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Difference between revisions of "34-127-23154"

m
 
m
Line 3: Line 3:
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-23154
 
| Well ID: 34-127-23154
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6820668654, -82.2513375994 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.68206687, -82.2513376 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Perry County, Ohio|Perry]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[JEANIE ENTERPISES LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1972-05-11
 
| Spud Date: 1972-05-11
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 3
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.6820668654
+
| Latitude: 39.68206687
 
|-
 
|-
| Longitude: -82.2513375994
+
| Longitude: -82.2513376
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 1218.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 575.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 2053.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 479.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 2130.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 521.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 2226.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 452.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 1457.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 288.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 1528.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 304.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1258.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 223.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 1545.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 281.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 1285.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 247.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 1061.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 213.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 1007.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 176.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 72.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 647.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 40.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 582.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 121.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 280.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 297.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 69.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 222.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 311.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 487.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 439.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 238.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 283:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -135180267
+
| 1045092224
| 2013-03-05
+
| 2013-12-10
|
+
|  
| Make well capable of commercial production within 60  days; or plugging is required within 90 days.
+
| This well has been plugged. The rig crew has moved there rig off of the location. The clay is at the surface. The well will be left open for a couple of weeks to see if the clay settles at all. I met with Keith Matheney to get the affidavit off of him for this well.
Failure to comply may result in Forfeiture of Bond.
+
|  
|
+
|  
| 9-9-05(A)10
+
| Field Visit or Inspection
|
 
 
|-
 
|-
 
|-
 
|-
| -135180267
+
| 1162922234
| 2013-03-05
+
| 2013-11-29
|
+
|  
| Make well capable of commercial production within 60  days; or plugging is required within 90 days.
+
| The rig crew had Appalachian come in to shoot the 4 off.  They shot it off at 2510ft. They then pulled out 110ft of 4 before they washed in the Lime plug. They washed in 500ft of clay.
Failure to comply may result in Forfeiture of Bond.
+
|  
|
+
|  
| NONE
+
|  
|
 
 
|-
 
|-
 
|-
 
|-
 
| -135180267
 
| -135180267
 
| 2013-03-05
 
| 2013-03-05
|
+
|  
 
| Make well capable of commercial production within 60  days; or plugging is required within 90 days.
 
| Make well capable of commercial production within 60  days; or plugging is required within 90 days.
 
Failure to comply may result in Forfeiture of Bond.
 
Failure to comply may result in Forfeiture of Bond.
|
+
|  
| NONE_
+
|  
|
+
|  
|-
 
|-
 
| -1752692522
 
| 2013-08-29
 
|
 
| Mark called me to let me know that he is working on trying to put this well back in production before he decides to plug it. He said he was not around at the time when this well was shut down. He wants to find out why and if they can get it going again. He will know something within the next month.
 
|
 
|
 
|
 
|-
 
|-
 
| -842550963
 
| 2014-01-14
 
|
 
| I had to stop by Jeanie Enterprises to get the clay tickets for the plug job on this well. They made me a copy of them.
 
|
 
|
 
|
 
|-
 
|-
 
| 1045092224
 
| 2013-12-10
 
|
 
| This well has been plugged. The rig crew has moved there rig off of the location. The clay is at the surface. The well will be left open for a couple of weeks to see if the clay settles at all. I met with Keith Matheney to get the affidavit off of him for this well.
 
|
 
|
 
|
 
|-
 
|-
 
| 1162922234
 
| 2013-11-29
 
|
 
| The rig crew had Appalachian come in to shoot the 4" off.  They shot it off at 2510ft. They then pulled out 110ft of 4" before they washed in the Lime plug. They washed in 500ft of clay.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1384797574
 
| 1384797574
 
| 2013-11-15
 
| 2013-11-15
|
+
|  
| Keith Matheney has his rig on this well to plug it. I met them at the well to see what they are planning on doing. The clay is bridged at 1882. They are trying to find some 3" tools  to beat on the bridge. They will call me if they work on the well today.
+
| Keith Matheney has his rig on this well to plug it. I met them at the well to see what they are planning on doing. The clay is bridged at 1882. They are trying to find some 3 tools  to beat on the bridge. They will call me if they work on the well today.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1385125053
 
| 1385125053
 
| 2013-11-20
 
| 2013-11-20
|
+
|  
| Keith Matheney and rig crew were on location to run 2" tubing in hole with a drill bit on bottom. They were having trouble getting down hole. They got the tubing down to were the bridge was and shut down until the next day.
+
| Keith Matheney and rig crew were on location to run 2 tubing in hole with a drill bit on bottom. They were having trouble getting down hole. They got the tubing down to were the bridge was and shut down until the next day.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1385933282
 
| 1385933282
 
| 2013-11-25
 
| 2013-11-25
|
+
|  
| The rig crew was on location to work on plugging this well. They pulled the tubing back out of the well and tagged the clay to see how much was left in the hole. They washed in another 300ft of clay and tagged the plug again. The clay was up to 2640ft. The rig crew shut down for the day to set up someone to shoot the 4" off.
+
| The rig crew was on location to work on plugging this well. They pulled the tubing back out of the well and tagged the clay to see how much was left in the hole. They washed in another 300ft of clay and tagged the plug again. The clay was up to 2640ft. The rig crew shut down for the day to set up someone to shoot the 4 off.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1403612508
 
| 1403612508
 
| 2014-06-23
 
| 2014-06-23
|
+
|  
 
| The final restoration meets 1509.072.
 
| The final restoration meets 1509.072.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1752692522
 +
| 2013-08-29
 +
|
 +
| Mark called me to let me know that he is working on trying to put this well back in production before he decides to plug it. He said he was not around at the time when this well was shut down. He wants to find out why and if they can get it going again. He will know something within the next month.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1769753614
 
| 1769753614
 
| 2013-11-26
 
| 2013-11-26
|
+
|  
| The job was canceled to shoot off the 4" do to the weather. It is rescheduled for the November 29th at 8am.
+
| The job was canceled to shoot off the 4 do to the weather. It is rescheduled for the November 29th at 8am.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2040928754
 
| 2040928754
 
| 2013-11-18
 
| 2013-11-18
|
+
|  
 
| I showed up to the rig. There was no one on location. I contacted Keith Maheney and he said they would not be onsite today. They are working on getting a bit and rounding up some tubing to drill out the bridge.
 
| I showed up to the rig. There was no one on location. I contacted Keith Maheney and he said they would not be onsite today. They are working on getting a bit and rounding up some tubing to drill out the bridge.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 374235680
 
| 374235680
 
| 2013-10-17
 
| 2013-10-17
|
+
|  
 
| I stopped at Jeanie Enterprises to see what they are planning on doing with this well. There was no one at the office when I arrived. I tried to call Mark Schmeltzer and left him a message. I then waited a few minutes and Tim Schmeltzer arrived at the office. I talked with him about this well and he informed me that it is on the plug list. They do plan on plugging this well soon.
 
| I stopped at Jeanie Enterprises to see what they are planning on doing with this well. There was no one at the office when I arrived. I tried to call Mark Schmeltzer and left him a message. I then waited a few minutes and Tim Schmeltzer arrived at the office. I talked with him about this well and he informed me that it is on the plug list. They do plan on plugging this well soon.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 4095122
 
| 4095122
 
| 2013-11-21
 
| 2013-11-21
|
+
|  
 
| The rig crew bridge the well off at 1882 with plugging clay on this well so we had Cemenco LLC onsite to wash the clay out and drill through the bridge. When we first started pumping through the tubing the bit plugged up so the rig crew started pulling out the tubing. We got 22 joints out and it cleaned up. When then started cleaning up the hole and pumping out the clay until we made it down through the plug. We ran the rest of the tubing in to make sure the hole was clean.
 
| The rig crew bridge the well off at 1882 with plugging clay on this well so we had Cemenco LLC onsite to wash the clay out and drill through the bridge. When we first started pumping through the tubing the bit plugged up so the rig crew started pulling out the tubing. We got 22 joints out and it cleaned up. When then started cleaning up the hole and pumping out the clay until we made it down through the plug. We ran the rest of the tubing in to make sure the hole was clean.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 806974962
 
| 806974962
 
| 2013-10-09
 
| 2013-10-09
|
+
|  
 
| I tried to contact Mark about this well. The last time I talked to him he was trying to get the approval on putting it back in production. I left him a message to call me about it but have not received a call back yet at this time.
 
| I tried to contact Mark about this well. The last time I talked to him he was trying to get the approval on putting it back in production. I left him a message to call me about it but have not received a call back yet at this time.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -842550963
 +
| 2014-01-14
 +
|
 +
| I had to stop by Jeanie Enterprises to get the clay tickets for the plug job on this well. They made me a copy of them.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 880909532
 
| 880909532
 
| 2014-05-27
 
| 2014-05-27
|
+
|  
 
| I returned to this well to do a final restoration. The well does not meet the requirements of 1509.072. I have contacted Tim Schmeltzer and let him know that the plastic line needs removed along with the 100 barrel tank that is still there. I will check on this well at a later date.
 
| I returned to this well to do a final restoration. The well does not meet the requirements of 1509.072. I have contacted Tim Schmeltzer and let him know that the plastic line needs removed along with the 100 barrel tank that is still there. I will check on this well at a later date.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 15:12, 15 July 2015

Well Details

Well ID: 34-127-23154
Loading map...
County: Perry
Municipality:
Operator Name: JEANIE ENTERPISES LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1972-05-11
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.68206687
Longitude: -82.2513376

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 1218.0 575.0
1985-0 2053.0 479.0
1986-0 2130.0 521.0
1987-0 2226.0 452.0
1988-0 1457.0 288.0
1989-0 1528.0 304.0
1990-0 1258.0 223.0
1991-0 1545.0 281.0
1992-0 1285.0 247.0
1993-0 1061.0 213.0
1994-0 1007.0 176.0
1995-0 0.0 0.0
1996-0 0.0 72.0
1997-0 647.0 40.0
1998-0 582.0 121.0
1999-0 280.0 0.0
2000-0 297.0 69.0
2001-0 222.0 0.0
2002-0 0.0 0.0
2003-0 311.0 0.0
2004-0 487.0 0.0
2005-0 439.0 0.0
2007-0 238.0 0.0
2008-0 0.0 0.0
2009-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1045092224 2013-12-10 This well has been plugged. The rig crew has moved there rig off of the location. The clay is at the surface. The well will be left open for a couple of weeks to see if the clay settles at all. I met with Keith Matheney to get the affidavit off of him for this well. Field Visit or Inspection
1162922234 2013-11-29 The rig crew had Appalachian come in to shoot the 4 off. They shot it off at 2510ft. They then pulled out 110ft of 4 before they washed in the Lime plug. They washed in 500ft of clay.
-135180267 2013-03-05 Make well capable of commercial production within 60 days; or plugging is required within 90 days.

Failure to comply may result in Forfeiture of Bond.

1384797574 2013-11-15 Keith Matheney has his rig on this well to plug it. I met them at the well to see what they are planning on doing. The clay is bridged at 1882. They are trying to find some 3 tools to beat on the bridge. They will call me if they work on the well today.
1385125053 2013-11-20 Keith Matheney and rig crew were on location to run 2 tubing in hole with a drill bit on bottom. They were having trouble getting down hole. They got the tubing down to were the bridge was and shut down until the next day.
1385933282 2013-11-25 The rig crew was on location to work on plugging this well. They pulled the tubing back out of the well and tagged the clay to see how much was left in the hole. They washed in another 300ft of clay and tagged the plug again. The clay was up to 2640ft. The rig crew shut down for the day to set up someone to shoot the 4 off.
1403612508 2014-06-23 The final restoration meets 1509.072.
-1752692522 2013-08-29 Mark called me to let me know that he is working on trying to put this well back in production before he decides to plug it. He said he was not around at the time when this well was shut down. He wants to find out why and if they can get it going again. He will know something within the next month.
1769753614 2013-11-26 The job was canceled to shoot off the 4 do to the weather. It is rescheduled for the November 29th at 8am.
2040928754 2013-11-18 I showed up to the rig. There was no one on location. I contacted Keith Maheney and he said they would not be onsite today. They are working on getting a bit and rounding up some tubing to drill out the bridge.
374235680 2013-10-17 I stopped at Jeanie Enterprises to see what they are planning on doing with this well. There was no one at the office when I arrived. I tried to call Mark Schmeltzer and left him a message. I then waited a few minutes and Tim Schmeltzer arrived at the office. I talked with him about this well and he informed me that it is on the plug list. They do plan on plugging this well soon.
4095122 2013-11-21 The rig crew bridge the well off at 1882 with plugging clay on this well so we had Cemenco LLC onsite to wash the clay out and drill through the bridge. When we first started pumping through the tubing the bit plugged up so the rig crew started pulling out the tubing. We got 22 joints out and it cleaned up. When then started cleaning up the hole and pumping out the clay until we made it down through the plug. We ran the rest of the tubing in to make sure the hole was clean.
806974962 2013-10-09 I tried to contact Mark about this well. The last time I talked to him he was trying to get the approval on putting it back in production. I left him a message to call me about it but have not received a call back yet at this time.
-842550963 2014-01-14 I had to stop by Jeanie Enterprises to get the clay tickets for the plug job on this well. They made me a copy of them.
880909532 2014-05-27 I returned to this well to do a final restoration. The well does not meet the requirements of 1509.072. I have contacted Tim Schmeltzer and let him know that the plastic line needs removed along with the 100 barrel tank that is still there. I will check on this well at a later date.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.