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Difference between revisions of "34-173-61118"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-173-61118
 
| Well ID: 34-173-61118
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.3087834581, -83.5819122119 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.30867769, -83.58206864 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Wood County, Ohio|Wood]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[LANDOWNER GRANT PROGRAM 2006]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 41.3087834581
+
| Latitude: 41.30867769
 
|-
 
|-
| Longitude: -83.5819122119
+
| Longitude: -83.58206864
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1748805332155141
 
| 2004-08-05
 
|
 
| Reviewed oil well on site for I&O program. The landowner said an application was submitted 10 years ago for I&O when house was built but there is no record in Columbus. Landowner is now considering selling property. Tanks and junk around well were removed at property owners expense. There was no production equipment but the tubing and rods were in place. No sign of contamination around well. Well is within 200 feet of water well and pond.
 
|
 
|
 
|
 
|-
 
|-
 
| -847062622
 
| 2006-07-13
 
|
 
| All equipment removed from site. Well has been cut off below ground and backfilled. Operator said ID plate was attached. It does not appear as though the site has been seeded and cement on ground from plugging needs to be cleaned up.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1152132480
 
| 1152132480
 
| 2006-07-05
 
| 2006-07-05
|
+
|  
 
| Witnessed completion of plugging well. The operator attempted to plug the well on 6/30/06 with inspector Sam Faust but in hole obstruction prevented cementing. Obstruction was cleared and well was plugged on 7/3/06 and witnessed by inspector Tom Benko. Operator pumped 125 sacks of cement in well but there was no cement return to the surface on that day. On 7/5/06 the operator determined the cement depth at 476 feet and  pumped an additional 75 bags of cement which include 1% CaCl. Cement returned to the surface but then fell to about 10 feet below top of pipe. Additional cement will be mixed and added when pipe is cut off and ID plate attached. Problems occurred in hole when the operator tried to have the 4 inch casing shot to remove the casing. Apparently the 6 inch casing was shot by mistake which may have resulted in an obstruction in the pipe. The 4 inch casing was then shot and the casing removed.
 
| Witnessed completion of plugging well. The operator attempted to plug the well on 6/30/06 with inspector Sam Faust but in hole obstruction prevented cementing. Obstruction was cleared and well was plugged on 7/3/06 and witnessed by inspector Tom Benko. Operator pumped 125 sacks of cement in well but there was no cement return to the surface on that day. On 7/5/06 the operator determined the cement depth at 476 feet and  pumped an additional 75 bags of cement which include 1% CaCl. Cement returned to the surface but then fell to about 10 feet below top of pipe. Additional cement will be mixed and added when pipe is cut off and ID plate attached. Problems occurred in hole when the operator tried to have the 4 inch casing shot to remove the casing. Apparently the 6 inch casing was shot by mistake which may have resulted in an obstruction in the pipe. The 4 inch casing was then shot and the casing removed.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1152543094
 
| 1152543094
 
| 2006-07-03
 
| 2006-07-03
|
+
|  
 
| Plug well. Circulate tubing to 952 feet.  Six inch casing was shot at 394 feet thinking it was the four inch casing. Shot the four inch casing at 277 feet and pulled casing. Shale / clay fell into well. Tubing was plugged with shale when run in hole, pulled tubing and re ran to 952. Well plugged with cement.
 
| Plug well. Circulate tubing to 952 feet.  Six inch casing was shot at 394 feet thinking it was the four inch casing. Shot the four inch casing at 277 feet and pulled casing. Shale / clay fell into well. Tubing was plugged with shale when run in hole, pulled tubing and re ran to 952. Well plugged with cement.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1156968867
 
| 1156968867
 
| 2006-08-30
 
| 2006-08-30
|
+
|  
 
| Area around well head is being used for livestock. No cement remaining on ground. Final restoration approved.
 
| Area around well head is being used for livestock. No cement remaining on ground. Final restoration approved.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1.74881E+15
 +
| 2004-08-05
 +
|
 +
| Reviewed oil well on site for I&O program. The landowner said an application was submitted 10 years ago for I&O when house was built but there is no record in Columbus. Landowner is now considering selling property. Tanks and junk around well were removed at property owners expense. There was no production equipment but the tubing and rods were in place. No sign of contamination around well. Well is within 200 feet of water well and pond.
 +
|
 +
|
 +
|
 +
|-
 +
|-
 +
| -847062622
 +
| 2006-07-13
 +
|
 +
| All equipment removed from site. Well has been cut off below ground and backfilled. Operator said ID plate was attached. It does not appear as though the site has been seeded and cement on ground from plugging needs to be cleaned up.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 05:09, 16 July 2015

Well Details

Well ID: 34-173-61118
Loading map...
County: Wood
Municipality:
Operator Name: LANDOWNER GRANT PROGRAM 2006
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 41.30867769
Longitude: -83.58206864

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1152132480 2006-07-05 Witnessed completion of plugging well. The operator attempted to plug the well on 6/30/06 with inspector Sam Faust but in hole obstruction prevented cementing. Obstruction was cleared and well was plugged on 7/3/06 and witnessed by inspector Tom Benko. Operator pumped 125 sacks of cement in well but there was no cement return to the surface on that day. On 7/5/06 the operator determined the cement depth at 476 feet and pumped an additional 75 bags of cement which include 1% CaCl. Cement returned to the surface but then fell to about 10 feet below top of pipe. Additional cement will be mixed and added when pipe is cut off and ID plate attached. Problems occurred in hole when the operator tried to have the 4 inch casing shot to remove the casing. Apparently the 6 inch casing was shot by mistake which may have resulted in an obstruction in the pipe. The 4 inch casing was then shot and the casing removed.
1152543094 2006-07-03 Plug well. Circulate tubing to 952 feet. Six inch casing was shot at 394 feet thinking it was the four inch casing. Shot the four inch casing at 277 feet and pulled casing. Shale / clay fell into well. Tubing was plugged with shale when run in hole, pulled tubing and re ran to 952. Well plugged with cement.
1156968867 2006-08-30 Area around well head is being used for livestock. No cement remaining on ground. Final restoration approved.
-1.74881E+15 2004-08-05 Reviewed oil well on site for I&O program. The landowner said an application was submitted 10 years ago for I&O when house was built but there is no record in Columbus. Landowner is now considering selling property. Tanks and junk around well were removed at property owners expense. There was no production equipment but the tubing and rods were in place. No sign of contamination around well. Well is within 200 feet of water well and pond.
-847062622 2006-07-13 All equipment removed from site. Well has been cut off below ground and backfilled. Operator said ID plate was attached. It does not appear as though the site has been seeded and cement on ground from plugging needs to be cleaned up.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.