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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-153-21417 | | Well ID: 34-153-21417 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.28520478, -81.49029282 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Summit County, Ohio|Summit]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[PETROX, INC]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1985-01-10 | | Spud Date: 1985-01-10 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Plugged and Abandoned |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.28520478 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.49029282 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1984-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1985-0 | ||
+ | | style="text-align:right;" | 2529.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 136.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 6418.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 232.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 4376.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 201.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 3550.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 66.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1989-0 | ||
+ | | style="text-align:right;" | 2010.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 65.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1990-0 | ||
+ | | style="text-align:right;" | 1295.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 115.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1991-0 | ||
+ | | style="text-align:right;" | 1202.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 69.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1992-0 | ||
+ | | style="text-align:right;" | 629.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1993-0 | ||
+ | | style="text-align:right;" | 510.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 56.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1994-0 | ||
+ | | style="text-align:right;" | 280.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1995-0 | ||
+ | | style="text-align:right;" | 189.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 166: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
|- | |- | ||
| -1551822884 | | -1551822884 | ||
| 2005-05-06 | | 2005-05-06 | ||
− | | | + | | |
| Received a cll from Patrick Duncan with P&S Environmental Consultants reporting a gas leak at the Athey #2 location. The well was plugged by Petrox in 1995 and appears to be leaking around the wellhead. The area is under water and gas is bubbling through the water. There is no sheen or any odor associated with the bubbles. I contacted Duncan and requested that the water around the leak be pumped out so that the leak source can be seen. | | Received a cll from Patrick Duncan with P&S Environmental Consultants reporting a gas leak at the Athey #2 location. The well was plugged by Petrox in 1995 and appears to be leaking around the wellhead. The area is under water and gas is bubbling through the water. There is no sheen or any odor associated with the bubbles. I contacted Duncan and requested that the water around the leak be pumped out so that the leak source can be seen. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| -2072464879 | | -2072464879 | ||
| 2005-06-03 | | 2005-06-03 | ||
− | | | + | | |
| The well head has been uncovered and bulk cement was placed in the hole. The ID plate was attached and the hole backfilled. The replugging was not witnessed by any ODNR personel. | | The well head has been uncovered and bulk cement was placed in the hole. The ID plate was attached and the hole backfilled. The replugging was not witnessed by any ODNR personel. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| PL4650 | | PL4650 | ||
− | | | + | | |
− | | | + | | |
| Preliminary Restoration done information from Data Point | | Preliminary Restoration done information from Data Point | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-153-21417 | Loading map...
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County: Summit | |
Municipality: | |
Operator Name: PETROX, INC | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1985-01-10 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Plugged and Abandoned | |
Violations: 0 | |
Latitude: 41.28520478 | |
Longitude: -81.49029282 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 0.0 | 0.0 | ||||
1985-0 | 2529.0 | 136.0 | ||||
1986-0 | 6418.0 | 232.0 | ||||
1987-0 | 4376.0 | 201.0 | ||||
1988-0 | 3550.0 | 66.0 | ||||
1989-0 | 2010.0 | 65.0 | ||||
1990-0 | 1295.0 | 115.0 | ||||
1991-0 | 1202.0 | 69.0 | ||||
1992-0 | 629.0 | 0.0 | ||||
1993-0 | 510.0 | 56.0 | ||||
1994-0 | 280.0 | 0.0 | ||||
1995-0 | 189.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
-1551822884 | 2005-05-06 | Received a cll from Patrick Duncan with P&S Environmental Consultants reporting a gas leak at the Athey #2 location. The well was plugged by Petrox in 1995 and appears to be leaking around the wellhead. The area is under water and gas is bubbling through the water. There is no sheen or any odor associated with the bubbles. I contacted Duncan and requested that the water around the leak be pumped out so that the leak source can be seen. | ||||
-2072464879 | 2005-06-03 | The well head has been uncovered and bulk cement was placed in the hole. The ID plate was attached and the hole backfilled. The replugging was not witnessed by any ODNR personel. | ||||
PL4650 | Preliminary Restoration done information from Data Point |
For data sources see[2]