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Difference between revisions of "34-009-21546"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-009-21546
 
| Well ID: 34-009-21546
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.3409185303, -81.9501238494 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.34091853, -81.95012385 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Athens County, Ohio|Athens]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[STRIGHT ROGER]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.3409185303
+
| Latitude: 39.34091853
 
|-
 
|-
| Longitude: -81.9501238494
+
| Longitude: -81.95012385
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | INSPECTION ID
 
!scope="col" | DATE
 
!scope="col" | DESCRIPTION
 
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION_COMMENT
 
 
|-
 
|-
| -704947287
+
| 1984-0
| 2013-11-22
+
| style="text-align:right;" | 0.0
|
+
|
| The landowner asked to meet me at the well to discuss concerns of his. Well equipped with a pumping unit with no powersource. No identification at the well. The tubing was plumbed into a 2" sales line. The line was equipped with a T fitting near the wellhead. One section of line was reduced to a 1" nipple with a partially open gate valve. No sign of contamination, but there was a smell of gas. The other section of line had a 2" gate valve in the closed position.
+
|
|
+
|
| 9-9-05(A)1
+
| style="text-align:right;" | 104.0
|
+
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 132.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 94.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 89.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 68.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 34.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 41.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 52.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 27.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 16.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 25.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 240.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 152.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 96.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 110.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 150.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 112.0
 +
|  
 
|-
 
|-
 
|-
 
|-
| -704947287
+
| 2008-0
| 2013-11-22
+
| style="text-align:right;" | 0.0
|
+
|  
| The landowner asked to meet me at the well to discuss concerns of his. Well equipped with a pumping unit with no powersource. No identification at the well. The tubing was plumbed into a 2" sales line. The line was equipped with a T fitting near the wellhead. One section of line was reduced to a 1" nipple with a partially open gate valve. No sign of contamination, but there was a smell of gas. The other section of line had a 2" gate valve in the closed position.
+
|  
|
+
|  
| 9-9-05(A)10
+
| style="text-align:right;" | 75.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -704947287
+
| 2009-0
| 2013-11-22
+
| style="text-align:right;" | 0.0
|
+
|  
| The landowner asked to meet me at the well to discuss concerns of his. Well equipped with a pumping unit with no powersource. No identification at the well. The tubing was plumbed into a 2" sales line. The line was equipped with a T fitting near the wellhead. One section of line was reduced to a 1" nipple with a partially open gate valve. No sign of contamination, but there was a smell of gas. The other section of line had a 2" gate valve in the closed position.
+
|  
|
+
|  
| 9-9-05(B)
+
| style="text-align:right;" | 150.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -716271123
+
| 2010-0
| 2013-07-25
+
| style="text-align:right;" | 0.0
|
+
|  
| Follow up to -795571006. No clean up.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 105.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -795571006
+
| 2011-0
| 2013-06-19
+
| style="text-align:right;" | 0.0
|
+
|  
| The landowner had concerns about the well and apparent lack of maintenance. The well was equipped with a pumping unit with no power source. Tank battery consists of one 100 Barrel (Bbl) steel tank, one 80 Bbl steel tank and one 2600 gallon poly tank. There is a scalded are inside the dike roughly 20 x 20' that registered 280ppm Chlorides when field tested. Contaminated soils shall be removed and disposed of properly. Any affected areas shall be reseeded and mulched and steps shall be taken to encourage vegetative cover. I spoke with the producer at the well site.
+
|  
|
+
|  
| 9-1-07
+
| style="text-align:right;" | 70.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -87563097
+
| 2012-0
| 2014-02-21
+
| style="text-align:right;" | 0.0
|
+
|  
| Follow up to -704947287. Ground around well head dug up and work has been done. The back flow preventor is still leaking.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 105.0
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -95647606
+
| 2013-0
| 2014-03-31
+
| style="text-align:right;" | 0.0
|
+
|  
| Follow up to -795571006. No clean up has taken place at the tank battery.
+
|  
|
+
|  
|
+
| style="text-align:right;" | 210.0
|
+
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
 +
| accessdate = 2015-06-20 }}</ref>
 +
== Inspection Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" | INSPECTION ID
 +
!scope="col" | DATE
 +
!scope="col" | DESCRIPTION
 +
!scope="col" | COMMENT
 +
!scope="col" | VIOLATION ID
 +
!scope="col" | VIOLATION CODE
 +
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| 1385562353
 
| 1385562353
 
| 2013-11-27
 
| 2013-11-27
|
+
|  
 
| Follow up to -795571006. No clean up.
 
| Follow up to -795571006. No clean up.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1395754133
 
| 1395754133
 
| 2014-03-25
 
| 2014-03-25
|
+
|  
 
| Follow up to -795571006. The lines at the wellhead are no longer leaking, the backflow preventor has been replaced with a plug. There has been no clean up at the contaminated area around the tank battery.
 
| Follow up to -795571006. The lines at the wellhead are no longer leaking, the backflow preventor has been replaced with a plug. There has been no clean up at the contaminated area around the tank battery.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1403271650
 
| 1403271650
 
| 2014-06-20
 
| 2014-06-20
|
+
|  
 
| Follow up to -795571006. The contaminated soils have been removed, the dike has been reconstructed, the new tank will be placed into the dike soon.
 
| Follow up to -795571006. The contaminated soils have been removed, the dike has been reconstructed, the new tank will be placed into the dike soon.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1949891169
 
| 1949891169
 
| 2014-02-19
 
| 2014-02-19
|
+
|  
 
| Follow up to -795571006. There is still a scald area inside the dike and standing water at the lower side of the dike. Spoke with Roger Stright, issued a 4 week extension to restore vegetative cover due to weather.
 
| Follow up to -795571006. There is still a scald area inside the dike and standing water at the lower side of the dike. Spoke with Roger Stright, issued a 4 week extension to restore vegetative cover due to weather.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 305604878
 
| 305604878
 
| 2014-02-19
 
| 2014-02-19
|
+
|  
 
| Follow up to -704947287.  Pumping unit has no power source and is overgrown with vegetation. Valves on tubing open and line is open to air with no plug. There is also a line that is plumbed into either the production or surface casing and is also open to air. Gas seen escaping from this line. Unable to tell which string of casing this line is tied into because most of well head is below ground. Spoke with Roger Stright issued a 2 day extension to get a plug in the back flow preventor.
 
| Follow up to -704947287.  Pumping unit has no power source and is overgrown with vegetation. Valves on tubing open and line is open to air with no plug. There is also a line that is plumbed into either the production or surface casing and is also open to air. Gas seen escaping from this line. Unable to tell which string of casing this line is tied into because most of well head is below ground. Spoke with Roger Stright issued a 2 day extension to get a plug in the back flow preventor.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -704947287
 +
| 2013-11-22
 +
|
 +
| The landowner asked to meet me at the well to discuss concerns of his. Well equipped with a pumping unit with no powersource. No identification at the well. The tubing was plumbed into a 2 sales line. The line was equipped with a T fitting near the wellhead. One section of line was reduced to a 1 nipple with a partially open gate valve. No sign of contamination, but there was a smell of gas. The other section of line had a 2 gate valve in the closed position.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -716271123
 +
| 2013-07-25
 +
|
 +
| Follow up to -795571006. No clean up.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -795571006
 +
| 2013-06-19
 +
|
 +
| The landowner had concerns about the well and apparent lack of maintenance. The well was equipped with a pumping unit with no power source. Tank battery consists of one 100 Barrel (Bbl) steel tank, one 80 Bbl steel tank and one 2600 gallon poly tank. There is a scalded are inside the dike roughly 20 x 20' that registered 280ppm Chlorides when field tested. Contaminated soils shall be removed and disposed of properly. Any affected areas shall be reseeded and mulched and steps shall be taken to encourage vegetative cover. I spoke with the producer at the well site.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -87563097
 +
| 2014-02-21
 +
|
 +
| Follow up to -704947287. Ground around well head dug up and work has been done. The back flow preventor is still leaking.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -95647606
 +
| 2014-03-31
 +
|
 +
| Follow up to -795571006. No clean up has taken place at the tank battery.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 13:47, 15 July 2015

Well Details

Well ID: 34-009-21546
Loading map...
County: Athens
Municipality:
Operator Name: STRIGHT ROGER
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.34091853
Longitude: -81.95012385

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 0.0 104.0
1987-0 0.0 132.0
1988-0 0.0 94.0
1989-0 0.0 89.0
1990-0 0.0 68.0
1991-0 0.0 34.0
1992-0 0.0 41.0
1993-0 0.0 52.0
1994-0 0.0 27.0
1996-0 0.0 16.0
1997-0 0.0 25.0
1998-0 0.0 0.0
2000-0 0.0 0.0
2001-0 0.0 240.0
2002-0 0.0 152.0
2003-0 0.0 96.0
2004-0 0.0 110.0
2005-0 0.0 0.0
2006-0 0.0 150.0
2007-0 0.0 112.0
2008-0 0.0 75.0
2009-0 0.0 150.0
2010-0 0.0 105.0
2011-0 0.0 70.0
2012-0 0.0 105.0
2013-0 0.0 210.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1385562353 2013-11-27 Follow up to -795571006. No clean up.
1395754133 2014-03-25 Follow up to -795571006. The lines at the wellhead are no longer leaking, the backflow preventor has been replaced with a plug. There has been no clean up at the contaminated area around the tank battery.
1403271650 2014-06-20 Follow up to -795571006. The contaminated soils have been removed, the dike has been reconstructed, the new tank will be placed into the dike soon.
1949891169 2014-02-19 Follow up to -795571006. There is still a scald area inside the dike and standing water at the lower side of the dike. Spoke with Roger Stright, issued a 4 week extension to restore vegetative cover due to weather.
305604878 2014-02-19 Follow up to -704947287. Pumping unit has no power source and is overgrown with vegetation. Valves on tubing open and line is open to air with no plug. There is also a line that is plumbed into either the production or surface casing and is also open to air. Gas seen escaping from this line. Unable to tell which string of casing this line is tied into because most of well head is below ground. Spoke with Roger Stright issued a 2 day extension to get a plug in the back flow preventor.
-704947287 2013-11-22 The landowner asked to meet me at the well to discuss concerns of his. Well equipped with a pumping unit with no powersource. No identification at the well. The tubing was plumbed into a 2 sales line. The line was equipped with a T fitting near the wellhead. One section of line was reduced to a 1 nipple with a partially open gate valve. No sign of contamination, but there was a smell of gas. The other section of line had a 2 gate valve in the closed position.
-716271123 2013-07-25 Follow up to -795571006. No clean up.
-795571006 2013-06-19 The landowner had concerns about the well and apparent lack of maintenance. The well was equipped with a pumping unit with no power source. Tank battery consists of one 100 Barrel (Bbl) steel tank, one 80 Bbl steel tank and one 2600 gallon poly tank. There is a scalded are inside the dike roughly 20 x 20' that registered 280ppm Chlorides when field tested. Contaminated soils shall be removed and disposed of properly. Any affected areas shall be reseeded and mulched and steps shall be taken to encourage vegetative cover. I spoke with the producer at the well site.
-87563097 2014-02-21 Follow up to -704947287. Ground around well head dug up and work has been done. The back flow preventor is still leaking.
-95647606 2014-03-31 Follow up to -795571006. No clean up has taken place at the tank battery.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.