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Difference between revisions of "34-073-21521"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-073-21521
 
| Well ID: 34-073-21521
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.4559356883, -82.4207234807 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.45593569, -82.42072348 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Hocking County, Ohio|Hocking]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[KILBARGER INVESTMENTS INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2008-03-12
 
| Spud Date: 2008-03-12
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 2
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.4559356883
+
| Latitude: 39.45593569
 
|-
 
|-
| Longitude: -82.4207234807
+
| Longitude: -82.42072348
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 291.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 59.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 22.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 53.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 37.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 38.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 36.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 35.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 94.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 256:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1021229757
 
| -1021229757
 
| 2008-02-19
 
| 2008-02-19
|
+
|  
 
| Checked on plugging status.  An inspection revealed that the company will be utilizing Appalachian Well Service to cut the 5.5 inch casing.
 
| Checked on plugging status.  An inspection revealed that the company will be utilizing Appalachian Well Service to cut the 5.5 inch casing.
|
+
|
|
+
|
|
+
| Compliance Notice
 +
|-
 +
|-
 +
| 1052037959
 +
| 2008-03-14
 +
|
 +
| An inspection revealed that the company is removing dirt tracked onto Rauber Road.  80 sacks of cement was placed behind 4.5 inch casing on 3/12/2008.  Kilbarger has been instructed on several occassions to acquire a plug/back permit for this well.  This well was plugged back to the Berea.  During the process, the ownership of this well changed from Jeanie Enterprises to Kilbarger Investments.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -1055103105
 
| -1055103105
 
| 2008-02-20
 
| 2008-02-20
|
+
|  
 
| An inspection revealed that 5.5 inch casing was cut at 2100 feet.  Kilbarger is having problems retrieving the casing.  Cement contractor made attempt to circulate on the casing.  The casing did not free up nor circulate.  A 200ft cement was plug was set thru tubing.
 
| An inspection revealed that 5.5 inch casing was cut at 2100 feet.  Kilbarger is having problems retrieving the casing.  Cement contractor made attempt to circulate on the casing.  The casing did not free up nor circulate.  A 200ft cement was plug was set thru tubing.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| -1923364678
 
| 2008-02-25
 
|
 
| Witnessed pre-cast set on 7 inch seat.  Kilbarger, plugging contractor, was again informed that a plug-back permit would be required.  Spoke with Mr. Mike McCormac, DMRM, regarding the setback distance from existing Berea wells.  Mr. McCormac states that this well will meet setback requirement if plugged back to the Berea.
 
|
 
|
 
|
 
|-
 
|-
 
| -2145846754
 
| 2008-06-16
 
|
 
| Witnessed bottom plug.
 
|
 
|
 
|
 
|-
 
|-
 
| -450759647
 
| 2008-02-21
 
|
 
| An inspection revealed that Appalachian Well Service made a second attempt to cut casing.  The casing was cut at 1717 feet.  5.5 inch casing is being pulled.  Appalachian will be back to log the hole.  Jim Kilbarger states that if the Berea looks good they plan to purchase this well.  He was informed that a plug-back permit would then be required.
 
|
 
|
 
|
 
|-
 
|-
 
| -943234284
 
| 2008-06-17
 
|
 
| Checked on plugging.  Kilbarger is pulling 4.5" casing.
 
|
 
|
 
|
 
|-
 
|-
 
| 1052037959
 
| 2008-03-14
 
|
 
| An inspection revealed that the company is removing dirt tracked onto Rauber Road.  80 sacks of cement was placed behind 4.5 inch casing on 3/12/2008.  Kilbarger has been instructed on several occassions to acquire a plug/back permit for this well.  This well was plugged back to the Berea.  During the process, the ownership of this well changed from Jeanie Enterprises to Kilbarger Investments.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1114454664
 
| 1114454664
 
| 2008-06-18
 
| 2008-06-18
|
+
|  
 
| Checked on plugging.  ID plate has been installed.  Company grading well site.
 
| Checked on plugging.  ID plate has been installed.  Company grading well site.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1383679330
 
| 1383679330
 
| 2007-08-21
 
| 2007-08-21
|
+
|  
 
| An inspection revealed that this well is idle and not capable of production.  During the inspection, it was observed that the well did not contain an engine or a motor.  This well may be routed to a tank battery located across the road (common tank battery).  The production lines to this tank battery do not appear to be connected.  The identification displayed at the well did not contain the current owner and will need to be updated.
 
| An inspection revealed that this well is idle and not capable of production.  During the inspection, it was observed that the well did not contain an engine or a motor.  This well may be routed to a tank battery located across the road (common tank battery).  The production lines to this tank battery do not appear to be connected.  The identification displayed at the well did not contain the current owner and will need to be updated.
|
+
|  
| 9-9-05(A)10
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 1383679330
+
| 1408377692
| 2007-08-21
+
| 2009-05-15
|
+
|  
| An inspection revealed that this well is idle and not capable of production.  During the inspection, it was observed that the well did not contain an engine or a motorThis well may be routed to a tank battery located across the road (common tank battery)The production lines to this tank battery do not appear to be connectedThe identification displayed at the well did not contain the current owner and will need to be updated.
+
| An inspection of the property revealed a 50' section of 1 black plastic line observed above ground.  The well location and lease road is pasture field and the vegetative growth is acceptableThe tank battery is located across the street and being utilized by the remaining that had been left in productionAt the conclusion of the inspection, an attempt to meet with the landowner was not successful.  A business card was then leftReceived a telephone call from the landowner regarding the final restoration.  The landowner states that she will consult with her husband regarding the plastic line, as to whether he may have wanted the line.
|
+
|  
| NONE
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 1408377692
+
| -1923364678
| 2009-05-15
+
| 2008-02-25
|
+
|  
| An inspection of the property revealed a 50' section of 1" black plastic line observed above groundThe well location and lease road is pasture field and the vegetative growth is acceptable.  The tank battery is located across the street and being utilized by the remaining that had been left in productionAt the conclusion of the inspection, an attempt to meet with the landowner was not successful. A business card was then left.  Received a telephone call from the landowner regarding the final restorationThe landowner states that she will consult with her husband regarding the plastic line, as to whether he may have wanted the line.
+
| Witnessed pre-cast set on 7 inch seatKilbarger, plugging contractor, was again informed that a plug-back permit would be requiredSpoke with Mr. Mike McCormac, DMRM, regarding the setback distance from existing Berea wellsMr. McCormac states that this well will meet setback requirement if plugged back to the Berea.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2114033034
 
| 2114033034
 
| 2008-02-15
 
| 2008-02-15
|
+
|  
 
| Checked on plugging.  Company is pulling rods and tubing.
 
| Checked on plugging.  Company is pulling rods and tubing.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -2145846754
 +
| 2008-06-16
 +
|
 +
| Witnessed bottom plug.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 350507654
 
| 350507654
 
| 2008-06-13
 
| 2008-06-13
|
+
|  
 
| Checked on plugging.  No activity observed.
 
| Checked on plugging.  No activity observed.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -450759647
 +
| 2008-02-21
 +
|
 +
| An inspection revealed that Appalachian Well Service made a second attempt to cut casing.  The casing was cut at 1717 feet.  5.5 inch casing is being pulled.  Appalachian will be back to log the hole.  Jim Kilbarger states that if the Berea looks good they plan to purchase this well.  He was informed that a plug-back permit would then be required.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -943234284
 +
| 2008-06-17
 +
|
 +
| Checked on plugging.  Kilbarger is pulling 4.5 casing.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 07:01, 15 July 2015

Well Details

Well ID: 34-073-21521
Loading map...
County: Hocking
Municipality:
Operator Name: KILBARGER INVESTMENTS INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2008-03-12
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.45593569
Longitude: -82.42072348

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 0.0 291.0
1985-0 0.0 59.0
1987-0 0.0 0.0
1988-0 0.0 0.0
1989-0 0.0 0.0
1990-0 0.0 0.0
1991-0 0.0 22.0
1992-0 0.0 53.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 37.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 38.0
2004-0 0.0 36.0
2005-0 0.0 0.0
2006-0 0.0 35.0
2007-0 0.0 0.0
2008-0 0.0 94.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1021229757 2008-02-19 Checked on plugging status. An inspection revealed that the company will be utilizing Appalachian Well Service to cut the 5.5 inch casing. Compliance Notice
1052037959 2008-03-14 An inspection revealed that the company is removing dirt tracked onto Rauber Road. 80 sacks of cement was placed behind 4.5 inch casing on 3/12/2008. Kilbarger has been instructed on several occassions to acquire a plug/back permit for this well. This well was plugged back to the Berea. During the process, the ownership of this well changed from Jeanie Enterprises to Kilbarger Investments.
-1055103105 2008-02-20 An inspection revealed that 5.5 inch casing was cut at 2100 feet. Kilbarger is having problems retrieving the casing. Cement contractor made attempt to circulate on the casing. The casing did not free up nor circulate. A 200ft cement was plug was set thru tubing.
1114454664 2008-06-18 Checked on plugging. ID plate has been installed. Company grading well site.
1383679330 2007-08-21 An inspection revealed that this well is idle and not capable of production. During the inspection, it was observed that the well did not contain an engine or a motor. This well may be routed to a tank battery located across the road (common tank battery). The production lines to this tank battery do not appear to be connected. The identification displayed at the well did not contain the current owner and will need to be updated.
1408377692 2009-05-15 An inspection of the property revealed a 50' section of 1 black plastic line observed above ground. The well location and lease road is pasture field and the vegetative growth is acceptable. The tank battery is located across the street and being utilized by the remaining that had been left in production. At the conclusion of the inspection, an attempt to meet with the landowner was not successful. A business card was then left. Received a telephone call from the landowner regarding the final restoration. The landowner states that she will consult with her husband regarding the plastic line, as to whether he may have wanted the line.
-1923364678 2008-02-25 Witnessed pre-cast set on 7 inch seat. Kilbarger, plugging contractor, was again informed that a plug-back permit would be required. Spoke with Mr. Mike McCormac, DMRM, regarding the setback distance from existing Berea wells. Mr. McCormac states that this well will meet setback requirement if plugged back to the Berea.
2114033034 2008-02-15 Checked on plugging. Company is pulling rods and tubing.
-2145846754 2008-06-16 Witnessed bottom plug.
350507654 2008-06-13 Checked on plugging. No activity observed.
-450759647 2008-02-21 An inspection revealed that Appalachian Well Service made a second attempt to cut casing. The casing was cut at 1717 feet. 5.5 inch casing is being pulled. Appalachian will be back to log the hole. Jim Kilbarger states that if the Berea looks good they plan to purchase this well. He was informed that a plug-back permit would then be required.
-943234284 2008-06-17 Checked on plugging. Kilbarger is pulling 4.5 casing.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.