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Difference between revisions of "34-127-25208"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-127-25208
 
| Well ID: 34-127-25208
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.6680373052, -82.238598867 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.66803731, -82.23859887 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Perry County, Ohio|Perry]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[SCHMELZER PLUGGING LLC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1981-07-22
 
| Spud Date: 1981-07-22
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
| Violations: 3
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.6680373052
+
| Latitude: 39.66803731
 
|-
 
|-
| Longitude: -82.238598867
+
| Longitude: -82.23859887
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 229.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 210.0
 +
|
 +
|-
 +
|-
 +
| 2008-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 350.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 85:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
| -916697962
+
| 1161744354
| 2011-09-08
+
| 2013-06-14
|
+
|  
| Follow-up on Comliance Notice, In-Compliance.
+
| I stopped by the job site to see how they are getting along. The rig crew is still pulling out rods and tubing. They are not going to wash in bottom plug until Monday morning.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| -999416446
+
| 1182759490
| 2013-06-17
+
| 2013-07-09
|
+
|  
| I covered this clay plug job for Justin Smith. MH well service washed in clay for the bootm plug. Justin on site 10:30 AM.
+
| I checked this well to see if the clay was still at the surface. It was still at the surface so I let Mark Hines know that they are ok to cut it off and start reclaiming.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1278758291
 
| 1278758291
 
| 2013-08-27
 
| 2013-08-27
|
+
|  
 
| Checked the location to see if everything had been removed. There is still a small trailer on location and some boards the pipe was laid on. Chris showed up as I was leaving and told me he would be getting the trailer soon. The ground has already been reclaimed.
 
| Checked the location to see if everything had been removed. There is still a small trailer on location and some boards the pipe was laid on. Chris showed up as I was leaving and told me he would be getting the trailer soon. The ground has already been reclaimed.
|
+
|  
|
+
|  
|
+
|  
|-
 
|-
 
| 1312815617
 
| 2011-08-05
 
|
 
| An inspection of the well and tank battery revealed no ID. It appears a tank had been leaking brine and has been replaced, there is contaminated materials around tanks and approx. 50'ft away a tree has died in a yard. Done a field test around tree with Quantabs and got a reading over 2000 ppm of chlorides. No kill area noted and grass appears to be ok. No production report submitted since 2008 and dike does not meet SPCC requirements.  Need full and legible ID at the well and tank battery. Clean up and remove any and all contaminated materials around tank battery and in yard. Build a dike to meet SPCC requirements. Submit production records and records of brine being hauled. Seed and mulch areas as needed. Submit production records to Columbus Office and Brine records and disposal slips for contaminated material to Inspector. Failure to comply may result in legal actions.
 
|
 
| 9-1-07
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1312815617
 
| 1312815617
 
| 2011-08-05
 
| 2011-08-05
|
+
|  
 
| An inspection of the well and tank battery revealed no ID. It appears a tank had been leaking brine and has been replaced, there is contaminated materials around tanks and approx. 50'ft away a tree has died in a yard. Done a field test around tree with Quantabs and got a reading over 2000 ppm of chlorides. No kill area noted and grass appears to be ok. No production report submitted since 2008 and dike does not meet SPCC requirements.  Need full and legible ID at the well and tank battery. Clean up and remove any and all contaminated materials around tank battery and in yard. Build a dike to meet SPCC requirements. Submit production records and records of brine being hauled. Seed and mulch areas as needed. Submit production records to Columbus Office and Brine records and disposal slips for contaminated material to Inspector. Failure to comply may result in legal actions.
 
| An inspection of the well and tank battery revealed no ID. It appears a tank had been leaking brine and has been replaced, there is contaminated materials around tanks and approx. 50'ft away a tree has died in a yard. Done a field test around tree with Quantabs and got a reading over 2000 ppm of chlorides. No kill area noted and grass appears to be ok. No production report submitted since 2008 and dike does not meet SPCC requirements.  Need full and legible ID at the well and tank battery. Clean up and remove any and all contaminated materials around tank battery and in yard. Build a dike to meet SPCC requirements. Submit production records and records of brine being hauled. Seed and mulch areas as needed. Submit production records to Columbus Office and Brine records and disposal slips for contaminated material to Inspector. Failure to comply may result in legal actions.
|
+
|  
| NONE_
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
| 1312815617
+
| -1660149897
| 2011-08-05
+
| 2013-07-02
|
+
|  
| An inspection of the well and tank battery revealed no ID. It appears a tank had been leaking brine and has been replaced, there is contaminated materials around tanks and approx. 50'ft away a tree has died in a yard. Done a field test around tree with Quantabs and got a reading over 2000 ppm of chlorides. No kill area noted and grass appears to be ok. No production report submitted since 2008 and dike does not meet SPCC requirements.  Need full and legible ID at the well and tank battery. Clean up and remove any and all contaminated materials around tank battery and in yard. Build a dike to meet SPCC requirements. Submit production records and records of brine being hauled. Seed and mulch areas as needed. Submit production records to Columbus Office and Brine records and disposal slips for contaminated material to Inspector. Failure to comply may result in legal actions.
+
| I checked to see if the clay was still at surface. It had settled 30 ft. I had Mark Hines top the well back off. We are going to leave it open a couple of days and check it again.
|
+
|  
| NONEC
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1886619913
 
| 1886619913
 
| 2013-06-13
 
| 2013-06-13
|
+
|  
 
| The rig crew is not on location. They did not get all of the rods and tubing out of the well. I will check on them tomorrow.
 
| The rig crew is not on location. They did not get all of the rods and tubing out of the well. I will check on them tomorrow.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1900822831
 
| 1900822831
 
| 2013-09-10
 
| 2013-09-10
|
+
|  
 
| The final restoration meets 1509.072.
 
| The final restoration meets 1509.072.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1943437088
 +
| 2013-06-17
 +
|
 +
| M&H Oilfield services is on location. They are putting in the bottom plug today with clay then going in to rip the 4.  Then they are going to wash in another 500 shovels.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 2073733718
 
| 2073733718
 
| 2013-07-03
 
| 2013-07-03
|
+
|  
 
| I checked to see if the clay had settled at all. It is still at the top of the hole. They are going to leave it open another week to make sure it does not settle.
 
| I checked to see if the clay had settled at all. It is still at the top of the hole. They are going to leave it open another week to make sure it does not settle.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -302400460
 +
| 2013-06-25
 +
|
 +
| The rig crew finished pulling out the 8 while washing clay up to the surface.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -59676125
 +
| 2013-06-12
 +
|
 +
| This well is going to be plugged. Mark Hines has moved in on it and is starting to pull out rods and tubing.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 687820162
 
| 687820162
 
| 2013-06-27
 
| 2013-06-27
|
+
|  
 
| I stopped by the job site to see if the clay had settled. It had so I had the rig crew top the well off again and let it sit open.
 
| I stopped by the job site to see if the clay had settled. It had so I had the rig crew top the well off again and let it sit open.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -818200554
 +
| 2013-06-24
 +
|
 +
| Mark Hines rig crew is on location to finish plugging this well. They are working on getting the 8 out today. They picked up on  it for a few hours then it finally started to move. They were able to recover all of the 8.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 823732354
 
| 823732354
 
| 2013-06-19
 
| 2013-06-19
|
+
|  
| The rig crew finished pulling out the 4". Then they ran in the 7" pre-cast plug. It set down at 1170ft. They washed in clay after that to bottom of 8".
+
| The rig crew finished pulling out the 4. Then they ran in the 7 pre-cast plug. It set down at 1170ft. They washed in clay after that to bottom of 8.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -916697962
 +
| 2011-09-08
 +
|
 +
| Follow-up on Comliance Notice, In-Compliance.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -999416446
 +
| 2013-06-17
 +
|
 +
| I covered this clay plug job for Justin Smith. MH well service washed in clay for the bootm plug. Justin on site 10:30 AM.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 02:20, 16 July 2015

Well Details

Well ID: 34-127-25208
Loading map...
County: Perry
Municipality:
Operator Name: SCHMELZER PLUGGING LLC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1981-07-22
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 39.66803731
Longitude: -82.23859887

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1993-0 0.0 229.0
2000-0 0.0 210.0
2008-0 0.0 350.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1161744354 2013-06-14 I stopped by the job site to see how they are getting along. The rig crew is still pulling out rods and tubing. They are not going to wash in bottom plug until Monday morning.
1182759490 2013-07-09 I checked this well to see if the clay was still at the surface. It was still at the surface so I let Mark Hines know that they are ok to cut it off and start reclaiming.
1278758291 2013-08-27 Checked the location to see if everything had been removed. There is still a small trailer on location and some boards the pipe was laid on. Chris showed up as I was leaving and told me he would be getting the trailer soon. The ground has already been reclaimed.
1312815617 2011-08-05 An inspection of the well and tank battery revealed no ID. It appears a tank had been leaking brine and has been replaced, there is contaminated materials around tanks and approx. 50'ft away a tree has died in a yard. Done a field test around tree with Quantabs and got a reading over 2000 ppm of chlorides. No kill area noted and grass appears to be ok. No production report submitted since 2008 and dike does not meet SPCC requirements. Need full and legible ID at the well and tank battery. Clean up and remove any and all contaminated materials around tank battery and in yard. Build a dike to meet SPCC requirements. Submit production records and records of brine being hauled. Seed and mulch areas as needed. Submit production records to Columbus Office and Brine records and disposal slips for contaminated material to Inspector. Failure to comply may result in legal actions.
-1660149897 2013-07-02 I checked to see if the clay was still at surface. It had settled 30 ft. I had Mark Hines top the well back off. We are going to leave it open a couple of days and check it again.
1886619913 2013-06-13 The rig crew is not on location. They did not get all of the rods and tubing out of the well. I will check on them tomorrow.
1900822831 2013-09-10 The final restoration meets 1509.072.
-1943437088 2013-06-17 M&H Oilfield services is on location. They are putting in the bottom plug today with clay then going in to rip the 4. Then they are going to wash in another 500 shovels.
2073733718 2013-07-03 I checked to see if the clay had settled at all. It is still at the top of the hole. They are going to leave it open another week to make sure it does not settle.
-302400460 2013-06-25 The rig crew finished pulling out the 8 while washing clay up to the surface.
-59676125 2013-06-12 This well is going to be plugged. Mark Hines has moved in on it and is starting to pull out rods and tubing.
687820162 2013-06-27 I stopped by the job site to see if the clay had settled. It had so I had the rig crew top the well off again and let it sit open.
-818200554 2013-06-24 Mark Hines rig crew is on location to finish plugging this well. They are working on getting the 8 out today. They picked up on it for a few hours then it finally started to move. They were able to recover all of the 8.
823732354 2013-06-19 The rig crew finished pulling out the 4. Then they ran in the 7 pre-cast plug. It set down at 1170ft. They washed in clay after that to bottom of 8.
-916697962 2011-09-08 Follow-up on Comliance Notice, In-Compliance.
-999416446 2013-06-17 I covered this clay plug job for Justin Smith. MH well service washed in clay for the bootm plug. Justin on site 10:30 AM.

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.