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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-111-22477 | | Well ID: 34-111-22477 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 39.85425802, -81.12609188 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Monroe County, Ohio|Monroe]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[NORTHWOOD ENERGY CORP]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1981-07-25 | | Spud Date: 1981-07-25 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 39. | + | | Latitude: 39.85425802 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.12609188 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1993-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2003-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2004-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2005-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2006-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2007-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2008-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2009-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2010-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2011-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2012-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2013-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 175: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| -1082963784 | | -1082963784 | ||
| 2013-12-10 | | 2013-12-10 | ||
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | | | + | | |
− | | | + | | |
− | | | + | | Informal Letter |
|- | |- | ||
|- | |- | ||
− | | - | + | | -1082963784 |
− | | | + | | 2013-12-10 |
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | | | + | | |
− | | | + | | |
− | | | + | | Phone Call |
|- | |- | ||
|- | |- | ||
− | | - | + | | -1082963784 |
− | | 2013-12- | + | | 2013-12-10 |
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | | | + | | |
− | | | + | | |
− | | | + | | Phone Call |
|- | |- | ||
|- | |- | ||
− | | - | + | | -1082963784 |
− | | | + | | 2013-12-10 |
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | | | + | | |
− | | | + | | |
− | | | + | | Phone Call |
|- | |- | ||
|- | |- | ||
− | | - | + | | -1082963784 |
− | | | + | | 2013-12-10 |
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | | | + | | |
− | | | + | | |
− | | | + | | Phone Call |
|- | |- | ||
|- | |- | ||
− | | - | + | | -1082963784 |
− | | | + | | 2013-12-10 |
− | | | + | | |
− | | | + | | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5'' production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. |
− | + | | | |
− | + | | | |
− | + | | | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | | | ||
− | | | ||
− | | | ||
|- | |- | ||
|- | |- | ||
| 1181162750 | | 1181162750 | ||
| 2007-06-05 | | 2007-06-05 | ||
− | | | + | | |
| No violations noted, well is equipped with pump jack and tubing&rods and 1-100 bbl tank,tank site will need better dike construction when SPCC rules go into effect. | | No violations noted, well is equipped with pump jack and tubing&rods and 1-100 bbl tank,tank site will need better dike construction when SPCC rules go into effect. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1235063472 | | 1235063472 | ||
| 2009-02-05 | | 2009-02-05 | ||
− | | | + | | |
| WELL HAD RODS AND TUBING AND PUMP JACK AT ONE TIME .RODS WERE PULLED OUT.PUMPJACK REMOVED.WELL IS IDLE AT PRESENT TIME.WILL CALL MIKE CORP. | | WELL HAD RODS AND TUBING AND PUMP JACK AT ONE TIME .RODS WERE PULLED OUT.PUMPJACK REMOVED.WELL IS IDLE AT PRESENT TIME.WILL CALL MIKE CORP. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1268851680 | | 1268851680 | ||
| 2010-03-15 | | 2010-03-15 | ||
− | | | + | | |
| Called Mike Corp on this NOV.There was a swab rig in the location. There are two 300bbl frac tanks that are 1/2 full. One is leaking. I told mike to get water truck in and remove brine out of tanks and get them back on Jr. Burkhart's farm. Put well into working order as the location dries up.No id at tank or wellhead. | | Called Mike Corp on this NOV.There was a swab rig in the location. There are two 300bbl frac tanks that are 1/2 full. One is leaking. I told mike to get water truck in and remove brine out of tanks and get them back on Jr. Burkhart's farm. Put well into working order as the location dries up.No id at tank or wellhead. | ||
− | | | + | | |
− | | | + | | |
− | + | | | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | | | ||
|- | |- | ||
|- | |- | ||
| 1389107407 | | 1389107407 | ||
| 2014-01-07 | | 2014-01-07 | ||
− | | | + | | |
| Administrative Inspection to document that contact has been made with Bill Arnholt with Northwood energy in regards to the well being idle and the 2 unresolved violations numbering 208127806 & 1393718879, Mr. Arnholt says they will apply for a plugging permit. | | Administrative Inspection to document that contact has been made with Bill Arnholt with Northwood energy in regards to the well being idle and the 2 unresolved violations numbering 208127806 & 1393718879, Mr. Arnholt says they will apply for a plugging permit. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1393718879 | ||
+ | | 2010-01-04 | ||
+ | | | ||
+ | | FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 1402266643 | | 1402266643 | ||
| 2014-06-08 | | 2014-06-08 | ||
− | | | + | | |
− | | | + | | The said well plugging took place on 05/27/2014 with Davis Well Svc rig on the hole and Cemennco cement services, the bottom was tagged at 2,285' by the rig's wireline tools and 2'' tubing was ran into 2,270' and a bottom plug was set using 30 sacks of class A cement, the 4.5'' production casing was ripped at 610' and pulled to a free point at 484' , a solid plug was set covering the bottom of the surface pipe to surface from 484' to surface with the casing cut off 30'' below the ground surface and a permanent marker installed. Contractors were on site removing the production equipment. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1506730562 | ||
+ | | 2015-04-23 | ||
+ | | | ||
+ | | Compliance Notices # -1393718879 & # -2108127806 were resolved on this day, the said well has been plugged resolving the violations. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1628218038 | ||
+ | | 2013-12-11 | ||
+ | | | ||
+ | | On this day I spoke with Bill Arnholt with Northwood energy and He confirmed that the well 4.5'' production casing has a hole in it up high possibly from a coal seam, They will file for a plugging permit. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -186975000 | ||
+ | | 2010-01-04 | ||
+ | | | ||
+ | | FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -2108127806 | ||
+ | | 2010-01-04 | ||
+ | | | ||
+ | | Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -2117874206 | ||
+ | | 2014-05-27 | ||
+ | | | ||
+ | | Glen Davis rig is plugging well with Cemenco placing the plugs. Well circulated good. Set bottom plug thru 2.375''upset 8 round tubing. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 587938114 | ||
+ | | 2014-09-23 | ||
+ | | | ||
+ | | Final Restoration status check inspection found the well site meets ORC 1509.072 will all equipment removed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -659286123 | ||
+ | | 2010-01-04 | ||
+ | | | ||
+ | | FOLLOW UP TO NOV # -1393718879 FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy. No production reports filed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-111-22477 | Loading map...
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County: Monroe | |
Municipality: | |
Operator Name: NORTHWOOD ENERGY CORP | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1981-07-25 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 39.85425802 | |
Longitude: -81.12609188 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1993-0 | 0.0 | 0.0 | ||||
2003-0 | 0.0 | 0.0 | ||||
2004-0 | 0.0 | 0.0 | ||||
2005-0 | 0.0 | 0.0 | ||||
2006-0 | 0.0 | 0.0 | ||||
2007-0 | 0.0 | 0.0 | ||||
2008-0 | 0.0 | 0.0 | ||||
2009-0 | 0.0 | 0.0 | ||||
2010-0 | 0.0 | 0.0 | ||||
2011-0 | 0.0 | 0.0 | ||||
2012-0 | 0.0 | 0.0 | ||||
2013-0 | 0.0 | 0.0 | ||||
2014-0 | 0.0 | 0.0 | 0.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | Informal Letter | |||
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | Phone Call | |||
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | Phone Call | |||
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | Phone Call | |||
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | Phone Call | |||
-1082963784 | 2013-12-10 | Compliance agreement # 1393718879 & 2108127806 follow up inspection found the well idle with only 4.5 production casing present with no production equipment hooked up or present and no current gas sales chart in the meter. Production records show no reported production in the Database. Instructions are as follows- File for a plugging permit within 30 days. ODNR contact- Monroe Co Inspector Bill Stolarik 1-740-507-6592. | ||||
1181162750 | 2007-06-05 | No violations noted, well is equipped with pump jack and tubing&rods and 1-100 bbl tank,tank site will need better dike construction when SPCC rules go into effect. | ||||
1235063472 | 2009-02-05 | WELL HAD RODS AND TUBING AND PUMP JACK AT ONE TIME .RODS WERE PULLED OUT.PUMPJACK REMOVED.WELL IS IDLE AT PRESENT TIME.WILL CALL MIKE CORP. | ||||
1268851680 | 2010-03-15 | Called Mike Corp on this NOV.There was a swab rig in the location. There are two 300bbl frac tanks that are 1/2 full. One is leaking. I told mike to get water truck in and remove brine out of tanks and get them back on Jr. Burkhart's farm. Put well into working order as the location dries up.No id at tank or wellhead. | ||||
1389107407 | 2014-01-07 | Administrative Inspection to document that contact has been made with Bill Arnholt with Northwood energy in regards to the well being idle and the 2 unresolved violations numbering 208127806 & 1393718879, Mr. Arnholt says they will apply for a plugging permit. | ||||
-1393718879 | 2010-01-04 | FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||||
1402266643 | 2014-06-08 | The said well plugging took place on 05/27/2014 with Davis Well Svc rig on the hole and Cemennco cement services, the bottom was tagged at 2,285' by the rig's wireline tools and 2 tubing was ran into 2,270' and a bottom plug was set using 30 sacks of class A cement, the 4.5 production casing was ripped at 610' and pulled to a free point at 484' , a solid plug was set covering the bottom of the surface pipe to surface from 484' to surface with the casing cut off 30 below the ground surface and a permanent marker installed. Contractors were on site removing the production equipment. | ||||
-1506730562 | 2015-04-23 | Compliance Notices # -1393718879 & # -2108127806 were resolved on this day, the said well has been plugged resolving the violations. | ||||
-1628218038 | 2013-12-11 | On this day I spoke with Bill Arnholt with Northwood energy and He confirmed that the well 4.5 production casing has a hole in it up high possibly from a coal seam, They will file for a plugging permit. | ||||
-186975000 | 2010-01-04 | FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||||
-2108127806 | 2010-01-04 | Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy.No production reports filed. | ||||
-2117874206 | 2014-05-27 | Glen Davis rig is plugging well with Cemenco placing the plugs. Well circulated good. Set bottom plug thru 2.375upset 8 round tubing. | ||||
587938114 | 2014-09-23 | Final Restoration status check inspection found the well site meets ORC 1509.072 will all equipment removed. | ||||
-659286123 | 2010-01-04 | FOLLOW UP TO NOV # -1393718879 FOLLOW UP TO NOV # -2108127806 Well is idle and not capable. I called and talked to Bill Arnholt of Northwood Energy. No production reports filed. |
For data sources see[2]