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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-099-23197 | | Well ID: 34-099-23197 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.01369671, -80.53613717 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Mahoning County, Ohio|Mahoning]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[HILCORP ENERGY COMPANY]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 2013-08-14 | | Spud Date: 2013-08-14 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | Producing | + | | Well Status: Producing |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.01369671 |
|- | |- | ||
− | | Longitude: -80. | + | | Longitude: -80.53613717 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 2014-2 | ||
+ | | style="text-align:right;" | 95534.0 | ||
+ | | style="text-align:right;" | 22.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 22.0 | ||
+ | |- | ||
+ | |- | ||
+ | | 2014-4 | ||
+ | | style="text-align:right;" | 243289.0 | ||
+ | | style="text-align:right;" | 91.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 91.0 | ||
+ | |- | ||
+ | |- | ||
+ | | 2015-1 | ||
+ | | style="text-align:right;" | 222631.0 | ||
+ | | style="text-align:right;" | 90.0 | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | style="text-align:right;" | 90.0 | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 85: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1203133780 | | 1203133780 | ||
| 2013-10-17 | | 2013-10-17 | ||
− | | | + | | |
− | | | + | | I was on location to perform a status check. Bill Mitchell Drilling Consultaion for Hilcorp explained what they were doing. On 8/24/2013 Falcone Rig 18 was drilling with there 12.25 with a air hammer bit when they tripped out of the hole they discovered that the bottom of the bit and some parts were still in the well bore. There was two cement plugs set in the well bore. H&P 225 drilling rig was drilling the offset to go around the fish but the cement was too soft. They had to drill out the plug and set a new cement plug through drill pipe. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1377631042 | | 1377631042 | ||
| 2013-08-26 | | 2013-08-26 | ||
− | | | + | | |
| I was on location to check the status of drilling the wells on this pad location. Currently a top hole rig is on location drilling the surface holes for the wells so that the completions rig can come onto location. Currently the rig is around 4200 feet and sidetracking the well due to the fact that an air hammer was lost down hole. A plug was set and the rig is going to drill out the plug. | | I was on location to check the status of drilling the wells on this pad location. Currently a top hole rig is on location drilling the surface holes for the wells so that the completions rig can come onto location. Currently the rig is around 4200 feet and sidetracking the well due to the fact that an air hammer was lost down hole. A plug was set and the rig is going to drill out the plug. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1379959507 | | 1379959507 | ||
| 2013-08-26 | | 2013-08-26 | ||
− | | | + | | |
| Falcone Rig #18 ran back in the hole to tag there 200' cement plug at 4070' but tagged at 4280' the plug had dropped. The decision was made by Hilcorp Energy to set a new plug through drill pipe from 4280' to 3580' ( 700' plug ) and wait 4 hours and set another plug from 3580' to 2900' ( 680' plug ). Cap well until the horizontal rig moves on location to drill the off set. | | Falcone Rig #18 ran back in the hole to tag there 200' cement plug at 4070' but tagged at 4280' the plug had dropped. The decision was made by Hilcorp Energy to set a new plug through drill pipe from 4280' to 3580' ( 700' plug ) and wait 4 hours and set another plug from 3580' to 2900' ( 680' plug ). Cap well until the horizontal rig moves on location to drill the off set. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1380718930 | | 1380718930 | ||
| 2013-08-16 | | 2013-08-16 | ||
− | | | + | | |
− | | Falcone Drilling Rig #18 drilled a 17.5 | + | | Falcone Drilling Rig #18 drilled a 17.5 hole to a total depth of 950' and ran 950' of 13- 3/8 61# J-55 casing. Baker Hughes pumped 140 barrels ahead and 35 barrels of Gel with Fed Seal and Cello flake followed by 10 barrels of fresh water spacer. They pumped 821 sacks of PRE-NE-1+.05S-FREE=2CACL2 cement. There was good circulation through out the job. Dropped plug displaced with 138 barrels of water, plug held with 605 psi. shut cement head in. There was 15 barrels of cement returned to surface. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1419877793 | ||
+ | | 2014-12-26 | ||
+ | | | ||
+ | | I performed a status check on the above location. The well is in production. ID signs are posted at the well head. All safety areas are marked and emergency shut downs are marked. A motor value was sand cut and released sand and some stain on the gravel between the GPU units. I contacted Hilcorps Operations Manager, Tom Havanek and spoke to him about the clean up of the stained gravel, there were no noted fluids on the gravel. He stated that they would be a crew there on Tuesday 12/30/2014 to vacuume it up. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 143660252 | | 143660252 | ||
| 2013-10-15 | | 2013-10-15 | ||
− | | | + | | |
− | | I performed a status check on the above location. H&P Rig 225 is drilling out from under the 9.625 | + | | I performed a status check on the above location. H&P Rig 225 is drilling out from under the 9.625 casing to their kick off point. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 1612717525 | | 1612717525 | ||
| 2014-03-05 | | 2014-03-05 | ||
− | | | + | | |
| Universal Well Service is fracing the above location. All equipment is setting inside of containment. Safety lanes are marked. All annuals are monitored. No noted violations noted at this time. | | Universal Well Service is fracing the above location. All equipment is setting inside of containment. Safety lanes are marked. All annuals are monitored. No noted violations noted at this time. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 1786922027 | ||
+ | | 2014-06-11 | ||
+ | | | ||
+ | | I was on location with Geologist Mike McCormac and Geologist Teresa McQuade from the ODNR Columbus Office and also Adam Mullet a production personal from Hilcorp. Adam was explaining how the Gas Production Units ( GPU ) measured the gas and fluids before it went to the central production facility. The production facility is where the gas enters the sales point and the water and oil/condensate is collected. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | -1893303000 | ||
+ | | 2013-08-15 | ||
+ | | | ||
+ | | I performed a status check on the above location. At present Falcone Drilling Rig 18 is drilling at a depth of 630'. Area is clean of debri and spills. Permits are posted. No noted violations noted at this time. | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1927381017 | ||
+ | | 2014-12-30 | ||
+ | | | ||
+ | | Northeast Region Supervisor Tom Hill and my self were at the location to witness the clean up of a 10'x15' area of gravel that was stained. This was caused from a motor value at the separator sand cut which allowed the release of sand and causing the stain. There was no pools of oil/condensate were notice on the location. IPC Energy Services was the contractor on cleaning the location. The material that was removed will be disposed of at an approved facility. Job was completed. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 256627924 | | 256627924 | ||
| 2013-08-24 | | 2013-08-24 | ||
− | | | + | | |
| I received a phone call from Tex the consultant for Hilcorp Energy that Falcone Drilling Rig #18 tripped out of the hole to change out there 12.250 hammer bit. Once out of the hole they discovered that the bottom and some of the inside of the bit was still in the well bore. Hilcorp engineers decision was to place a two hundred ( 200' ) foot plug on top of bit debris through drill pipe. Wait 8 hours and go back and side track the plug. I called Deputy Chief Bob Worstall and talked with him he gave me the go head. There will be a plug back report on file. | | I received a phone call from Tex the consultant for Hilcorp Energy that Falcone Drilling Rig #18 tripped out of the hole to change out there 12.250 hammer bit. Once out of the hole they discovered that the bottom and some of the inside of the bit was still in the well bore. Hilcorp engineers decision was to place a two hundred ( 200' ) foot plug on top of bit debris through drill pipe. Wait 8 hours and go back and side track the plug. I called Deputy Chief Bob Worstall and talked with him he gave me the go head. There will be a plug back report on file. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 278929259 | | 278929259 | ||
| 2013-09-20 | | 2013-09-20 | ||
− | | | + | | |
− | | Falcone Drilling Rig #18 drilled a 12.25 | + | | Falcone Drilling Rig #18 drilled a 12.25 well bore to a total depth of 2584' and ran 2584' of 9.625 36# CSG J-55 intermediate casing. Baker Hughes pumped 237 barrels ahead followed by 35 barrels of Bentonit Pill w/Flake & Fed Seal and 10 barrels of fresh water spacer that was followed by 872 sacks of PNE-1+.05% Static Free + 1% cacl2 + .5% BA-10A cement. There was good circulation through out the job. There was 24 barrels of cement returned to surface. Plug bumped floats held. Shut cement head in. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 347065818 | | 347065818 | ||
| 2014-01-31 | | 2014-01-31 | ||
− | | | + | | |
− | | Northeast Region Supervisor Tom Hill and myself performed a status check on the above location. They are preparing the location and wellhead for fracing. There has been a 2 | + | | Northeast Region Supervisor Tom Hill and myself performed a status check on the above location. They are preparing the location and wellhead for fracing. There has been a 2 welded steel flow line installed and is caped with a blind flanged. No noted violations were noted at this time. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|- | |- | ||
| 491205845 | | 491205845 | ||
| 2013-07-20 | | 2013-07-20 | ||
− | | | + | | |
− | | Express Energy Service is on location drilling a 30 | + | | Express Energy Service is on location drilling a 30 conductor hole to a depth of 90' and ran 90' of 20 94# conductor casing. They cemented with 172 sacks of class A cement. They had 13 barrels of cement returned to surface. . Permits are posted. There has been safety meeting. No violations at this time. Kevin Perry covered this job. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | 753980958 | ||
+ | | 2014-06-09 | ||
+ | | | ||
+ | | On 6/9/2014. After receiving the approval to produce dated 6/6/2014. Hilcop Energy started turning the above well into production. I was on location to observe this operation. There were various Hilcorp personal on location. Turn on was completed with out incident. Equipment is set up with various safety shut downs. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 799047177 | | 799047177 | ||
| 2013-07-20 | | 2013-07-20 | ||
− | | | + | | |
− | | I was on location for the cementing of the conductor pipe. The 20 | + | | I was on location for the cementing of the conductor pipe. The 20 casing was set at 90'. Express Energy was the company on location for drilling the conductor and cementing it. Circulation was established and Class A cement with 2 % calcium and 8 oz. of flake was used. The cement scaled at approximatly 15.6 ppg. 173 sacks of cement was used at approximatly 50% excess. I witnessed cement return to surface and the casing was shut in for the cement to set. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-099-23197 | Loading map...
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County: Mahoning | |
Municipality: | |
Operator Name: HILCORP ENERGY COMPANY | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 2013-08-14 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Producing | |
Violations: 0 | |
Latitude: 41.01369671 | |
Longitude: -80.53613717 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
2014-2 | 95534.0 | 22.0 | 0.0 | 22.0 | ||
2014-4 | 243289.0 | 91.0 | 0.0 | 91.0 | ||
2015-1 | 222631.0 | 90.0 | 0.0 | 90.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1203133780 | 2013-10-17 | I was on location to perform a status check. Bill Mitchell Drilling Consultaion for Hilcorp explained what they were doing. On 8/24/2013 Falcone Rig 18 was drilling with there 12.25 with a air hammer bit when they tripped out of the hole they discovered that the bottom of the bit and some parts were still in the well bore. There was two cement plugs set in the well bore. H&P 225 drilling rig was drilling the offset to go around the fish but the cement was too soft. They had to drill out the plug and set a new cement plug through drill pipe. | ||||
1377631042 | 2013-08-26 | I was on location to check the status of drilling the wells on this pad location. Currently a top hole rig is on location drilling the surface holes for the wells so that the completions rig can come onto location. Currently the rig is around 4200 feet and sidetracking the well due to the fact that an air hammer was lost down hole. A plug was set and the rig is going to drill out the plug. | ||||
1379959507 | 2013-08-26 | Falcone Rig #18 ran back in the hole to tag there 200' cement plug at 4070' but tagged at 4280' the plug had dropped. The decision was made by Hilcorp Energy to set a new plug through drill pipe from 4280' to 3580' ( 700' plug ) and wait 4 hours and set another plug from 3580' to 2900' ( 680' plug ). Cap well until the horizontal rig moves on location to drill the off set. | ||||
1380718930 | 2013-08-16 | Falcone Drilling Rig #18 drilled a 17.5 hole to a total depth of 950' and ran 950' of 13- 3/8 61# J-55 casing. Baker Hughes pumped 140 barrels ahead and 35 barrels of Gel with Fed Seal and Cello flake followed by 10 barrels of fresh water spacer. They pumped 821 sacks of PRE-NE-1+.05S-FREE=2CACL2 cement. There was good circulation through out the job. Dropped plug displaced with 138 barrels of water, plug held with 605 psi. shut cement head in. There was 15 barrels of cement returned to surface. | ||||
1419877793 | 2014-12-26 | I performed a status check on the above location. The well is in production. ID signs are posted at the well head. All safety areas are marked and emergency shut downs are marked. A motor value was sand cut and released sand and some stain on the gravel between the GPU units. I contacted Hilcorps Operations Manager, Tom Havanek and spoke to him about the clean up of the stained gravel, there were no noted fluids on the gravel. He stated that they would be a crew there on Tuesday 12/30/2014 to vacuume it up. | ||||
143660252 | 2013-10-15 | I performed a status check on the above location. H&P Rig 225 is drilling out from under the 9.625 casing to their kick off point. | ||||
1612717525 | 2014-03-05 | Universal Well Service is fracing the above location. All equipment is setting inside of containment. Safety lanes are marked. All annuals are monitored. No noted violations noted at this time. | ||||
1786922027 | 2014-06-11 | I was on location with Geologist Mike McCormac and Geologist Teresa McQuade from the ODNR Columbus Office and also Adam Mullet a production personal from Hilcorp. Adam was explaining how the Gas Production Units ( GPU ) measured the gas and fluids before it went to the central production facility. The production facility is where the gas enters the sales point and the water and oil/condensate is collected. | ||||
-1893303000 | 2013-08-15 | I performed a status check on the above location. At present Falcone Drilling Rig 18 is drilling at a depth of 630'. Area is clean of debri and spills. Permits are posted. No noted violations noted at this time. | ||||
1927381017 | 2014-12-30 | Northeast Region Supervisor Tom Hill and my self were at the location to witness the clean up of a 10'x15' area of gravel that was stained. This was caused from a motor value at the separator sand cut which allowed the release of sand and causing the stain. There was no pools of oil/condensate were notice on the location. IPC Energy Services was the contractor on cleaning the location. The material that was removed will be disposed of at an approved facility. Job was completed. | ||||
256627924 | 2013-08-24 | I received a phone call from Tex the consultant for Hilcorp Energy that Falcone Drilling Rig #18 tripped out of the hole to change out there 12.250 hammer bit. Once out of the hole they discovered that the bottom and some of the inside of the bit was still in the well bore. Hilcorp engineers decision was to place a two hundred ( 200' ) foot plug on top of bit debris through drill pipe. Wait 8 hours and go back and side track the plug. I called Deputy Chief Bob Worstall and talked with him he gave me the go head. There will be a plug back report on file. | ||||
278929259 | 2013-09-20 | Falcone Drilling Rig #18 drilled a 12.25 well bore to a total depth of 2584' and ran 2584' of 9.625 36# CSG J-55 intermediate casing. Baker Hughes pumped 237 barrels ahead followed by 35 barrels of Bentonit Pill w/Flake & Fed Seal and 10 barrels of fresh water spacer that was followed by 872 sacks of PNE-1+.05% Static Free + 1% cacl2 + .5% BA-10A cement. There was good circulation through out the job. There was 24 barrels of cement returned to surface. Plug bumped floats held. Shut cement head in. | ||||
347065818 | 2014-01-31 | Northeast Region Supervisor Tom Hill and myself performed a status check on the above location. They are preparing the location and wellhead for fracing. There has been a 2 welded steel flow line installed and is caped with a blind flanged. No noted violations were noted at this time. | ||||
491205845 | 2013-07-20 | Express Energy Service is on location drilling a 30 conductor hole to a depth of 90' and ran 90' of 20 94# conductor casing. They cemented with 172 sacks of class A cement. They had 13 barrels of cement returned to surface. . Permits are posted. There has been safety meeting. No violations at this time. Kevin Perry covered this job. | ||||
753980958 | 2014-06-09 | On 6/9/2014. After receiving the approval to produce dated 6/6/2014. Hilcop Energy started turning the above well into production. I was on location to observe this operation. There were various Hilcorp personal on location. Turn on was completed with out incident. Equipment is set up with various safety shut downs. | ||||
799047177 | 2013-07-20 | I was on location for the cementing of the conductor pipe. The 20 casing was set at 90'. Express Energy was the company on location for drilling the conductor and cementing it. Circulation was established and Class A cement with 2 % calcium and 8 oz. of flake was used. The cement scaled at approximatly 15.6 ppg. 173 sacks of cement was used at approximatly 50% excess. I witnessed cement return to surface and the casing was shut in for the cement to set. |
For data sources see[2]