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Difference between revisions of "34-005-21791"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-005-21791
 
| Well ID: 34-005-21791
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.8959635406, -82.1558832874 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.89594361, -82.15612288 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Ashland County, Ohio|Ashland]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[DEEP RESOURCES LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1976-08-27
 
| Spud Date: 1976-08-27
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 5
+
| Violations: 0
 
|-
 
|-
| Latitude: 40.8959635406
+
| Latitude: 40.89594361
 
|-
 
|-
| Longitude: -82.1558832874
+
| Longitude: -82.15612288
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 13.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 67:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 +
|-
 +
| -1082935222
 +
| 2006-12-29
 +
|
 +
| NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 
|-
 
|-
 
| -1082935222
 
| -1082935222
 
| 2006-12-29
 
| 2006-12-29
|
+
|  
 
| NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi.
 
| NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi.
|
+
|
|
+
|
|
+
| Compliance Notice
 +
|-
 +
|-
 +
| -1082935222
 +
| 2006-12-29
 +
|
 +
| NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi.
 +
|
 +
|
 +
| Field Visit or Inspection
 +
|-
 +
|-
 +
| -1082935222
 +
| 2006-12-29
 +
|
 +
| NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi.
 +
|
 +
|
 +
| Compliance Notice
 +
|-
 +
|-
 +
| 111057061
 +
| 2010-04-06
 +
|
 +
| Injection and annulus pressure test.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1116355295
 +
| 2005-05-17
 +
|
 +
| Injection well test. GPS location and update to RBDMS.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -111963044
 
| -111963044
 
| 2007-03-30
 
| 2007-03-30
|
+
|  
 
| Injection and annulaus pressure test. Pressures are equalized at 350 psi.
 
| Injection and annulaus pressure test. Pressures are equalized at 350 psi.
|
+
|  
| 9-5-09[C]
+
|  
|
+
|
 +
|-
 +
|-
 +
| 1192038614
 +
| 2007-10-10
 +
|
 +
| Injection and annulus pressure test. Pressures are equalized at 330 psi. Suspended well operation at this time.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1350741638
 +
| 2012-06-04
 +
|
 +
| Inspect Well. Annulus valve was replaced. Box needs repair.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1371742425
 +
| 2013-06-20
 +
|
 +
| Request from operator to witness well plugging.  The well was plugged with 9 sack grout.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1376581904
 +
| 2013-08-15
 +
|
 +
| The site needs to be graded and a pipe rack with 1 inch tubing removed to approve final restoration.  Randy at Deep Resources was advised.  He stated he would call when work is complete.
 +
|
 +
|
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -1464663205
 
| -1464663205
 
| 2013-05-08
 
| 2013-05-08
|
+
|  
 
| Operator pickled and cleaned casing with acid. Run tubing and packer with new rubbers and cage. Pressure test of well did not pass. Significant loss of pressure when tested. Five times a joint of pipe was pulled up, packer set, loaded with water and pressure tested. Each test failed. Tool pusher reported the packer would set down at a depth of 268 feet below grade. Pulled packer up and set at 257 ft. above obstruction. Pressure tested ok at 257. The following day the packer was set and tested at 293 ft., below obstruction. Pressure test failed. Hole in casing about 268 feet. Reviewed old records the original well was drilled 8 to 10 inches from current hole. Due to casing being pushed out of bore hole by shooting with nitroglycerin. Well will be plugged.
 
| Operator pickled and cleaned casing with acid. Run tubing and packer with new rubbers and cage. Pressure test of well did not pass. Significant loss of pressure when tested. Five times a joint of pipe was pulled up, packer set, loaded with water and pressure tested. Each test failed. Tool pusher reported the packer would set down at a depth of 268 feet below grade. Pulled packer up and set at 257 ft. above obstruction. Pressure tested ok at 257. The following day the packer was set and tested at 293 ft., below obstruction. Pressure test failed. Hole in casing about 268 feet. Reviewed old records the original well was drilled 8 to 10 inches from current hole. Due to casing being pushed out of bore hole by shooting with nitroglycerin. Well will be plugged.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1542833910
 
| -1542833910
 
| 2008-12-11
 
| 2008-12-11
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1565115727
 
| -1565115727
 
| 2007-10-22
 
| 2007-10-22
|
+
|  
 
| Reset packer and tested but pressure equilized. Recommend pulling packer out and inspect. Shut well in until it will test.
 
| Reset packer and tested but pressure equilized. Recommend pulling packer out and inspect. Shut well in until it will test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1565488129
 
| -1565488129
 
| 2006-12-15
 
| 2006-12-15
|
+
|  
 
| Injection and annulus pressure test. Pressures are equalized at 350 psi.
 
| Injection and annulus pressure test. Pressures are equalized at 350 psi.
|
+
|  
| 9-5-09[C]
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1609952911
 
| -1609952911
 
| 2012-02-27
 
| 2012-02-27
|
+
|  
 
| Inspect well. Valve on Annulus is broken.
 
| Inspect well. Valve on Annulus is broken.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -1722416447
 
| -1722416447
 
| 2009-04-25
 
| 2009-04-25
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 1850524506
 +
| 2007-10-30
 +
|
 +
| Mechanical integrity test. Pulled 1'' tubing and packer. Replaced packer and circulated inhibitor thru annulus and pressure tested packer and tubing at 350 psi. Drop of 10 psi in 15 minutes. NOV in compliance. Sun, 55 degrees.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1948417058
 +
| 2004-04-22
 +
|
 +
| Injection pressure test. Could not test tubing pressure due to size of gauge threads. Advised Len Rex to install reducer and test. Report to Tom Tomastik in 30 days.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -1958963302
 
| -1958963302
 
| 2007-04-03
 
| 2007-04-03
|
+
|  
 
| NOV in compliance. Blew down annulus and pressured up to 320 psi. Pressure held at 320 psi for 15 minutes. 0% decline. Injection pressure is 290 psi. Advised Matt Miller of injection pressure decline. Run mini test April 30, 2007 and report to inspector.
 
| NOV in compliance. Blew down annulus and pressured up to 320 psi. Pressure held at 320 psi for 15 minutes. 0% decline. Injection pressure is 290 psi. Advised Matt Miller of injection pressure decline. Run mini test April 30, 2007 and report to inspector.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 2018932901
 +
| 2013-05-02
 +
|
 +
| Run packer and tubing into well, 21 joints at 25 feet each with a Butler Larkin 6 inch compression packer with new rubbers. Each individual joint of tubing was pressure tested for leaks. The packer was originally set at 525 feet. Formation gas was leaking past packer and the test was not successful. Operator will install tie downs to set and hold packer.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -208962727
 
| -208962727
 
| 2006-03-15
 
| 2006-03-15
|
+
|  
 
| Re-test annulus and tubing pressures. Nov in compliance. Snow, 29 degrees
 
| Re-test annulus and tubing pressures. Nov in compliance. Snow, 29 degrees
|
+
|  
| 9-5-10(H)
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -279559499
 
| -279559499
 
| 2010-11-27
 
| 2010-11-27
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 40325828
 +
| 2012-12-04
 +
|
 +
| Inspect well for integrity and pressure.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -43150819
 
| -43150819
 
| 2008-03-27
 
| 2008-03-27
|
+
|  
 
| Annulus and injection pressure test.
 
| Annulus and injection pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -473608655
 
| -473608655
 
| 2011-07-12
 
| 2011-07-12
|
+
|  
 
| inspect well
 
| inspect well
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -502459913
 
| -502459913
 
| 2003-08-07
 
| 2003-08-07
|
+
|  
| UNABLE TO GAUGE INJECTION PRESSURE, NEED TO REPLACE WITH VALVE TAP FOR 1/4" OR 1/2" GAUGE
+
| UNABLE TO GAUGE INJECTION PRESSURE, NEED TO REPLACE WITH VALVE TAP FOR 1/4 OR 1/2 GAUGE
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -503156724
 
| -503156724
 
| 2011-10-17
 
| 2011-10-17
|
+
|  
 
| Inspect well.
 
| Inspect well.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 510006879
 +
| 2013-03-04
 +
|
 +
| Inspect well for integrity and pressure.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -511764643
 
| -511764643
 
| 2012-09-11
 
| 2012-09-11
|
+
|  
 
| Inspect Well. Site ok.
 
| Inspect Well. Site ok.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 583280891
 +
| 2005-12-01
 +
|
 +
| Injection and annulus pressure test. Pressures have equalized at 350 psi.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -625117970
 
| -625117970
 
| 2004-11-18
 
| 2004-11-18
|
+
|  
 
| Injection pressure test.
 
| Injection pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -735082993
 
| -735082993
 
| 2011-04-13
 
| 2011-04-13
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 111057061
 
| 2010-04-06
 
|
 
| Injection and annulus pressure test.
 
|
 
|
 
|
 
|-
 
|-
 
| 1116355295
 
| 2005-05-17
 
|
 
| Injection well test. GPS location and update to RBDMS.
 
|
 
|
 
|
 
|-
 
|-
 
| 1192038614
 
| 2007-10-10
 
|
 
| Injection and annulus pressure test. Pressures are equalized at 330 psi. Suspended well operation at this time.
 
|
 
| 9-5-09[C]
 
|
 
|-
 
|-
 
| 1350741638
 
| 2012-06-04
 
|
 
| Inspect Well. Annulus valve was replaced. Box needs repair.
 
|
 
|
 
|
 
|-
 
|-
 
| 1371742425
 
| 2013-06-20
 
|
 
| Request from operator to witness well plugging.  The well was plugged with 9 sack grout.
 
|
 
|
 
|
 
|-
 
|-
 
| 1376581904
 
| 2013-08-15
 
|
 
| The site needs to be graded and a pipe rack with 1 inch tubing removed to approve final restoration.  Randy at Deep Resources was advised.  He stated he would call when work is complete.
 
|
 
|
 
|
 
|-
 
|-
 
| 1850524506
 
| 2007-10-30
 
|
 
| Mechanical integrity test. Pulled 1'' tubing and packer. Replaced packer and circulated inhibitor thru annulus and pressure tested packer and tubing at 350 psi. Drop of 10 psi in 15 minutes. NOV in compliance. Sun, 55 degrees.
 
|
 
|
 
|
 
|-
 
|-
 
| 1948417058
 
| 2004-04-22
 
|
 
| Injection pressure test. Could not test tubing pressure due to size of gauge threads. Advised Len Rex to install reducer and test. Report to Tom Tomastik in 30 days.
 
|
 
|
 
|
 
|-
 
|-
 
| 2018932901
 
| 2013-05-02
 
|
 
| Run packer and tubing into well, 21 joints at 25 feet each with a Butler Larkin 6 inch compression packer with new rubbers. Each individual joint of tubing was pressure tested for leaks. The packer was originally set at 525 feet. Formation gas was leaking past packer and the test was not successful. Operator will install tie downs to set and hold packer.
 
|
 
|
 
|
 
|-
 
|-
 
| 40325828
 
| 2012-12-04
 
|
 
| Inspect well for integrity and pressure.
 
|
 
|
 
|
 
|-
 
|-
 
| 510006879
 
| 2013-03-04
 
|
 
| Inspect well for integrity and pressure.
 
|
 
|
 
|
 
|-
 
|-
 
| 583280891
 
| 2005-12-01
 
|
 
| Injection and annulus pressure test. Pressures have equalized at 350 psi.
 
|
 
| 9-5-10(H)
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 751620049
 
| 751620049
 
| 2006-04-24
 
| 2006-04-24
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 763086463
 
| 763086463
 
| 2013-04-04
 
| 2013-04-04
|
+
|  
 
| Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Test failed. Well shut in.
 
| Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Test failed. Well shut in.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 774942903
 
| 774942903
 
| 2013-10-17
 
| 2013-10-17
|
+
|  
 
| All equipment has been removed from the site.  The location is finish graded and vegetated.  Casing has been cut off.  The final restoration is approved.
 
| All equipment has been removed from the site.  The location is finish graded and vegetated.  Casing has been cut off.  The final restoration is approved.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 923400769
 
| 923400769
 
| 2009-10-07
 
| 2009-10-07
|
+
|  
 
| Injection and annulus pressure test.
 
| Injection and annulus pressure test.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 07:04, 15 July 2015

Well Details

Well ID: 34-005-21791
Loading map...
County: Ashland
Municipality:
Operator Name: DEEP RESOURCES LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1976-08-27
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.89594361
Longitude: -82.15612288

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2007-0 0.0 13.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1082935222 2006-12-29 NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi. Compliance Notice
-1082935222 2006-12-29 NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi. Compliance Notice
-1082935222 2006-12-29 NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi. Field Visit or Inspection
-1082935222 2006-12-29 NOV followup. Ran Mini test on annulus and pressure held at 410psi for 15 minutes. Injection pressure is at 350 psi. Compliance Notice
111057061 2010-04-06 Injection and annulus pressure test.
1116355295 2005-05-17 Injection well test. GPS location and update to RBDMS.
-111963044 2007-03-30 Injection and annulaus pressure test. Pressures are equalized at 350 psi.
1192038614 2007-10-10 Injection and annulus pressure test. Pressures are equalized at 330 psi. Suspended well operation at this time.
1350741638 2012-06-04 Inspect Well. Annulus valve was replaced. Box needs repair.
1371742425 2013-06-20 Request from operator to witness well plugging. The well was plugged with 9 sack grout.
1376581904 2013-08-15 The site needs to be graded and a pipe rack with 1 inch tubing removed to approve final restoration. Randy at Deep Resources was advised. He stated he would call when work is complete.
-1464663205 2013-05-08 Operator pickled and cleaned casing with acid. Run tubing and packer with new rubbers and cage. Pressure test of well did not pass. Significant loss of pressure when tested. Five times a joint of pipe was pulled up, packer set, loaded with water and pressure tested. Each test failed. Tool pusher reported the packer would set down at a depth of 268 feet below grade. Pulled packer up and set at 257 ft. above obstruction. Pressure tested ok at 257. The following day the packer was set and tested at 293 ft., below obstruction. Pressure test failed. Hole in casing about 268 feet. Reviewed old records the original well was drilled 8 to 10 inches from current hole. Due to casing being pushed out of bore hole by shooting with nitroglycerin. Well will be plugged.
-1542833910 2008-12-11 Injection and annulus pressure test.
-1565115727 2007-10-22 Reset packer and tested but pressure equilized. Recommend pulling packer out and inspect. Shut well in until it will test.
-1565488129 2006-12-15 Injection and annulus pressure test. Pressures are equalized at 350 psi.
-1609952911 2012-02-27 Inspect well. Valve on Annulus is broken.
-1722416447 2009-04-25 Injection and annulus pressure test.
1850524506 2007-10-30 Mechanical integrity test. Pulled 1 tubing and packer. Replaced packer and circulated inhibitor thru annulus and pressure tested packer and tubing at 350 psi. Drop of 10 psi in 15 minutes. NOV in compliance. Sun, 55 degrees.
1948417058 2004-04-22 Injection pressure test. Could not test tubing pressure due to size of gauge threads. Advised Len Rex to install reducer and test. Report to Tom Tomastik in 30 days.
-1958963302 2007-04-03 NOV in compliance. Blew down annulus and pressured up to 320 psi. Pressure held at 320 psi for 15 minutes. 0% decline. Injection pressure is 290 psi. Advised Matt Miller of injection pressure decline. Run mini test April 30, 2007 and report to inspector.
2018932901 2013-05-02 Run packer and tubing into well, 21 joints at 25 feet each with a Butler Larkin 6 inch compression packer with new rubbers. Each individual joint of tubing was pressure tested for leaks. The packer was originally set at 525 feet. Formation gas was leaking past packer and the test was not successful. Operator will install tie downs to set and hold packer.
-208962727 2006-03-15 Re-test annulus and tubing pressures. Nov in compliance. Snow, 29 degrees
-279559499 2010-11-27 Injection and annulus pressure test.
40325828 2012-12-04 Inspect well for integrity and pressure.
-43150819 2008-03-27 Annulus and injection pressure test.
-473608655 2011-07-12 inspect well
-502459913 2003-08-07 UNABLE TO GAUGE INJECTION PRESSURE, NEED TO REPLACE WITH VALVE TAP FOR 1/4 OR 1/2 GAUGE
-503156724 2011-10-17 Inspect well.
510006879 2013-03-04 Inspect well for integrity and pressure.
-511764643 2012-09-11 Inspect Well. Site ok.
583280891 2005-12-01 Injection and annulus pressure test. Pressures have equalized at 350 psi.
-625117970 2004-11-18 Injection pressure test.
-735082993 2011-04-13 Injection and annulus pressure test.
751620049 2006-04-24 Injection and annulus pressure test.
763086463 2013-04-04 Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Test failed. Well shut in.
774942903 2013-10-17 All equipment has been removed from the site. The location is finish graded and vegetated. Casing has been cut off. The final restoration is approved.
923400769 2009-10-07 Injection and annulus pressure test.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.