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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-053-20507 | | Well ID: 34-053-20507 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 38. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 38.92925109, -82.18530105 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Gallia County, Ohio|Gallia]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[ALTIER BROTHERS INC]] |
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− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
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| Spud Date: 1980-04-24 | | Spud Date: 1980-04-24 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
− | | Violations: | + | | Violations: 0 |
|- | |- | ||
− | | Latitude: 38. | + | | Latitude: 38.92925109 |
|- | |- | ||
− | | Longitude: -82. | + | | Longitude: -82.18530105 |
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|} | |} | ||
== Inspection Data == | == Inspection Data == | ||
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!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
− | | | + | | 1040221252 |
− | | | + | | 2009-05-05 |
− | | | + | | |
− | | | + | | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. |
− | | | + | | |
− | | | + | | |
− | | | + | | Compliance Notice |
|- | |- | ||
|- | |- | ||
− | | | + | | 1040221252 |
− | | | + | | 2009-05-05 |
− | + | | | |
− | + | | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. | |
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| 1040221252 | | 1040221252 | ||
| 2009-05-05 | | 2009-05-05 | ||
− | | | + | | |
− | | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 | + | | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. |
− | | | + | | |
− | | | + | | |
− | | | + | | Compliance Notice |
|- | |- | ||
|- | |- | ||
| 1186406806 | | 1186406806 | ||
| 2007-07-30 | | 2007-07-30 | ||
− | | | + | | |
| Follow up, Idle well, No id, Valves are off, Electric lines are disconnected at pole. No motor for pump jack. Tank has leaked some brine (small scald area) Tank does not have a dike. Brush has over grown the well and pump jack. I called and talked to Dale Compston (Altier Brothers) at 10:10am on 8-6-2007 about the status of this well. Dale said that they had a plug permit that had expired ( Exp. On 6-12-2007) He said that they need to get a new permit to plug and get started plugging before bad weather sets in. Dale asked about methods of plugging the well. He is interested in using clay for the bottom hole plug. | | Follow up, Idle well, No id, Valves are off, Electric lines are disconnected at pole. No motor for pump jack. Tank has leaked some brine (small scald area) Tank does not have a dike. Brush has over grown the well and pump jack. I called and talked to Dale Compston (Altier Brothers) at 10:10am on 8-6-2007 about the status of this well. Dale said that they had a plug permit that had expired ( Exp. On 6-12-2007) He said that they need to get a new permit to plug and get started plugging before bad weather sets in. Dale asked about methods of plugging the well. He is interested in using clay for the bottom hole plug. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -133365121 | ||
+ | | 2010-09-29 | ||
+ | | | ||
+ | | Site graded. Good vegetative cover established. Equipment removed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
− | | | + | | -1545764750 |
− | | | + | | 2006-05-15 |
− | | | + | | |
− | | | + | | Well is not operating and has been shut in for several years. Needs new jack and jack shaft is broken. Electric line is too low for safe passage to well site. Needs dike around tank. Well is owned by Althier Oil not JD Drilling. No ID. |
− | | | + | | |
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|- | |- | ||
|- | |- | ||
| 437480727 | | 437480727 | ||
| 2007-09-26 | | 2007-09-26 | ||
− | | | + | | |
| Road has been marked with orange marking tape. So has the well. No other changes were noticed to the site. | | Road has been marked with orange marking tape. So has the well. No other changes were noticed to the site. | ||
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| 529644376 | | 529644376 | ||
| 2009-04-29 | | 2009-04-29 | ||
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| Received call from Dale Compton. Re: plug job. Moving dozer today. Rig on site Thursday. Set bottom plug Friday morning. 8am Formation Cementing. | | Received call from Dale Compton. Re: plug job. Moving dozer today. Rig on site Thursday. Set bottom plug Friday morning. 8am Formation Cementing. | ||
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+ | |- | ||
+ | |- | ||
+ | | -687837591 | ||
+ | | 2006-05-15 | ||
+ | | | ||
+ | | FOLLOW UP TO NOV # -1545764750 Well is not operating and has been shut in for several years. Needs new jack and jack shaft is broken. Electric line is too low for safe passage to well site. Needs dike around tank. Well is owned by Althier Oil not JD Drilling. No ID. | ||
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| 770945672 | | 770945672 | ||
| 2009-04-23 | | 2009-04-23 | ||
− | | | + | | |
| Talked to Dale Compton 9:38 am, about plug schedule. Dale told me that the rig will be moving week of the 27th. To the well site. I told Dale to call me when rig is moving. | | Talked to Dale Compton 9:38 am, about plug schedule. Dale told me that the rig will be moving week of the 27th. To the well site. I told Dale to call me when rig is moving. | ||
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|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-053-20507 | Loading map...
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County: Gallia | |
Municipality: | |
Operator Name: ALTIER BROTHERS INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1980-04-24 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 38.92925109 | |
Longitude: -82.18530105 |
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1040221252 | 2009-05-05 | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. | Compliance Notice | |||
1040221252 | 2009-05-05 | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. | Compliance Notice | |||
1040221252 | 2009-05-05 | Plugging well from TD 1690' Ran 51 joints of tubing. Cement pumped through tubing. 1275' top of 1st plug. Telegraph at 1100'. Rip 4.5 at 1126'. Pump Injun plug through 4.5. Surface plug dropped 150'. Set bridge plug at 150' and filled to surface with cement. Cement stayed at surface. Hauled one load of pit water (30 bbls) before leaving. | Compliance Notice | |||
1186406806 | 2007-07-30 | Follow up, Idle well, No id, Valves are off, Electric lines are disconnected at pole. No motor for pump jack. Tank has leaked some brine (small scald area) Tank does not have a dike. Brush has over grown the well and pump jack. I called and talked to Dale Compston (Altier Brothers) at 10:10am on 8-6-2007 about the status of this well. Dale said that they had a plug permit that had expired ( Exp. On 6-12-2007) He said that they need to get a new permit to plug and get started plugging before bad weather sets in. Dale asked about methods of plugging the well. He is interested in using clay for the bottom hole plug. | ||||
-133365121 | 2010-09-29 | Site graded. Good vegetative cover established. Equipment removed. | ||||
-1545764750 | 2006-05-15 | Well is not operating and has been shut in for several years. Needs new jack and jack shaft is broken. Electric line is too low for safe passage to well site. Needs dike around tank. Well is owned by Althier Oil not JD Drilling. No ID. | ||||
437480727 | 2007-09-26 | Road has been marked with orange marking tape. So has the well. No other changes were noticed to the site. | ||||
529644376 | 2009-04-29 | Received call from Dale Compton. Re: plug job. Moving dozer today. Rig on site Thursday. Set bottom plug Friday morning. 8am Formation Cementing. | ||||
-687837591 | 2006-05-15 | FOLLOW UP TO NOV # -1545764750 Well is not operating and has been shut in for several years. Needs new jack and jack shaft is broken. Electric line is too low for safe passage to well site. Needs dike around tank. Well is owned by Althier Oil not JD Drilling. No ID. | ||||
770945672 | 2009-04-23 | Talked to Dale Compton 9:38 am, about plug schedule. Dale told me that the rig will be moving week of the 27th. To the well site. I told Dale to call me when rig is moving. |
For data sources see[1]