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Difference between revisions of "34-111-65469"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-111-65469
 
| Well ID: 34-111-65469
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.7306811816, -81.1799201119 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.73034722, -81.17967797 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Monroe County, Ohio|Monroe]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[CISLER OIL AND GAS]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 39.7306811816
+
| Latitude: 39.73034722
 
|-
 
|-
| Longitude: -81.1799201119
+
| Longitude: -81.17967797
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 67:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1108846301
 
| 1108846301
 
| 2005-02-17
 
| 2005-02-17
|
+
|  
 
| No violations noted,well appears capable of producing.Well is equipped with pumpjack rods and tubing in place,electric motor on pumpjack.No production has ever been reported on said well.
 
| No violations noted,well appears capable of producing.Well is equipped with pumpjack rods and tubing in place,electric motor on pumpjack.No production has ever been reported on said well.
|
+
|
|
+
|
|
+
| Compliance Notice
 +
|-
 +
|-
 +
| 1426378194
 +
| 2015-03-14
 +
|
 +
| Inspection on this day revealed that fresh water had filled up area between wooden conductor pipe and 7 surface casing and let oil escape onto the ground and it entered a small wet weather stream that feeds Rich  Fork Creek and estimated release was 1-2 bbl of oil and the Monroe county EMA contacted local inspector Bill Stolarik and I received call from him at 12:00 pm  asking if I would look into the matter and I arrived on site at 1:15 pm and located problem well and then contacted well owner requesting his presence at site to begin clean up efforts on spill, instructed owner to remove any contaminated soils  and properly dispose of it at a EPA approved landfill.
 +
Note: Equipment for clean up arrived on site and soils were placed onto plastic liner and covered for the night and then they started to work there way down stream to clean up small pockets of oil in creek.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1426512539
 +
| 2015-03-15
 +
|
 +
| Inspection on this day indicated that contaminated soils were still on plastic containment and crew was trying to haul material up the hill and place into roll off container and I walked entire creek bed to check area for any free standing oil and on this day very little was found and I told cleanup crew to change out absorbent pads twice daily until given father notice.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -1746527227
 +
| 2015-03-15
 +
|
 +
| Administrative report to document the situation with a oil spill at the well head that entered the waters of the State. At 11:32 Am on 03/14/15 I was notified by Phil Keevert with the Monroe Co EMA  that they had an oil spill of approximate 50 gallons that had entered the waters of the state and the EPA was also notified and enroot, I notified my Supervisor Brent Bear and contacted Inspector Dave Ball to respond. I also made contact with the Steve Sapio with the USDA who is the area inspector for the US Forest Service and reported the spill to Mr. Sapio on this day. I remained in contact with Inspector Ball and Supervisor Bear through the course of events of the day documenting the situation. 03/16/2015 The initial well identification reported by the County EMA Director was found to be incorrect- I have correctly identified the well as 3411165719.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1837868187
 +
| 2015-03-15
 +
|
 +
| Status check inspection of the well head found the following equipment present at the well head 6.625'' casing 2'' tubing and pumping rods with no production lines attached to the well head. A small fuel type tank is located near the well head as a production tank but not in use. ODNR-RBDMS records show no reported production in the database. Instructions are as follows-Plug the said well within 180 days -ODNR Monroe County Inspector Bill Stolarik- 740-507-6592.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 2097318503
 
| 2097318503
 
| 2012-07-16
 
| 2012-07-16
|
+
|  
 
| Inspection of the well head found the following equipment, 6.188'' surface casing, 2'' tubing & rods, with the well equipped with a pumping unit and gasoline motor, no production lines hooked up and a 800 gallon vertical tank sitting next to the well head. Well identification present.
 
| Inspection of the well head found the following equipment, 6.188'' surface casing, 2'' tubing & rods, with the well equipped with a pumping unit and gasoline motor, no production lines hooked up and a 800 gallon vertical tank sitting next to the well head. Well identification present.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 12:41, 15 July 2015

Well Details

Well ID: 34-111-65469
Loading map...
County: Monroe
Municipality:
Operator Name: CISLER OIL AND GAS
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.73034722
Longitude: -81.17967797

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1108846301 2005-02-17 No violations noted,well appears capable of producing.Well is equipped with pumpjack rods and tubing in place,electric motor on pumpjack.No production has ever been reported on said well. Compliance Notice
1426378194 2015-03-14 Inspection on this day revealed that fresh water had filled up area between wooden conductor pipe and 7 surface casing and let oil escape onto the ground and it entered a small wet weather stream that feeds Rich Fork Creek and estimated release was 1-2 bbl of oil and the Monroe county EMA contacted local inspector Bill Stolarik and I received call from him at 12:00 pm asking if I would look into the matter and I arrived on site at 1:15 pm and located problem well and then contacted well owner requesting his presence at site to begin clean up efforts on spill, instructed owner to remove any contaminated soils and properly dispose of it at a EPA approved landfill.

Note: Equipment for clean up arrived on site and soils were placed onto plastic liner and covered for the night and then they started to work there way down stream to clean up small pockets of oil in creek.

1426512539 2015-03-15 Inspection on this day indicated that contaminated soils were still on plastic containment and crew was trying to haul material up the hill and place into roll off container and I walked entire creek bed to check area for any free standing oil and on this day very little was found and I told cleanup crew to change out absorbent pads twice daily until given father notice.
-1746527227 2015-03-15 Administrative report to document the situation with a oil spill at the well head that entered the waters of the State. At 11:32 Am on 03/14/15 I was notified by Phil Keevert with the Monroe Co EMA that they had an oil spill of approximate 50 gallons that had entered the waters of the state and the EPA was also notified and enroot, I notified my Supervisor Brent Bear and contacted Inspector Dave Ball to respond. I also made contact with the Steve Sapio with the USDA who is the area inspector for the US Forest Service and reported the spill to Mr. Sapio on this day. I remained in contact with Inspector Ball and Supervisor Bear through the course of events of the day documenting the situation. 03/16/2015 The initial well identification reported by the County EMA Director was found to be incorrect- I have correctly identified the well as 3411165719.
1837868187 2015-03-15 Status check inspection of the well head found the following equipment present at the well head 6.625 casing 2 tubing and pumping rods with no production lines attached to the well head. A small fuel type tank is located near the well head as a production tank but not in use. ODNR-RBDMS records show no reported production in the database. Instructions are as follows-Plug the said well within 180 days -ODNR Monroe County Inspector Bill Stolarik- 740-507-6592.
2097318503 2012-07-16 Inspection of the well head found the following equipment, 6.188 surface casing, 2 tubing & rods, with the well equipped with a pumping unit and gasoline motor, no production lines hooked up and a 800 gallon vertical tank sitting next to the well head. Well identification present.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.