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Difference between revisions of "34-115-21984"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-115-21984
 
| Well ID: 34-115-21984
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.66746641, -81.99753362 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.667397309, -81.99767116 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Morgan County, Ohio|Morgan]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[ALTIER H L SERVICE CO INC]]
+
| County: [[Morgan_County,_Ohio|Morgan]]
 +
|-
 +
| Municipality: [[Deerfield,_Morgan_County,_Ohio|Deerfield]]
 +
|-
 +
| Operator Name: [[H L ALTIER SERVICE CO INC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: TAYLOR
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2015-09-01
 
|-
 
|-
 
| Spud Date: 1980-02-18
 
| Spud Date: 1980-02-18
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1980-03-24
 +
|-
 +
| Well Total Depth: 1378 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Plugged and Abandoned
+
| Latitude: 39.667397309
 
|-
 
|-
| Violations: 0
+
| Longitude: -81.99767116
|-
+
|}
| Latitude: 39.66746641
+
For data sources see<ref name=RBDMS>{{cite web
 +
| title = RBDMS
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" style="width: 50%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 
|-
 
|-
| Longitude: -81.99753362
+
| 2006-09-11
 +
| style="text-align: right;" | 1339
 +
| style="text-align: right;" | 1343
 +
| style="text-align: right;" | 1
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref name = RBDMS/>
 
== Production Data ==
 
== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Period
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | OIL QUANTITY
+
|-
!scope="col" | OIL PRODUCTION DAYS
+
| 1991
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 25
 +
| style="text-align: right;" | 35
 +
|-
 +
| 1992
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 20
 +
| style="text-align: right;" | 30
 
|-
 
|-
| 1991-0
+
| 1993
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 20
|  
+
| style="text-align: right;" | 30
| style="text-align:right;" | 25.0
 
|
 
 
|-
 
|-
 +
| 1994
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 20
 +
| style="text-align: right;" | 30
 
|-
 
|-
| 1992-0
+
| 1995
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 5
|  
+
| style="text-align: right;" | 30
| style="text-align:right;" | 20.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1993-0
+
| 2010
|  
+
| [[H L ALTIER SERVICE CO INC]]
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 20.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1994-0
+
| 2012
|  
+
| [[H L ALTIER SERVICE CO INC]]
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 20.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1995-0
+
|}
| style="text-align:right;" | 0.0
+
For data sources see<ref name=RBDMS/><ref name = Annual_Prod>{{cite web
|  
+
| title = Ohio Combined Annual Production Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date = 2019-05-07
| style="text-align:right;" | 5.0
+
| url = http://wellwiki.org/wiki/Pennsylvania_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1991
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| Brine
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 35
 
|-
 
|-
| 2009-0
+
| 1992
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 10
|
+
| style="text-align: right;" | 30
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| Brine
 +
| style="text-align: right;" | 10
 +
| style="text-align: right;" | 30
 
|-
 
|-
| 2010-0
+
| 1994
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 10
|
+
| style="text-align: right;" | 30
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| Brine
 +
| style="text-align: right;" | 5
 +
| style="text-align: right;" | 30
 
|-
 
|-
| 2011-0
+
| 2009
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2012-0
+
| 2011
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[H L ALTIER SERVICE CO INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2013-0
+
| 2013
| style="text-align:right;" | 0.0
+
| [[H L ALTIER SERVICE CO INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
For data sources see<ref>{{cite web
+
For data sources see<ref name=RBDMS/><ref name=Annual_Prod/>
| title = Ohio Department of Natural Resources RBDMS
 
| publisher = [http://oilandgas.ohiodnr.gov/]
 
| date = 2015-06-19
 
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
 
| accessdate = 2015-06-20 }}</ref>
 
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0199750800
 +
| 2015-09-01
 +
| Final Restoration
 +
| No Violations
 +
| The final restoration meets 1509.072B.
 +
|-
 +
| 0242332708
 +
| 2013-07-12
 +
| Production Wells
 +
| Violations Noted
 +
| I found an overgrown pumpjack with valves open however I could no find the tank associated with this well. It is hard to tell if this well is actually in production especially since no production has been reported since 1995. I called Tim Altier and left a message concerning the issues. Operator must report production to the state, and operator must post ID and must make well capable of production within 60 days; or plugging is required in 60 days. 7/16/2013: Tim Altier called and said the well is incapable of producing and it is no longer providing house gas. He is going to try and work out a way to plug the well.
 +
|-
 +
| 0443538079
 +
| 2015-02-12
 +
| Plug / Plug Back
 +
| No Violations
 +
| The casing, tubing, and pumpjack are still on location. The areas has not yet been graded and there are still pieces of steel and plastic flowline in various places as well as the electric wire. I will continue to monitor the restoration.
 +
|-
 +
| 0734533749
 +
| 2005-09-14
 +
| Production Wells
 +
| No Violations
 +
| Well appears to be hooked up,but no production has been reported on well in quite some time.
 +
Will need to contact company rep and find out why they are not reporting production.
 +
|-
 +
| 0826272942
 +
| 2014-06-23
 +
| Production Wells
 +
| No Violations
 +
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues.
 
|-
 
|-
 
| 1022431627
 
| 1022431627
 
| 2013-10-21
 
| 2013-10-21
|  
+
| Production Wells
 +
| No Violations
 
| Compliance Action Follow-up -242332708: There has been no resolution to any of the issues.
 
| Compliance Action Follow-up -242332708: There has been no resolution to any of the issues.
|
 
|
 
| Phone Call
 
|-
 
 
|-
 
|-
| -1099003537
+
| 1099003537
 
| 2014-02-13
 
| 2014-02-13
|  
+
| Production Wells
 +
| No Violations
 
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I left a message with Tim Altier in regards to the well issues.
 
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I left a message with Tim Altier in regards to the well issues.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1346795453
 
| 1346795453
 
| 2015-01-23
 
| 2015-01-23
|  
+
| Plug / Plug Back
| I was onsite to witness the plugging of this well. Kenny Wright and his rig crew were on location when I arrived. They rigged up their 4 tools to tag the cement plug. They ran the tools down hole and tagged the plug at 1042'. They then brought the tools back out of the hole and put the ripper on the bottom. They ran back in the well to find telegraph and started ripping the 4.5 at 826ft. They were able to rip the 4.5 at 826ft. The 4.5 was pulled up to 370ft and a plug was set to the surface. The well will be left open over the weekend and checked on Monday .
+
| No Violations
|
+
| I was onsite to witness the plugging of this well. Kenny Wright and his rig crew were on location when I arrived. They rigged up their 4 tools to tag the cement plug. They ran the tools down hole and tagged the plug at 1042. They then brought the tools back out of the hole and put the ripper on the bottom. They ran back in the well to find telegraph and started ripping the 4.5 at 826ft. They were able to rip the 4.5 at 826ft. The 4.5 was pulled up to 370ft and a plug was set to the surface. The well will be left open over the weekend and checked on Monday .
|
 
|
 
|-
 
 
|-
 
|-
 
| 1422293310
 
| 1422293310
 
| 2015-01-22
 
| 2015-01-22
|  
+
| Plug / Plug Back
| I was on location to witness Kenny Wright of Wright Well Services and formation Cement Company set the bottom hole Berea Plug. Formation set the plug from 1124-1378' using 20 sacks of Class A cement.
+
| No Violations
|
+
| I was on location to witness Kenny Wright of Wright Well Services and formation Cement Company set the bottom hole Berea Plug. Formation set the plug from 1124-1378 using 20 sacks of Class A cement.
|
 
|
 
|-
 
 
|-
 
|-
| -1549856405
+
| 1549856405
 
| 2014-06-23
 
| 2014-06-23
|  
+
| Production Wells
 +
| No Violations
 
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I talked to Tim Altier and he is going to apply for a plug permit this week and line up a rig for this summer to plug the well.
 
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I talked to Tim Altier and he is going to apply for a plug permit this week and line up a rig for this summer to plug the well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1878098072
+
| 1878098072
 
| 2015-03-26
 
| 2015-03-26
|  
+
| Plug / Plug Back
| The pumpjack and casing was still on location. There were sections of line still lying around and the wellhead was still open with cement around 10' down. I met with Pat Altier and he stated he was in charge of restoration and was planning on getting the location complete once the ground was dry enough to move in heavy equipment.
+
| No Violations
|
+
| The pumpjack and casing was still on location. There were sections of line still lying around and the wellhead was still open with cement around 10 down. I met with Pat Altier and he stated he was in charge of restoration and was planning on getting the location complete once the ground was dry enough to move in heavy equipment.
|
 
|
 
 
|-
 
|-
 +
| 2112382723
 +
| 2015-07-08
 +
| Final Restoration
 +
| No Violations
 +
| I went out to this well to do a final restoration on it. I was unable to pass the final restoration because the well has not been cut off at the surface. The plastic line is still on location along with the pumping unit and some electric line. Once  all the equipment and reclaiming has been done I can pass the final restoration.
 
|-
 
|-
 
| 2131060594
 
| 2131060594
 
| 2015-01-20
 
| 2015-01-20
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Kenny Wright of Wright Well Services has his service rig on location. He has removed the pumpjack and pulled the rods and 41 joints of tubing from the well. There was no activity on the well today.
 
| Kenny Wright of Wright Well Services has his service rig on location. He has removed the pumpjack and pulled the rods and 41 joints of tubing from the well. There was no activity on the well today.
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -242332708
+
| 0242332708
| 2013-07-12
+
| US-OH-122436
 +
| 2015-02-02
 
|  
 
|  
| I found an overgrown pumpjack with valves open however I could no find the tank associated with this well. It is hard to tell if this well is actually in production especially since no production has been reported since 1995. I called Tim Altier and left a message concerning the issues. Operator must report production to the state, and operator must post ID and must make well capable of production within 60 days; or plugging is required in 60 days. 7/16/2013: Tim Altier called and said the well is incapable of producing and it is no longer providing house gas. He is going to try and work out a way to plug the well.
+
| Failure to legibly identify well
 +
|-
 +
| 0242332708
 +
| US-OH-122437
 +
| 2015-02-02
 
|  
 
|  
 +
| Well shall be plugged
 +
|-
 +
| 0242332708
 +
| US-OH-122438
 +
| 2015-02-02
 
|  
 
|  
 +
| Nonproduction; well shall be plugged or placed in temporary inactive status
 +
|-
 +
| 0242332708
 +
| US-OH-122439
 +
| 2015-02-02
 
|  
 
|  
 +
| Statement of annual production not filed
 +
|-
 +
|}
 +
For data sources see<ref name=RBDMS/>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
 +
|}-->
 +
 +
== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 443538079
 
| 2015-02-12
 
|
 
| The casing, tubing, and pumpjack are still on location. The areas has not yet been graded and there are still pieces of steel and plastic flowline in various places as well as the electric wire. I will continue to monitor the restoration.
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 18000 Gal
 +
| style="text-align: right;" | 6500
 
|  
 
|  
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref name = RBDMS/>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| CO
 +
| 1979-12-12
 +
| 1512  ALTIER H L SERVICE CO INC  GeoDate  12/12/79
 
|-
 
|-
| -734533749
+
| Original Spud
| 2005-09-14
+
| 1980-02-18
|
 
| Well appears to be hooked up,but no production has been reported on well in quite some time.
 
Will need to contact company rep and find out why they are not reporting production.
 
 
|  
 
|  
 +
|-
 +
| Completed
 +
| 1980-03-24
 
|  
 
|  
 +
|-
 +
| Reached Total Depth
 +
| 1980-03-24
 
|  
 
|  
 
|-
 
|-
 +
| Correction to Well
 +
| 2008-11-07
 +
| CORRECTION TO X, Y COORDINATES; X= 2,141,410 AND Y= 607,679.
 +
|-
 +
| APP
 +
| 2014-09-29
 +
| Proposed Formations:BEREA, Issued Date:9/29/2014, Expired Date:9/28/2016 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| -826272942
+
| Plugged/Abandoned
| 2014-06-23
+
| 2015-01-23
|
 
| Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues.
 
 
|  
 
|  
 +
|-
 +
| Construction Permit Expires
 +
| 2016-09-28
 
|  
 
|  
 +
|-
 +
| Record Last Modified
 +
| 2017-02-10
 
|  
 
|  
 
|-
 
|-
 
|}
 
|}
For data sources see<ref>{{cite web
+
For data sources see<ref name=RBDMS/>
| title = Ohio Department of Natural Resources RBDMS
+
==References==
| publisher = [http://oilandgas.ohiodnr.gov/]
+
<references/>
| date = 2015-06-19
 
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
 
| accessdate = 2015-06-20 }}</ref>
 
== References ==
 
{{reflist}}
 
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 21:31, 20 July 2019

Well Details

Well ID: 34-115-21984
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Country: United States
State: Ohio
County: Morgan
Municipality: Deerfield
Operator Name: H L ALTIER SERVICE CO INC
Well Pad ID:
Farm/Lease Name: TAYLOR
License Status: Final Restoration
License Date: 2015-09-01
Spud Date: 1980-02-18
Spud Drilling Contractor:
Final Drill Date: 1980-03-24
Well Total Depth: 1378 ft
Configuration: Vertical
Latitude: 39.667397309
Longitude: -81.99767116

For data sources see[1]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 1339 1343 1

For data sources see[1]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1991 H L ALTIER SERVICE CO INC 0 25 35
1992 H L ALTIER SERVICE CO INC 0 20 30
1993 H L ALTIER SERVICE CO INC 0 20 30
1994 H L ALTIER SERVICE CO INC 0 20 30
1995 H L ALTIER SERVICE CO INC 0 5 30
2009 H L ALTIER SERVICE CO INC 0 0 0
2010 H L ALTIER SERVICE CO INC 0 0 0
2011 H L ALTIER SERVICE CO INC 0 0 0
2012 H L ALTIER SERVICE CO INC 0 0 0
2013 H L ALTIER SERVICE CO INC 0 0 0

For data sources see[1][2]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1991 H L ALTIER SERVICE CO INC Brine 10 35
1992 H L ALTIER SERVICE CO INC Brine 10 30
1993 H L ALTIER SERVICE CO INC Brine 10 30
1994 H L ALTIER SERVICE CO INC Brine 10 30
1995 H L ALTIER SERVICE CO INC Brine 5 30
2009 H L ALTIER SERVICE CO INC Brine 0 0
2010 H L ALTIER SERVICE CO INC Brine 0 0
2011 H L ALTIER SERVICE CO INC Brine 0 0
2012 H L ALTIER SERVICE CO INC Brine 0 0
2013 H L ALTIER SERVICE CO INC Brine 0 0

For data sources see[1][2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0199750800 2015-09-01 Final Restoration No Violations The final restoration meets 1509.072B.
0242332708 2013-07-12 Production Wells Violations Noted I found an overgrown pumpjack with valves open however I could no find the tank associated with this well. It is hard to tell if this well is actually in production especially since no production has been reported since 1995. I called Tim Altier and left a message concerning the issues. Operator must report production to the state, and operator must post ID and must make well capable of production within 60 days; or plugging is required in 60 days. 7/16/2013: Tim Altier called and said the well is incapable of producing and it is no longer providing house gas. He is going to try and work out a way to plug the well.
0443538079 2015-02-12 Plug / Plug Back No Violations The casing, tubing, and pumpjack are still on location. The areas has not yet been graded and there are still pieces of steel and plastic flowline in various places as well as the electric wire. I will continue to monitor the restoration.
0734533749 2005-09-14 Production Wells No Violations Well appears to be hooked up,but no production has been reported on well in quite some time.

Will need to contact company rep and find out why they are not reporting production.

0826272942 2014-06-23 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues.
1022431627 2013-10-21 Production Wells No Violations Compliance Action Follow-up -242332708: There has been no resolution to any of the issues.
1099003537 2014-02-13 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I left a message with Tim Altier in regards to the well issues.
1346795453 2015-01-23 Plug / Plug Back No Violations I was onsite to witness the plugging of this well. Kenny Wright and his rig crew were on location when I arrived. They rigged up their 4 tools to tag the cement plug. They ran the tools down hole and tagged the plug at 1042. They then brought the tools back out of the hole and put the ripper on the bottom. They ran back in the well to find telegraph and started ripping the 4.5 at 826ft. They were able to rip the 4.5 at 826ft. The 4.5 was pulled up to 370ft and a plug was set to the surface. The well will be left open over the weekend and checked on Monday .
1422293310 2015-01-22 Plug / Plug Back No Violations I was on location to witness Kenny Wright of Wright Well Services and formation Cement Company set the bottom hole Berea Plug. Formation set the plug from 1124-1378 using 20 sacks of Class A cement.
1549856405 2014-06-23 Production Wells No Violations Compliance Action Follow-up -242332708: The well is still equipped with an idle pumpjack. There has been no resolution to any of the issues. I talked to Tim Altier and he is going to apply for a plug permit this week and line up a rig for this summer to plug the well.
1878098072 2015-03-26 Plug / Plug Back No Violations The pumpjack and casing was still on location. There were sections of line still lying around and the wellhead was still open with cement around 10 down. I met with Pat Altier and he stated he was in charge of restoration and was planning on getting the location complete once the ground was dry enough to move in heavy equipment.
2112382723 2015-07-08 Final Restoration No Violations I went out to this well to do a final restoration on it. I was unable to pass the final restoration because the well has not been cut off at the surface. The plastic line is still on location along with the pumping unit and some electric line. Once all the equipment and reclaiming has been done I can pass the final restoration.
2131060594 2015-01-20 Plug / Plug Back No Violations Kenny Wright of Wright Well Services has his service rig on location. He has removed the pumpjack and pulled the rods and 41 joints of tubing from the well. There was no activity on the well today.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0242332708 US-OH-122436 2015-02-02 Failure to legibly identify well
0242332708 US-OH-122437 2015-02-02 Well shall be plugged
0242332708 US-OH-122438 2015-02-02 Nonproduction; well shall be plugged or placed in temporary inactive status
0242332708 US-OH-122439 2015-02-02 Statement of annual production not filed

For data sources see[1]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 18000 Gal 6500

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1979-12-12 1512 ALTIER H L SERVICE CO INC GeoDate 12/12/79
Original Spud 1980-02-18
Completed 1980-03-24
Reached Total Depth 1980-03-24
Correction to Well 2008-11-07 CORRECTION TO X, Y COORDINATES; X= 2,141,410 AND Y= 607,679.
APP 2014-09-29 Proposed Formations:BEREA, Issued Date:9/29/2014, Expired Date:9/28/2016 12:00:00 PM, Drilling unit acres:10, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2015-01-23
Construction Permit Expires 2016-09-28
Record Last Modified 2017-02-10

For data sources see[1]

References

  1. 1.0 1.1 1.2 1.3 1.4 1.5 1.6 "RBDMS". Ohio Department of Natural Resources. 2019-05-07. Retrieved 2019-05-21. 
  2. 2.0 2.1 "Ohio Combined Annual Production Data". Ohio Department of Natural Resources. 2019-05-07. Retrieved 2019-05-21.