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Difference between revisions of "34-093-21246"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-093-21246
 
| Well ID: 34-093-21246
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.3387799583, -81.9066125758 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.33869958, -81.90762003 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Lorain County, Ohio|Lorain]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[ROBERTS BOB / WILDWOOD PARK]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1984-02-08
 
| Spud Date: 1984-02-08
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 4
+
| Violations: 0
 
|-
 
|-
| Latitude: 41.3387799583
+
| Latitude: 41.33869958
 
|-
 
|-
| Longitude: -81.9066125758
+
| Longitude: -81.90762003
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 12050.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 10905.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 3179.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 4901.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 1897.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1193.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 946.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 640.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 16.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 738.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 449.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 370.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 393.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 62.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 184:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -485034269
+
| 1087479368
| 2014-07-18
+
| 2004-06-17
|
+
|  
| Inspected production well on 07/18/2014.  The well is equipped with a wellhead with a swedge, gauge, and elbow.  No well identification is posted.  The well did not appear to be hooked up at the time of the inspection.  No tanks were noted nearby. Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
+
| Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only.
|
+
|  
| 9-9-05(A)10
+
|  
|
+
| Compliance Notice
|-
 
|-
 
| -485034269
 
| 2014-07-18
 
|
 
| Inspected production well on 07/18/2014.  The well is equipped with a wellhead with a swedge, gauge, and elbow. No well identification is posted. The well did not appear to be hooked up at the time of the inspection. No tanks were noted nearby.  Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
 
|
 
| NONE
 
|
 
|-
 
|-
 
| -485034269
 
| 2014-07-18
 
|
 
| Inspected production well on 07/18/2014.  The well is equipped with a wellhead with a swedge, gauge, and elbow.  No well identification is posted. The well did not appear to be hooked up at the time of the inspection. No tanks were noted nearby.  Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
 
|
 
| NONEC
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1087479368
 
| 1087479368
 
| 2004-06-17
 
| 2004-06-17
|
+
|  
 
| Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only.
 
| Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only.
|
+
|  
| 9-9-05(A)1
+
|  
|
+
| Compliance Notice
 
|-
 
|-
 
|-
 
|-
 
| 1089219472
 
| 1089219472
 
| 2004-07-07
 
| 2004-07-07
|
+
|  
 
| Gas leak has been repaired. Case # 04-010
 
| Gas leak has been repaired. Case # 04-010
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -485034269
 +
| 2014-07-18
 +
|
 +
| Inspected production well on 07/18/2014.  The well is equipped with a wellhead with a swedge, gauge, and elbow.  No well identification is posted.  The well did not appear to be hooked up at the time of the inspection.  No tanks were noted nearby.  Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| PL13351
 
| PL13351
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 15:26, 15 July 2015

Well Details

Well ID: 34-093-21246
Loading map...
County: Lorain
Municipality:
Operator Name: ROBERTS BOB / WILDWOOD PARK
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1984-02-08
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.33869958
Longitude: -81.90762003

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 12050.0 0.0
1986-0 10905.0 0.0
1987-0 3179.0 0.0
1988-0 4901.0 0.0
1989-0 1897.0 0.0
1990-0 1193.0 0.0
1991-0 0.0 946.0
1992-0 640.0 16.0
1993-0 738.0 0.0
1994-0 449.0 0.0
1995-0 370.0 0.0
1996-0 393.0 0.0
1997-0 62.0 0.0
1998-0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1087479368 2004-06-17 Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only. Compliance Notice
1087479368 2004-06-17 Called by Rhonda Vedda at 11036 East River Rd. that a gas leak in yard. Gas is bubbling at 4% lel. Sales line leading from well crossing SR 252. Called Jim Gessel of Dome Drilling. Jim advised he sold well to Bob Roberts but will repair the gas leak for him. Well is used for domestic house gas only. Compliance Notice
1089219472 2004-07-07 Gas leak has been repaired. Case # 04-010
-485034269 2014-07-18 Inspected production well on 07/18/2014. The well is equipped with a wellhead with a swedge, gauge, and elbow. No well identification is posted. The well did not appear to be hooked up at the time of the inspection. No tanks were noted nearby. Research into the production history of the well showed that no production has been filed since 1998, therefore the well must be plugged.
PL13351 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.