the electrical box was lying on the ground and a power line, in the pasture, was low.  Identification has been provided for both Sater#1 and Sater #2 wells.  This case will be handed over to management.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| PL16175
 
| PL16175
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 17:27, 14 July 2015

Well Details

Well ID: 34-073-22954
Loading map...
County: Hocking
Municipality:
Operator Name: SCHMELZER PLUGGING LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-05-31
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.54383849
Longitude: -82.3330354

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 1551.0 889.0
1986-0 2399.0 507.0
1987-0 2300.0 330.0
2010-0 0.0 0.0
2011-0 0.0 259.0
2012-0 0.0 180.0
2013-0 0.0 118.0
2014-0 0.0 365.0 154.0 365.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1004468912 2006-08-09 An inspection revealed that the well is idle. Production records show 1987 as the last year of production. Mr. Michael Tucker states that both Sater wells need new pumps. New identification will also be needed. Phone Call
1176740427 2007-04-11 A telephone conversation held with Mr. Michael Tucker on 4/11/2007 revealed that the well was not in-compliance.
1246291248 2007-06-06 An inspection revealed non-compliance.
-1339803441 2007-09-20 An administrative inspection revealed that the well is in-compliance..
1465361632 2007-08-13 An attempt to contact Mr. Michael Tucker by telephone was not successful. Mr. Dale Tucker states that the engine work has been completed on the Sater well. He states that he will have Michael Tucker return my call. An interview will be conducted with the landowner to see if house gas is now being received from these wells.
476604083 2007-07-17 A follow-up inspection revealed that the 100 bbl tank has been replaced. The previous tank contained large hole at top of tank. The engine for P#2873 is being reparied by Ohio Pump and Supply according to Mr. Michael Tucker. He states that the electric motor from P#2954 will be placed on this well. The engine will be placed on the P#2954. A new gas line is being ran to residential dwelling. Mr. Michael Tucker provided a run ticket from Ohio Oil Gathering Corporation showing commerical production from the Sater #1 & Sater #2 wells (common tank battery) on 7/3/2007. Records indicate that the last year of production was 1999.
753353878 2007-08-27 A follow-up inspection revealed that an engine has been placed on this well. Identification was not observed and is required. An interview with the landowner, confirmed that gas is not being received from either of the Sater wells. The gas line is still disconnected. Mr. Michael Tucker, the well owner, has not returned any phone calls.
755077191 2007-01-04 A follow-up inspection conducted on 1/4/2007 revealed that the well is still idle. The owner, Mr. Michael Tucker, stated that both the Sater #1 and #2 wells have bad pumps. Mr. Tucker also stated that the landowner, at one time was receiving house gas from these wells. An interview conducted with the landowner, on 1/4/2007 confirmed that no house gas is being received. The landowner stated that they are utilizing propane to heat their house. The gas line from the well to the house has been cut. Also, noted was that a 110bbl tank contained a hole near the top of the tank, the electrical box was lying on the ground and a power line, in the pasture, was low. Identification has been provided for both Sater#1 and Sater #2 wells. This case will be handed over to management.
PL16175 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.