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{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-133-22027 | | Well ID: 34-133-22027 | ||
− | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41. | + | | style="height=100%; align=center" rowspan="15" | {{#display_map: 41.31705903, -81.0090263 | width=100% | height=100% }} |
|- | |- | ||
− | | County: | + | | County: [[Portage County, Ohio|Portage]] |
|- | |- | ||
− | | Municipality: | + | | Municipality: |
|- | |- | ||
− | | Operator Name: | + | | Operator Name: [[SPOLARICH ALBERT & ANNE]] |
|- | |- | ||
− | | Well Pad ID: | + | | Well Pad ID: |
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: |
|- | |- | ||
− | | First Permit Date: | + | | First Permit Date: |
|- | |- | ||
− | | Last Permit Date: | + | | Last Permit Date: |
|- | |- | ||
| Spud Date: 1980-06-19 | | Spud Date: 1980-06-19 | ||
|- | |- | ||
− | | Unconventional: | + | | Unconventional: No |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Well Status: Final Restoration |
|- | |- | ||
| Violations: 0 | | Violations: 0 | ||
|- | |- | ||
− | | Latitude: 41. | + | | Latitude: 41.31705903 |
|- | |- | ||
− | | Longitude: -81. | + | | Longitude: -81.0090263 |
|- | |- | ||
|} | |} | ||
Line 43: | Line 43: | ||
!scope="col" | OIL QUANTITY | !scope="col" | OIL QUANTITY | ||
!scope="col" | OIL PRODUCTION DAYS | !scope="col" | OIL PRODUCTION DAYS | ||
+ | |- | ||
+ | | 1984-0 | ||
+ | | style="text-align:right;" | 1117.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 140.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1985-0 | ||
+ | | style="text-align:right;" | 1320.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 165.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1986-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1987-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1988-0 | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
+ | |- | ||
+ | | 1989-0 | ||
+ | | style="text-align:right;" | 388.0 | ||
+ | | | ||
+ | | | ||
+ | | | ||
+ | | style="text-align:right;" | 0.0 | ||
+ | | | ||
+ | |- | ||
|} | |} | ||
− | + | For data sources see<ref>{{cite web | |
− | + | | title = Ohio Department of Natural Resources RBDMS | |
− | + | | publisher = [http://oilandgas.ohiodnr.gov/] | |
− | + | | date = 2015-06-19 | |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production | |
− | + | | accessdate = 2015-06-20 }}</ref> | |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
== Inspection Data == | == Inspection Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 64: | Line 112: | ||
!scope="col" | VIOLATION ID | !scope="col" | VIOLATION ID | ||
!scope="col" | VIOLATION CODE | !scope="col" | VIOLATION CODE | ||
− | !scope="col" | | + | !scope="col" | VIOLATION COMMENT |
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1371237638 | | 1371237638 | ||
| 2013-05-16 | | 2013-05-16 | ||
− | | | + | | |
| I was on location to check the restoration status of this plugged and abandoned domestic well. The tank battery had been disassembled and all surface equipment was removed from the location. Mr. Spolarich had just finished grading the areas of the wellhead and tank battery. This location has been restored. Final restoration is approved. | | I was on location to check the restoration status of this plugged and abandoned domestic well. The tank battery had been disassembled and all surface equipment was removed from the location. Mr. Spolarich had just finished grading the areas of the wellhead and tank battery. This location has been restored. Final restoration is approved. | ||
− | | | + | | |
− | | | + | | |
− | | | + | | |
+ | |- | ||
+ | |- | ||
+ | | -1591275900 | ||
+ | | 2013-05-01 | ||
+ | | | ||
+ | | I was on location with inspector Kevin Perry and Nick's Well Plugging to spot the bottom plug in this well. There was approximately 4,176' of 1.5 tubing in the well to spot the bottom plug. Nick's rigged up, began circulating the hole, mixed and pumped 6.3 barrels of cement, and displaced the cement with 9.3 barrels of water. The tubing was pulled and the wellhead was shut-in for the night. No violations. | ||
+ | | | ||
+ | | | ||
+ | | | ||
|- | |- | ||
|- | |- | ||
| 2011702581 | | 2011702581 | ||
| 2013-05-02 | | 2013-05-02 | ||
− | | | + | | |
− | | I was on location with inspector Kevin Perry and Nick's Well Plugging to plug and abandon this domestic well. Nick's ran in the hole and tagged the Clinton plug at a depth of 3806'. They pulled up the hole and ripped the 4.5 | + | | I was on location with inspector Kevin Perry and Nick's Well Plugging to plug and abandon this domestic well. Nick's ran in the hole and tagged the Clinton plug at a depth of 3806'. They pulled up the hole and ripped the 4.5 casing at 2745' and pulled 4-42' joints to set the Big Lime plug. They pulled 48 more joints and set a 200' plug across the bottom of the surface casing and pulled 7 joints to set the surface plug. The hole was circulated prior to setting each plug and the hole was topped off after setting the surface plug. The cement held and the casing was cut off 36 below grade. The ID sign was welded on and the circulating pit was closed. The surface equipment will be removed tomorrow. This well has been properly plugged and abandoned. See plugging report for details on this job. No violations. |
− | | | + | | |
− | | | + | | |
− | | | + | | |
|- | |- | ||
|} | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Ohio Department of Natural Resources RBDMS | ||
+ | | publisher = [http://oilandgas.ohiodnr.gov/] | ||
+ | | date = 2015-06-19 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection | ||
+ | | accessdate = 2015-06-20 }}</ref> | ||
+ | == References == | ||
+ | {{reflist}} | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Wells]] | [[Category:Wells]] |
Well ID: 34-133-22027 | Loading map...
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County: Portage | |
Municipality: | |
Operator Name: SPOLARICH ALBERT & ANNE | |
Well Pad ID: | |
Farm/Lease Name: | |
First Permit Date: | |
Last Permit Date: | |
Spud Date: 1980-06-19 | |
Unconventional: No | |
Configuration: Vertical | |
Well Status: Final Restoration | |
Violations: 0 | |
Latitude: 41.31705903 | |
Longitude: -81.0090263 |
PERIOD | GAS QUANTITY | GAS PRODUCTION DAYS | CONDENSATE QUANTITY | CONDENSATE PRODUCTION DAYS | OIL QUANTITY | OIL PRODUCTION DAYS |
---|---|---|---|---|---|---|
1984-0 | 1117.0 | 140.0 | ||||
1985-0 | 1320.0 | 165.0 | ||||
1986-0 | 0.0 | 0.0 | ||||
1987-0 | 0.0 | 0.0 | ||||
1988-0 | 0.0 | 0.0 | ||||
1989-0 | 388.0 | 0.0 |
For data sources see[1]
INSPECTION ID | DATE | DESCRIPTION | COMMENT | VIOLATION ID | VIOLATION CODE | VIOLATION COMMENT |
---|---|---|---|---|---|---|
1371237638 | 2013-05-16 | I was on location to check the restoration status of this plugged and abandoned domestic well. The tank battery had been disassembled and all surface equipment was removed from the location. Mr. Spolarich had just finished grading the areas of the wellhead and tank battery. This location has been restored. Final restoration is approved. | ||||
-1591275900 | 2013-05-01 | I was on location with inspector Kevin Perry and Nick's Well Plugging to spot the bottom plug in this well. There was approximately 4,176' of 1.5 tubing in the well to spot the bottom plug. Nick's rigged up, began circulating the hole, mixed and pumped 6.3 barrels of cement, and displaced the cement with 9.3 barrels of water. The tubing was pulled and the wellhead was shut-in for the night. No violations. | ||||
2011702581 | 2013-05-02 | I was on location with inspector Kevin Perry and Nick's Well Plugging to plug and abandon this domestic well. Nick's ran in the hole and tagged the Clinton plug at a depth of 3806'. They pulled up the hole and ripped the 4.5 casing at 2745' and pulled 4-42' joints to set the Big Lime plug. They pulled 48 more joints and set a 200' plug across the bottom of the surface casing and pulled 7 joints to set the surface plug. The hole was circulated prior to setting each plug and the hole was topped off after setting the surface plug. The cement held and the casing was cut off 36 below grade. The ID sign was welded on and the circulating pit was closed. The surface equipment will be removed tomorrow. This well has been properly plugged and abandoned. See plugging report for details on this job. No violations. |
For data sources see[2]