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Difference between revisions of "34-127-25648"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-25648
 
| Well ID: 34-127-25648
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6784724343, -82.1367670751 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.67847243, -82.13676708 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Perry County, Ohio|Perry]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[STONEBRIDGE OPERATING CO]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1982-06-11
 
| Spud Date: 1982-06-11
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Producing
 
|-
 
|-
| Violations: 1
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.6784724343
+
| Latitude: 39.67847243
 
|-
 
|-
| Longitude: -82.1367670751
+
| Longitude: -82.13676708
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1984-0
 +
| style="text-align:right;" | 10457.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 7130.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1986-0
 +
| style="text-align:right;" | 7724.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 2941.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 2147.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 864.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 482.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 1.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2003-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2004-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2005-0
 +
| style="text-align:right;" | 46.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2006-0
 +
| style="text-align:right;" | 13.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2007-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2009-0
 +
| style="text-align:right;" | 23.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2010-0
 +
| style="text-align:right;" | 48.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2011-0
 +
| style="text-align:right;" | 67.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2012-0
 +
| style="text-align:right;" | 14.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2013-0
 +
| style="text-align:right;" | 134.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2014-0
 +
| style="text-align:right;" | 189.0
 +
| style="text-align:right;" | 252.0
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
| style="text-align:right;" | 252.0
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 301:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -377448404
+
| -1236436443
| 2014-02-21
+
| 2012-09-04
|
+
|  
| I inspected this well to see if it has been put back into production. The well is still not back in production. I met with Keith and he told me that at there meeting this morning John Schneider said that they would be putting the well back in production as soon as they got there bond back. They are going to set a new meter and hook up the well.
+
| FOLLOW UP TO NOV #  1346777428 I met with Mr. Esselstein concerning no production of the gas well on his property, A chart graph had been installed on 7/25/2012. The graph did not show any activity. The production shown on RBDMS is below minimum production standards for 2011,2010,2009. This well consists of one 100 barrel tank, one gas separator, a sale meter and well head. I spoke with Keith Kregor, pumper for Stone bridge Oil, he has stated the well was down due to the fact it feeds into a sales line with two other wells, one of these wells had a hole in the 4'' line, it has been repaired and Keith expects to have the Esselstein well back in production in one week.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1346777428
 
| 1346777428
 
| 2012-09-04
 
| 2012-09-04
|
+
|  
 
| I met with Mr. Esselstein concerning no production of the gas well on his property, A chart graph had been installed on 7/25/2012. The graph did not show any activity. The production shown on RBDMS is below minimum production standards for 2011,2010,2009. This well consists of one 100 barrel tank, one gas separator, a sale meter and well head. I spoke with Keith Kregor, pumper for Stone bridge Oil, he has stated the well was down due to the fact it feeds into a sales line with two other wells, one of these wells had a hole in the 4'' line, it has been repaired and Keith expects to have the Esselstein well back in production in one week.
 
| I met with Mr. Esselstein concerning no production of the gas well on his property, A chart graph had been installed on 7/25/2012. The graph did not show any activity. The production shown on RBDMS is below minimum production standards for 2011,2010,2009. This well consists of one 100 barrel tank, one gas separator, a sale meter and well head. I spoke with Keith Kregor, pumper for Stone bridge Oil, he has stated the well was down due to the fact it feeds into a sales line with two other wells, one of these wells had a hole in the 4'' line, it has been repaired and Keith expects to have the Esselstein well back in production in one week.
|
+
|  
| NONE_
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1346848452
 
| 1346848452
 
| 2012-09-05
 
| 2012-09-05
|
+
|  
 
| I spoke with Keith, pumper for stonbridge oil. Keith told me the well is one of three wells that feed into a SE Ohio gas line. One of the other wells had a hole in the line so that shut down the production, Keith expects the well to be up and producing gas in one week.
 
| I spoke with Keith, pumper for stonbridge oil. Keith told me the well is one of three wells that feed into a SE Ohio gas line. One of the other wells had a hole in the line so that shut down the production, Keith expects the well to be up and producing gas in one week.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| 2071134374
 +
| 2013-09-10
 +
|
 +
| The well was put back in production but the production tailed off. They brought a rig in and pulled tubing to swab well. The tubing was left out of the well. The pressure was checked about a week ago and is up to 20lbs. The company is either going to treat the well or plug it.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -377448404
 +
| 2014-02-21
 +
|
 +
| I inspected this well to see if it has been put back into production. The well is still not back in production. I met with Keith and he told me that at there meeting this morning John Schneider said that they would be putting the well back in production as soon as they got there bond back. They are going to set a new meter and hook up the well.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| PL7091
 
| PL7091
|
+
|  
|
+
|  
 
| Preliminary Restoration  done information from Data Point
 
| Preliminary Restoration  done information from Data Point
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 00:27, 16 July 2015

Well Details

Well ID: 34-127-25648
Loading map...
County: Perry
Municipality:
Operator Name: STONEBRIDGE OPERATING CO
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1982-06-11
Unconventional: No
Configuration: Vertical
Well Status: Producing
Violations: 0
Latitude: 39.67847243
Longitude: -82.13676708

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1984-0 10457.0 0.0
1985-0 7130.0 0.0
1986-0 7724.0 0.0
1987-0 2941.0 0.0
1988-0 2147.0 0.0
1990-0 864.0 0.0
1991-0 482.0 0.0
1993-0 0.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
2000-0 0.0 1.0
2001-0 0.0 0.0
2002-0 0.0 0.0
2003-0 0.0 0.0
2004-0 0.0 0.0
2005-0 46.0 0.0
2006-0 13.0 0.0
2007-0 0.0 0.0
2008-0 0.0 0.0
2009-0 23.0 0.0
2010-0 48.0 0.0
2011-0 67.0 0.0
2012-0 14.0 0.0
2013-0 134.0 0.0
2014-0 189.0 252.0 0.0 252.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1236436443 2012-09-04 FOLLOW UP TO NOV # 1346777428 I met with Mr. Esselstein concerning no production of the gas well on his property, A chart graph had been installed on 7/25/2012. The graph did not show any activity. The production shown on RBDMS is below minimum production standards for 2011,2010,2009. This well consists of one 100 barrel tank, one gas separator, a sale meter and well head. I spoke with Keith Kregor, pumper for Stone bridge Oil, he has stated the well was down due to the fact it feeds into a sales line with two other wells, one of these wells had a hole in the 4 line, it has been repaired and Keith expects to have the Esselstein well back in production in one week.
1346777428 2012-09-04 I met with Mr. Esselstein concerning no production of the gas well on his property, A chart graph had been installed on 7/25/2012. The graph did not show any activity. The production shown on RBDMS is below minimum production standards for 2011,2010,2009. This well consists of one 100 barrel tank, one gas separator, a sale meter and well head. I spoke with Keith Kregor, pumper for Stone bridge Oil, he has stated the well was down due to the fact it feeds into a sales line with two other wells, one of these wells had a hole in the 4 line, it has been repaired and Keith expects to have the Esselstein well back in production in one week.
1346848452 2012-09-05 I spoke with Keith, pumper for stonbridge oil. Keith told me the well is one of three wells that feed into a SE Ohio gas line. One of the other wells had a hole in the line so that shut down the production, Keith expects the well to be up and producing gas in one week.
2071134374 2013-09-10 The well was put back in production but the production tailed off. They brought a rig in and pulled tubing to swab well. The tubing was left out of the well. The pressure was checked about a week ago and is up to 20lbs. The company is either going to treat the well or plug it.
-377448404 2014-02-21 I inspected this well to see if it has been put back into production. The well is still not back in production. I met with Keith and he told me that at there meeting this morning John Schneider said that they would be putting the well back in production as soon as they got there bond back. They are going to set a new meter and hook up the well.
PL7091 Preliminary Restoration done information from Data Point

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.