X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-167-62158"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-167-62158
 
| Well ID: 34-167-62158
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.5148544407, -81.2392583715 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.51527606, -81.23938409 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Washington County, Ohio|Washington]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[HISTORIC OWNER]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing:
+
| Well Status:  
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.5148544407
+
| Latitude: 39.51527606
 
|-
 
|-
| Longitude: -81.2392583715
+
| Longitude: -81.23938409
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -859074665
 
| 2004-04-02
 
|
 
| Inspection this day found well not in production, believe this is on the bid list? - do we have access to bid list? - tank not in use, no ID's, well not equipped to produce.  Needs plugged.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1339782456
 
| 1339782456
 
| 2012-06-14
 
| 2012-06-14
|
+
|  
| My inspection this day to update I/O file.  New matrix score is 135, photos taken and this inspection added.  Project consists of 2 80+ bbl tanks sitting right off shoulder of township road 500' apart.  The north tank sits at the entrance of the barely existing lease road - drop off is sharp and steep with well located almost at creek level.  Top of casing is 2-3' above ground level with very old wellhead on 6.25" OD casing.  Wellhead is open to the air and when rock is dropped, find fluid level very far downhole.  Just above the well sits gumpy circle of oil where old tank has set - rotted completely away but should remove this contaminated soil to prevent runoff into creek.  Just below the well is spot about 10 x 10' full of water - may not have anything to do with well.  Local "experts" say this well is Peaker @750' deep.
+
| My inspection this day to update I/O file.  New matrix score is 135, photos taken and this inspection added.  Project consists of 2 80+ bbl tanks sitting right off shoulder of township road 500' apart.  The north tank sits at the entrance of the barely existing lease road - drop off is sharp and steep with well located almost at creek level.  Top of casing is 2-3' above ground level with very old wellhead on 6.25 OD casing.  Wellhead is open to the air and when rock is dropped, find fluid level very far downhole.  Just above the well sits gumpy circle of oil where old tank has set - rotted completely away but should remove this contaminated soil to prevent runoff into creek.  Just below the well is spot about 10 x 10' full of water - may not have anything to do with well.  Local experts say this well is Peaker @750' deep.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1374166611
 
| 1374166611
 
| 2013-07-17
 
| 2013-07-17
|
+
|  
 
| My inspection this day to check well after the flooding rains to see of oil overflowed well or otherwise got on ground.  I found no indication that oil had spilled from the well - undoubtedly, the well had been under water.
 
| My inspection this day to check well after the flooding rains to see of oil overflowed well or otherwise got on ground.  I found no indication that oil had spilled from the well - undoubtedly, the well had been under water.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -859074665
 +
| 2004-04-02
 +
|
 +
| Inspection this day found well not in production, believe this is on the bid list? - do we have access to bid list? - tank not in use, no ID's, well not equipped to produce.  Needs plugged.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 897426354
 
| 897426354
 
| 2013-07-31
 
| 2013-07-31
|
+
|  
 
| Inspection this day with Gene Chini to discuss plugging options, verify data.
 
| Inspection this day with Gene Chini to discuss plugging options, verify data.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 03:18, 15 July 2015

Well Details

Well ID: 34-167-62158
Loading map...
County: Washington
Municipality:
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status:
Violations: 0
Latitude: 39.51527606
Longitude: -81.23938409

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1339782456 2012-06-14 My inspection this day to update I/O file. New matrix score is 135, photos taken and this inspection added. Project consists of 2 80+ bbl tanks sitting right off shoulder of township road 500' apart. The north tank sits at the entrance of the barely existing lease road - drop off is sharp and steep with well located almost at creek level. Top of casing is 2-3' above ground level with very old wellhead on 6.25 OD casing. Wellhead is open to the air and when rock is dropped, find fluid level very far downhole. Just above the well sits gumpy circle of oil where old tank has set - rotted completely away but should remove this contaminated soil to prevent runoff into creek. Just below the well is spot about 10 x 10' full of water - may not have anything to do with well. Local experts say this well is Peaker @750' deep.
1374166611 2013-07-17 My inspection this day to check well after the flooding rains to see of oil overflowed well or otherwise got on ground. I found no indication that oil had spilled from the well - undoubtedly, the well had been under water.
-859074665 2004-04-02 Inspection this day found well not in production, believe this is on the bid list? - do we have access to bid list? - tank not in use, no ID's, well not equipped to produce. Needs plugged.
897426354 2013-07-31 Inspection this day with Gene Chini to discuss plugging options, verify data.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.