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Difference between revisions of "34-067-20600"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-067-20600
 
| Well ID: 34-067-20600
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.2028837057, -81.2798208714 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.20288371, -81.27982087 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Harrison County, Ohio|Harrison]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[EXCO - NORTH COAST ENERGY INC]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
 
| Spud Date: 1983-02-06
 
| Spud Date: 1983-02-06
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing: No
+
| Well Status: Final Restoration
 
|-
 
|-
 
| Violations: 0
 
| Violations: 0
 
|-
 
|-
| Latitude: 40.2028837057
+
| Latitude: 40.20288371
 
|-
 
|-
| Longitude: -81.2798208714
+
| Longitude: -81.27982087
 
|-
 
|-
 
|}
 
|}
Line 43: Line 43:
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
!scope="col" | OIL PRODUCTION DAYS
 +
|-
 +
| 1985-0
 +
| style="text-align:right;" | 28942.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 100.0
 +
|
 +
|-
 +
|-
 +
| 1987-0
 +
| style="text-align:right;" | 9558.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 116.0
 +
|
 +
|-
 +
|-
 +
| 1988-0
 +
| style="text-align:right;" | 4862.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1989-0
 +
| style="text-align:right;" | 2085.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 81.0
 +
|
 +
|-
 +
|-
 +
| 1990-0
 +
| style="text-align:right;" | 1191.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1991-0
 +
| style="text-align:right;" | 907.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1992-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1993-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1994-0
 +
| style="text-align:right;" | 121.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1995-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1996-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1997-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1998-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 1999-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2000-0
 +
| style="text-align:right;" | 273.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2001-0
 +
| style="text-align:right;" | 0.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 +
|-
 +
| 2002-0
 +
| style="text-align:right;" | 82.0
 +
|
 +
|
 +
|
 +
| style="text-align:right;" | 0.0
 +
|
 +
|-
 
|}
 
|}
== Waste Data ==
+
For data sources see<ref>{{cite web
{| class="wikitable sortable" width="95%"
+
| title = Ohio Department of Natural Resources RBDMS
!scope="col" | PERIOD
+
| publisher = [http://oilandgas.ohiodnr.gov/]
!scope="col" | TYPE
+
| date = 2015-06-19
!scope="col" | QUANTITY
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
!scope="col" | UNITS
+
| accessdate = 2015-06-20 }}</ref>
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
|}
 
 
== Inspection Data ==
 
== Inspection Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
Line 64: Line 211:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
|-
 
| -1155455712
 
| 2002-12-11
 
|
 
|  On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 
|
 
|
 
|
 
|-
 
|-
 
| -1338394820
 
| 2002-12-04
 
|
 
| W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
 
|
 
|
 
|
 
|-
 
|-
 
| -1701414275
 
| 2002-12-11
 
|
 
|  On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1039704373
 
| 1039704373
 
| 2002-11-18
 
| 2002-11-18
|
+
|  
 
| Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is  reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
 
| Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is  reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1039711345
 
| 1039711345
 
| 2002-12-03
 
| 2002-12-03
|
+
|  
 
| Rig  is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
 
| Rig  is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1155455712
 +
| 2002-12-11
 +
|
 +
| On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1237972050
 
| 1237972050
 
| 2002-11-19
 
| 2002-11-19
|
+
|  
 
| W/O operator to arrive and again a no show ?
 
| W/O operator to arrive and again a no show ?
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1287640570
 
| 1287640570
 
| 2002-12-12
 
| 2002-12-12
|
+
|  
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
+
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1338394820
 +
| 2002-12-04
 +
|
 +
| W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1412318881
 
| 1412318881
 
| 2002-12-12
 
| 2002-12-12
|
+
|  
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
+
| On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 1686216299
 
| 1686216299
 
| 2002-11-20
 
| 2002-11-20
|
+
|  
 
| Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
 
| Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -1701414275
 +
| 2002-12-11
 +
|
 +
| On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|-
 
|-
 
| 1864244869
 
| 1864244869
 
| 2013-09-16
 
| 2013-09-16
|
+
|  
 
| On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
 
| On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 648503960
 
| 648503960
 
| 2002-11-15
 
| 2002-11-15
|
+
|  
 
| Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The
 
| Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 07:17, 16 July 2015

Well Details

Well ID: 34-067-20600
Loading map...
County: Harrison
Municipality:
Operator Name: EXCO - NORTH COAST ENERGY INC
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date: 1983-02-06
Unconventional: No
Configuration: Vertical
Well Status: Final Restoration
Violations: 0
Latitude: 40.20288371
Longitude: -81.27982087

Production Data

PERIOD GAS QUANTITY GAS PRODUCTION DAYS CONDENSATE QUANTITY CONDENSATE PRODUCTION DAYS OIL QUANTITY OIL PRODUCTION DAYS
1985-0 28942.0 100.0
1987-0 9558.0 116.0
1988-0 4862.0 0.0
1989-0 2085.0 81.0
1990-0 1191.0 0.0
1991-0 907.0 0.0
1992-0 0.0 0.0
1993-0 0.0 0.0
1994-0 121.0 0.0
1995-0 0.0 0.0
1996-0 0.0 0.0
1997-0 0.0 0.0
1998-0 0.0 0.0
1999-0 0.0 0.0
2000-0 273.0 0.0
2001-0 0.0 0.0
2002-0 82.0 0.0

For data sources see[1]

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
1039704373 2002-11-18 Arrive to check on site after an explosion had occorred at wellsite . Found that the 8 inch casing appears to have collapsed and landed on the heavy wall conductor pipe with enough force to bell it outward . The well is not leaking badly at this time , there is reading of 18 TO 20 PPM H 2 S . Found that the operator is not going to arrive any time soon .
1039711345 2002-12-03 Rig is over the hole and is going in with tubing and will try and circulate well . Next rig had equipment problem and will reschedule work for Weds. Or Thurs.Review well with Inspector Grimm due to H 2S readings .
-1155455712 2002-12-11 On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
1237972050 2002-11-19 W/O operator to arrive and again a no show ?
1287640570 2002-12-12 On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
-1338394820 2002-12-04 W /O Operator to arrive and after contacting their office I found that job had been cancelled for today .
1412318881 2002-12-12 On location to witness plug job . The plug job was cancelled again today . Departed the location and went to the New Philadelphia office . I was advised by phone that they aren't going to plug the well until next week .
1686216299 2002-11-20 Arrive and found that service rig is over the hole and pulling tubing . Collected H2S reading at the 6 to 8 ppm range . Advise operator to maintain fluid level to avoid a possible kick . At this point there is not a way to control the well is a kick occurs . Check this well with Inspector Grimm due to the H 2 S potenial .The rig kis not running fast enough to be able to set plug today .
-1701414275 2002-12-11 On location to witness plug job . Waited on location and nobody showed up to plug the well while I was on location . Departed location and went to the New Philadelphia office . Talked with Inspector Mark Moreland and he advised that he had talked with North Coast personel and they advised that they are going to plug the well tomorrow .
1864244869 2013-09-16 On the day of my inspection I witnessed that the pit had been filled, vegetation was in place. All production equipment had been removed. Site passed according to 1509.072B.
648503960 2002-11-15 Arrive on site to cover possible blow out of H2S On a well to be plugged .Found H2S at low level and gas at the wellhead that set off the lower explosive limit on gas detector . Found that the surface casing has colapsed down onto the surface casing . The

For data sources see[2]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20. 
  2. "Ohio Department of Natural Resources RBDMS". [2]. 2015-06-19. Retrieved 2015-06-20.