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Difference between revisions of "34-167-63818"

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{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-167-63818
 
| Well ID: 34-167-63818
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.5727089162, -81.1659575914 | width=100% | height=100% }}
+
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.57270892, -81.16595759 | width=100% | height=100% }}  
 
|-
 
|-
| County:
+
| County: [[Washington County, Ohio|Washington]]
 
|-
 
|-
| Municipality:
+
| Municipality:  
 
|-
 
|-
| Operator Name:
+
| Operator Name: [[HISTORIC OWNER]]
 
|-
 
|-
| Well Pad ID:
+
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:
+
| Farm/Lease Name:  
 
|-
 
|-
| First Permit Date:
+
| First Permit Date:  
 
|-
 
|-
| Last Permit Date:
+
| Last Permit Date:  
 
|-
 
|-
| Spud Date:
+
| Spud Date:  
 
|-
 
|-
| Unconventional:
+
| Unconventional: No
 
|-
 
|-
| Horizontal:
+
| Configuration: Vertical
 
|-
 
|-
| Producing:
+
| Well Status:  
 
|-
 
|-
| Violations: 1
+
| Violations: 0
 
|-
 
|-
| Latitude: 39.5727089162
+
| Latitude: 39.57270892
 
|-
 
|-
| Longitude: -81.1659575914
+
| Longitude: -81.16595759
 
|-
 
|-
|}
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | GAS QUANTITY
 
!scope="col" | GAS PRODUCTION DAYS
 
!scope="col" | CONDENSATE QUANTITY
 
!scope="col" | CONDENSATE PRODUCTION DAYS
 
!scope="col" | OIL QUANTITY
 
!scope="col" | OIL PRODUCTION DAYS
 
|}
 
== Waste Data ==
 
{| class="wikitable sortable" width="95%"
 
!scope="col" | PERIOD
 
!scope="col" | TYPE
 
!scope="col" | QUANTITY
 
!scope="col" | UNITS
 
!scope="col" | DISPOSAL METHOD
 
!scope="col" | WASTE FACILITY PERMIT ID
 
!scope="col" | WASTE FACILITY NAME
 
!scope="col" | FACILITY CITY
 
!scope="col" | FACILITY STATE
 
 
|}
 
|}
 
== Inspection Data ==
 
== Inspection Data ==
Line 64: Line 42:
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION CODE
!scope="col" | VIOLATION_COMMENT
+
!scope="col" | VIOLATION COMMENT
 
|-
 
|-
 
| -1053162938
 
| -1053162938
 
| 2014-03-11
 
| 2014-03-11
|
+
|  
 
| Well owner has made no attempt to gain compliance.  There is still a line coming from the knockout tank down over the hill and into the streambed.  I will contact her again and to try and get her to correct the issue.  New pictures taken.  Accompanied by Inspector LJ Parkins.
 
| Well owner has made no attempt to gain compliance.  There is still a line coming from the knockout tank down over the hill and into the streambed.  I will contact her again and to try and get her to correct the issue.  New pictures taken.  Accompanied by Inspector LJ Parkins.
|
+
|  
|
+
|  
|
+
| Phone Call
 
|-
 
|-
 
|-
 
|-
 
| -1106952617
 
| -1106952617
 
| 2013-11-18
 
| 2013-11-18
|
+
|  
 
| Well is equipped for production with a pumping unit and electric motor.  It has been pumped recently.  The tank battery consists of 1 100 barrel tank with a knock out on top of it.  A piece of white PVC is plumbed into the knockout and runs outside of the dike and is reduced to 1 in black plastic line, and from there runs over the hill.  The end of that line is open.  I spoke with Mrs. Rinard, who owns the well and told her that she wasn't allowed to do this.  She agreed to my terms and will be making provisions to have brine hauled.  We spoke via cell phone on 11/19/13 at 8:42 AM.
 
| Well is equipped for production with a pumping unit and electric motor.  It has been pumped recently.  The tank battery consists of 1 100 barrel tank with a knock out on top of it.  A piece of white PVC is plumbed into the knockout and runs outside of the dike and is reduced to 1 in black plastic line, and from there runs over the hill.  The end of that line is open.  I spoke with Mrs. Rinard, who owns the well and told her that she wasn't allowed to do this.  She agreed to my terms and will be making provisions to have brine hauled.  We spoke via cell phone on 11/19/13 at 8:42 AM.
|
+
|  
| NONE(A)
+
|  
|
+
|  
|-
 
|-
 
| -994935272
 
| 2014-03-26
 
|
 
| Knockout tank has been removed from the top of the 100 barrel production tank.  The brine line that lead to the creek has been removed.  Owner has gained compliance as far as environmental regulations.  However the owner still needs to register with the state.  I spoke with Mr. Bobby Kroll.  His wife handle's the paperwork for Ms. Susan Rinard.  He stated he would ask her about it.
 
|
 
|
 
|
 
 
|-
 
|-
 
|-
 
|-
 
| 1109845568
 
| 1109845568
 
| 2014-03-11
 
| 2014-03-11
|
+
|  
 
| On March 11, 2014, I accompanied Inspector Andy Thomas on a follow up inspection of this well. Upon inspection, it was observed that this well is not yet in compliance. The brine line coming out of the knockout tank is still running downhill and into the creek bed on the lease property. Andy Thomas will contact the well owner (Susan Rinard) about the violation and notify her that brine cannot be released in this manner.
 
| On March 11, 2014, I accompanied Inspector Andy Thomas on a follow up inspection of this well. Upon inspection, it was observed that this well is not yet in compliance. The brine line coming out of the knockout tank is still running downhill and into the creek bed on the lease property. Andy Thomas will contact the well owner (Susan Rinard) about the violation and notify her that brine cannot be released in this manner.
|
+
|  
|
+
|  
|
+
|  
 
|-
 
|-
 
|-
 
|-
 
| 2114020055
 
| 2114020055
 
| 2013-11-18
 
| 2013-11-18
|
+
|  
 
| Inspection this day with Andy Thomas to show him the Susan Rinard wells, as requested by Columbus.
 
| Inspection this day with Andy Thomas to show him the Susan Rinard wells, as requested by Columbus.
|
+
|
|
+
|
|
+
|
 +
|-
 +
|-
 +
| -994935272
 +
| 2014-03-26
 +
|
 +
| Knockout tank has been removed from the top of the 100 barrel production tank.  The brine line that lead to the creek has been removed.  Owner has gained compliance as far as environmental regulations.  However the owner still needs to register with the state.  I spoke with Mr. Bobby Kroll.  His wife handle's the paperwork for Ms. Susan Rinard.  He stated he would ask her about it.
 +
|  
 +
|  
 +
|  
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Ohio Department of Natural Resources RBDMS
 +
| publisher = [http://oilandgas.ohiodnr.gov/]
 +
| date = 2015-06-19
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 +
| accessdate = 2015-06-20 }}</ref>
 +
== References ==
 +
{{reflist}}
 
__NOEDITSECTION__
 
__NOEDITSECTION__
 
[[Category:Wells]]
 
[[Category:Wells]]

Revision as of 09:43, 16 July 2015

Well Details

Well ID: 34-167-63818
Loading map...
County: Washington
Municipality:
Operator Name: HISTORIC OWNER
Well Pad ID:
Farm/Lease Name:
First Permit Date:
Last Permit Date:
Spud Date:
Unconventional: No
Configuration: Vertical
Well Status:
Violations: 0
Latitude: 39.57270892
Longitude: -81.16595759

Inspection Data

INSPECTION ID DATE DESCRIPTION COMMENT VIOLATION ID VIOLATION CODE VIOLATION COMMENT
-1053162938 2014-03-11 Well owner has made no attempt to gain compliance. There is still a line coming from the knockout tank down over the hill and into the streambed. I will contact her again and to try and get her to correct the issue. New pictures taken. Accompanied by Inspector LJ Parkins. Phone Call
-1106952617 2013-11-18 Well is equipped for production with a pumping unit and electric motor. It has been pumped recently. The tank battery consists of 1 100 barrel tank with a knock out on top of it. A piece of white PVC is plumbed into the knockout and runs outside of the dike and is reduced to 1 in black plastic line, and from there runs over the hill. The end of that line is open. I spoke with Mrs. Rinard, who owns the well and told her that she wasn't allowed to do this. She agreed to my terms and will be making provisions to have brine hauled. We spoke via cell phone on 11/19/13 at 8:42 AM.
1109845568 2014-03-11 On March 11, 2014, I accompanied Inspector Andy Thomas on a follow up inspection of this well. Upon inspection, it was observed that this well is not yet in compliance. The brine line coming out of the knockout tank is still running downhill and into the creek bed on the lease property. Andy Thomas will contact the well owner (Susan Rinard) about the violation and notify her that brine cannot be released in this manner.
2114020055 2013-11-18 Inspection this day with Andy Thomas to show him the Susan Rinard wells, as requested by Columbus.
-994935272 2014-03-26 Knockout tank has been removed from the top of the 100 barrel production tank. The brine line that lead to the creek has been removed. Owner has gained compliance as far as environmental regulations. However the owner still needs to register with the state. I spoke with Mr. Bobby Kroll. His wife handle's the paperwork for Ms. Susan Rinard. He stated he would ask her about it.

For data sources see[1]

References

  1. "Ohio Department of Natural Resources RBDMS". [1]. 2015-06-19. Retrieved 2015-06-20.