X

Track changes made to this page

If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.



Privacy policy
Close this window

powered by ChangeDetection

Difference between revisions of "34-147-61121"

m
m
Line 1: Line 1:
__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-147-61121
 
| Well ID: 34-147-61121
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.15385557, -83.1746907 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.153930799, -83.17460949 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Seneca County, Ohio|Seneca]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Seneca_County,_Ohio|Seneca]]
 +
|-
 +
| Municipality: [[Clinton_Township,_Seneca_County,_Ohio|Clinton Township]]
 
|-
 
|-
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2006]]
 
| Operator Name: [[LANDOWNER GRANT PROGRAM 2006]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: WELLER DON JR
 
|-
 
|-
| First Permit Date:  
+
| License Status: Plugged and Abandoned
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2006-10-10
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Plugged and Abandoned
+
| Latitude: 41.153930799
 +
|-
 +
| Longitude: -83.17460949
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| APP
 +
| 2006-03-09
 +
| Proposed Formations:TRENTON, Issued Date:3/9/2006, Expired Date:3/9/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 
|-
 
|-
| Violations: 0
+
| Change of Owner
 +
| 2006-03-09
 +
| Operator changed from 9999, UNKNOWN OWNER to 7952, LANDOWNER GRANT PROGRAM 2006
 
|-
 
|-
| Latitude: 41.15385557
+
| Plugged by Orphan Well Program
 +
| 2006-10-10
 +
| Plugged by Orphan Well Program
 
|-
 
|-
| Longitude: -83.1746907
+
| Plugged/Abandoned
 +
| 2006-10-10
 +
| INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.
 +
I&O CN 2004 12 124
 +
|-
 +
| Construction Permit Expires
 +
| 2007-03-09
 +
| INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.
 +
I&O CN 2004 12 124
 +
|-
 +
| Record Last Modified
 +
| 2013-03-14
 +
| INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.
 +
I&O CN 2004 12 124
 
|-
 
|-
 
|}
 
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 +
<!--== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
|}-->
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| 1090236010
 
| 1090236010
 
| 2004-07-15
 
| 2004-07-15
|  
+
| Orphan
 +
| No Violations
 
| Inspect well, collect photos, Well was requested for I&O porgram, conduct lease search, No current leases.  Well condition, 8 inch casing and 6 inch casing present open hole and rusted away at surface. No tubing, or rods present. Oil is present about 4 fe
 
| Inspect well, collect photos, Well was requested for I&O porgram, conduct lease search, No current leases.  Well condition, 8 inch casing and 6 inch casing present open hole and rusted away at surface. No tubing, or rods present. Oil is present about 4 fe
|
 
|
 
|
 
|-
 
|-
 
| 1.09024E+15
 
| 2004-07-15
 
|
 
| Inspect well, collect photos, Well was requested for I&O porgram, conduct lease search, No current leases.  Well condition, 8 inch casing and 6 inch casing present open hole and rusted away at surface. No tubing, or rods present. Oil is present about 4 feet below grade.
 
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1160653632
 
| 1160653632
 
| 2006-10-10
 
| 2006-10-10
|  
+
| Plug / Plug Back
 +
| No Violations
 
| Plug well. Well was cleaned out to 995 feet. Wood plug was driven to depth. Approval was given to cement well at depth. Adjacent water well became cloudy.  100 sacks of cement were displaced to 690 feet. Second load of 100 sacks was displaced to 448 feet. Allow cement to set for several hours. Tag cement at 474 feet. Cement was taken by the production formation.  Run tubing to 448 feet pump 130 sacks of cement and top off well.
 
| Plug well. Well was cleaned out to 995 feet. Wood plug was driven to depth. Approval was given to cement well at depth. Adjacent water well became cloudy.  100 sacks of cement were displaced to 690 feet. Second load of 100 sacks was displaced to 448 feet. Allow cement to set for several hours. Tag cement at 474 feet. Cement was taken by the production formation.  Run tubing to 448 feet pump 130 sacks of cement and top off well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1821317981
+
| 1821317981
 
| 2004-06-10
 
| 2004-06-10
|  
+
| Orphan
 +
| No Violations
 
| Inspect orphan well at request of landowner. Well conditions, 8 inch casing and 6 inch casing are present, both casings are rusted away at the surface. Well is filled with fluids and oil to 6 feet below grade.
 
| Inspect orphan well at request of landowner. Well conditions, 8 inch casing and 6 inch casing are present, both casings are rusted away at the surface. Well is filled with fluids and oil to 6 feet below grade.
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -1.82132E+15
+
|}-->
| 2004-06-10
 
|
 
| Inspect orphan well at request of landowner. Well conditions, 8 inch casing and 6 inch casing are present, both casings are rusted away at the surface. Well is filled with fluids and oil to 6 feet below grade.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 15:16, 23 July 2019

Well Details

Well ID: 34-147-61121
Loading map...
Country: United States
State: Ohio
County: Seneca
Municipality: Clinton Township
Operator Name: LANDOWNER GRANT PROGRAM 2006
Well Pad ID:
Farm/Lease Name: WELLER DON JR
License Status: Plugged and Abandoned
License Date: 2006-10-10
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.153930799
Longitude: -83.17460949

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2006-03-09 Proposed Formations:TRENTON, Issued Date:3/9/2006, Expired Date:3/9/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Change of Owner 2006-03-09 Operator changed from 9999, UNKNOWN OWNER to 7952, LANDOWNER GRANT PROGRAM 2006
Plugged by Orphan Well Program 2006-10-10 Plugged by Orphan Well Program
Plugged/Abandoned 2006-10-10 INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.

I&O CN 2004 12 124

Construction Permit Expires 2007-03-09 INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.

I&O CN 2004 12 124

Record Last Modified 2013-03-14 INSPECTED BY TOM BENKO ON JULY 15, 2004. WELL WAS REQUESTED FOR I/O PROGRAM.

I&O CN 2004 12 124

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1090236010 2004-07-15 Orphan No Violations Inspect well, collect photos, Well was requested for I&O porgram, conduct lease search, No current leases. Well condition, 8 inch casing and 6 inch casing present open hole and rusted away at surface. No tubing, or rods present. Oil is present about 4 fe
1160653632 2006-10-10 Plug / Plug Back No Violations Plug well. Well was cleaned out to 995 feet. Wood plug was driven to depth. Approval was given to cement well at depth. Adjacent water well became cloudy. 100 sacks of cement were displaced to 690 feet. Second load of 100 sacks was displaced to 448 feet. Allow cement to set for several hours. Tag cement at 474 feet. Cement was taken by the production formation. Run tubing to 448 feet pump 130 sacks of cement and top off well.
1821317981 2004-06-10 Orphan No Violations Inspect orphan well at request of landowner. Well conditions, 8 inch casing and 6 inch casing are present, both casings are rusted away at the surface. Well is filled with fluids and oil to 6 feet below grade.

For data sources see[3]

References