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Difference between revisions of "34-155-24016"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-155-24016
 
| Well ID: 34-155-24016
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.4691897177, -80.5993900592 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.46918972, -80.59939006 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Trumbull County, Ohio|Trumbull]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[STRYKER ENERGY LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 2010-02-01
 
| Spud Date: 2010-02-01
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 41.4691897177
+
| Latitude: 41.46918972
 
|-
 
|-
| Longitude: -80.5993900592
+
| Longitude: -80.59939006
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 3212.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 109.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 503.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 49.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 0.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 103:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1015311625
 
| -1015311625
 
| 2010-03-03
 
| 2010-03-03
|
+
|  
 
| Drilling pits have been closed ,
 
| Drilling pits have been closed ,
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 1363873667
 +
|
 +
|
 +
| My inspection found the well not in production.  The well was equipped with a plunger lift unit.  There was black 1 poly tubing wrapped around the well.  The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator.  It was surrounded by a dike capable of meeting containment requirements.  The identification sign on the production tank was faded and unreadable.  There was a 7 day production chart in the separator dated 4/2/2012.  I researched our database and found the last reported production was in 2010.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| 1701513542
 +
| 2010-02-02
 +
|
 +
| Kilbarger drilling at 154' . No violations .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| -2017604751
 
| -2017604751
 
| 2010-02-04
 
| 2010-02-04
|
+
|  
 
| Kilbarger drilling company . No violations .
 
| Kilbarger drilling company . No violations .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| -2120826228
 
| -2120826228
 
| 2010-02-01
 
| 2010-02-01
|
+
|  
 
| Kilbager rigging up . No violations .
 
| Kilbager rigging up . No violations .
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| -932951842
 
| 2010-02-08
 
|
 
| Drilling pits showed no violations .
 
|
 
|
 
|
 
|-
 
|-
 
| 1363873667
 
|
 
|
 
| My inspection found the well not in production.  The well was equipped with a plunger lift unit.  There was black 1" poly tubing wrapped around the well.  The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator.  It was surrounded by a dike capable of meeting containment requirements.  The identification sign on the production tank was faded and unreadable.  There was a 7 day production chart in the separator dated 4/2/2012.  I researched our database and found the last reported production was in 2010.
 
|
 
|
 
|
 
|-
 
|-
 
| 1701513542
 
| 2010-02-02
 
|
 
| Kilbarger drilling at 154' . No violations .
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 30286736
 
| 30286736
 
| 2013-04-03
 
| 2013-04-03
|
+
|  
 
| My inspection found the proper identification posted on the production tank per my request.
 
| My inspection found the proper identification posted on the production tank per my request.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 372945829
 
| 372945829
 
| 2013-03-21
 
| 2013-03-21
|
+
|  
| My inspection found this well not in production.  The well was equipped with a plunger lift unit.  There was 1" black tubing wrapped around the well.  The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator.  It was surrounded by a dike capable of meeting containment requirements.  The separator had a 7 day production chart that was dated 4/2/2012.  The identification was faded and hard to read.  There was a plug on the load line.  The last reported production was in 2010.  I called Stryker Energy at 440-446-9198.  I was informed the company sold the sales line to Dominion in 2011.  Stryker was in the process of working with Dominion on getting this well back into production.  I instructed Stryker to replace the identification sign and remove the tubing from around the well.  Also, I told them I would re-inspection the well by 5/1/2013 to see if it was placed back into production.
+
| My inspection found this well not in production.  The well was equipped with a plunger lift unit.  There was 1 black tubing wrapped around the well.  The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator.  It was surrounded by a dike capable of meeting containment requirements.  The separator had a 7 day production chart that was dated 4/2/2012.  The identification was faded and hard to read.  There was a plug on the load line.  The last reported production was in 2010.  I called Stryker Energy at 440-446-9198.  I was informed the company sold the sales line to Dominion in 2011.  Stryker was in the process of working with Dominion on getting this well back into production.  I instructed Stryker to replace the identification sign and remove the tubing from around the well.  Also, I told them I would re-inspection the well by 5/1/2013 to see if it was placed back into production.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -932951842
 +
| 2010-02-08
 +
|
 +
| Drilling pits showed no violations .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 18:21, 15 July 2015

Well Details

Well ID: 34-155-24016
Loading map...
County: Trumbull
Municipality:
Operator Name: STRYKER ENERGY LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 2010-02-01
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 41.46918972
Longitude: -80.59939006

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
2010-0 3212.0 109.0
2011-0 503.0 49.0
2012-0 0.0 0.0
2013-0 0.0 0.0
2014-0 0.0 0.0 0.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1015311625 2010-03-03 Drilling pits have been closed ,
1363873667 My inspection found the well not in production. The well was equipped with a plunger lift unit. There was black 1 poly tubing wrapped around the well. The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a dike capable of meeting containment requirements. The identification sign on the production tank was faded and unreadable. There was a 7 day production chart in the separator dated 4/2/2012. I researched our database and found the last reported production was in 2010.
1701513542 2010-02-02 Kilbarger drilling at 154' . No violations .
-2017604751 2010-02-04 Kilbarger drilling company . No violations .
-2120826228 2010-02-01 Kilbager rigging up . No violations .
30286736 2013-04-03 My inspection found the proper identification posted on the production tank per my request.
372945829 2013-03-21 My inspection found this well not in production. The well was equipped with a plunger lift unit. There was 1 black tubing wrapped around the well. The tank battery contained one, 100 barrel production tank, one, 50 barrel brine tank, and a separator. It was surrounded by a dike capable of meeting containment requirements. The separator had a 7 day production chart that was dated 4/2/2012. The identification was faded and hard to read. There was a plug on the load line. The last reported production was in 2010. I called Stryker Energy at 440-446-9198. I was informed the company sold the sales line to Dominion in 2011. Stryker was in the process of working with Dominion on getting this well back into production. I instructed Stryker to replace the identification sign and remove the tubing from around the well. Also, I told them I would re-inspection the well by 5/1/2013 to see if it was placed back into production.
-932951842 2010-02-08 Drilling pits showed no violations .

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.