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Difference between revisions of "34-151-22155"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-151-22155
 
| Well ID: 34-151-22155
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.80350274, -81.56102557 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.800296594, -81.56087413 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Stark County, Ohio|Stark]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[PETROX, INC]]
+
| County: [[Stark_County,_Ohio|Stark]]
 +
|-
 +
| Municipality: [[Tuscarawas_Township,_Stark_County,_Ohio|Tuscarawas Township]]
 +
|-
 +
| Operator Name: [[ENERVEST OPERATING LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: VETTE R& J
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 1970-09-01
 
|-
 
|-
 
| Spud Date: 1970-09-01
 
| Spud Date: 1970-09-01
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1970-09-16
 +
|-
 +
| Well Total Depth: 4271 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 40.800296594
 +
|-
 +
| Longitude: -81.56087413
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| CO
 +
| 1970-09-01
 +
| 182  BELDEN & BLAKE CO  GeoDate  9/1/70
 +
|-
 +
| Original Spud
 +
| 1970-09-01
 +
| EB-1021.49, KB-1028.5, LOG TYPE=HI
 +
|-
 +
| Completed
 +
| 1970-09-16
 +
| EB-1021.49, KB-1028.5, LOG TYPE=HI
 +
|-
 +
| Reached Total Depth
 +
| 1970-09-16
 +
| EB-1021.49, KB-1028.5, LOG TYPE=HI
 +
|-
 +
| Change of Owner
 +
| 2002-08-12
 +
| Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC
 +
|-
 +
| Change of Owner
 +
| 2015-01-22
 +
| Operator changed from 1966, PETROX, INC to 7578, ENERVEST OPERATING L
 
|-
 
|-
| Violations: 0
+
| Record Last Modified
 +
| 2019-06-04
 +
| EB-1021.49, KB-1028.5, LOG TYPE=HI
 
|-
 
|-
| Latitude: 40.80350274
+
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 
|-
 
|-
| Longitude: -81.56102557
+
| 2006-09-11
 +
| style="text-align: right;" | 4072
 +
| style="text-align: right;" | 4200
 +
| style="text-align: right;" | 0
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 5026.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 23350 Gal
 +
| style="text-align: right;" | 8000
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 3.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 5026
 +
| style="text-align: right;" | 3
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 4168
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1986
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 4207
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 4517
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 3903
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 +
|-
 +
| 1990
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 3102
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 356
 +
|-
 +
| 1991
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 2705
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 2528
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 359
 +
|-
 +
| 1993
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 2253
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 2162
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1985-0
+
| 1995
| style="text-align:right;" | 4168.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 1915
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 1534
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1986-0
+
| 1997
| style="text-align:right;" | 4207.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 1434
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 358
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 1544
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 358
 
|-
 
|-
| 1987-0
+
| 1999
| style="text-align:right;" | 4517.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 1436
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 1178
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 359
 
|-
 
|-
| 1988-0
+
| 2001
| style="text-align:right;" | 3903.0
+
| [[BELDEN & BLAKE CORPORATION]]
|  
+
| style="text-align: right;" | 1184
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 318
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| style="text-align: right;" | 716
 +
| style="text-align: right;" | 12
 +
| style="text-align: right;" | 140
 
|-
 
|-
| 1990-0
+
| 2003
| style="text-align:right;" | 3102.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 1055
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 921
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 2005
| style="text-align:right;" | 2705.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 1079
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 1265
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1992-0
+
| 2007
| style="text-align:right;" | 2528.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 1297
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 1182
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2009
| style="text-align:right;" | 2253.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 666
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 324
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 545
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1994-0
+
| 2011
| style="text-align:right;" | 2162.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 597
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 769
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1995-0
+
| 2013
| style="text-align:right;" | 1915.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 640
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[PETROX, INC]]
 +
| style="text-align: right;" | 744
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 2015
| style="text-align:right;" | 1534.0
+
| [[PETROX, INC]]
|  
+
| style="text-align: right;" | 190
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 60
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 837
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1997-0
+
| 2017
| style="text-align:right;" | 1434.0
+
| [[ENERVEST OPERATING LLC]]
|  
+
| style="text-align: right;" | 696
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2018
 +
| [[ENERVEST OPERATING LLC]]
 +
| style="text-align: right;" | 876
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
|}
| style="text-align:right;" | 1544.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1984
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1999-0
+
| 1985
| style="text-align:right;" | 1436.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 2
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1986
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
| 1987
| style="text-align:right;" | 1178.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1988
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 2001-0
+
| 1990
| style="text-align:right;" | 1184.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 356
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1992
| style="text-align:right;" | 716.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 359
| style="text-align:right;" | 12.0
 
|
 
 
|-
 
|-
 +
| 1993
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2003-0
+
| 1994
| style="text-align:right;" | 1055.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2004-0
+
| 1996
| style="text-align:right;" | 921.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 358
 
|-
 
|-
| 2005-0
+
| 1998
| style="text-align:right;" | 1079.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 358
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2000
| style="text-align:right;" | 1265.0
+
| [[BELDEN & BLAKE CORPORATION]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 359
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[BELDEN & BLAKE CORPORATION]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 318
 
|-
 
|-
| 2007-0
+
| 2002
| style="text-align:right;" | 1297.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 28
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2004
| style="text-align:right;" | 1182.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2006
| style="text-align:right;" | 666.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2008
| style="text-align:right;" | 545.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 324
 
|-
 
|-
| 2011-0
+
| 2010
| style="text-align:right;" | 597.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2012
| style="text-align:right;" | 769.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2013-0
+
| 2014
| style="text-align:right;" | 640.0
+
| [[PETROX, INC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[PETROX, INC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 60
 
|-
 
|-
| 2014-0
+
| 2016
| style="text-align:right;" | 744.0
+
| [[ENERVEST OPERATING LLC]]
| style="text-align:right;" | 365.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 +
| 2017
 +
| [[ENERVEST OPERATING LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2018
| style="text-align:right;" | 0.0
+
| [[ENERVEST OPERATING LLC]]
| style="text-align:right;" | 0.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 0.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 256342955
+
| 0256342955
 
| 2009-09-24
 
| 2009-09-24
|  
+
| Production Wells
 +
| No Violations
 
| The excavation around the wellhead is filled in. There is a swab rig on the well. The complaint is RESOLVED.
 
| The excavation around the wellhead is filled in. There is a swab rig on the well. The complaint is RESOLVED.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0692163391
| 692163391
 
 
| 2009-04-28
 
| 2009-04-28
|  
+
| Production Wells
 +
| No Violations
 
| I received a call on 4-27-2009 from Steve Collins (Massillon Fire Department, 330-833-1053) regarding an odor complaint at a well located at 106 Rolling Park Dr., Massillon, OH. On 4-28-2009, I met with John Casper (Rolling Hills Trailer Park) at the well site. A gas leak was reported on Sunday 4-26-2009 and the Massillon Fire Department responded. Petrox was notified and addressed the leak. During my inspection on 4-28-2009, I called Bill Magrell (330-565-5873) with Petrox to get the details of the incident. Gas had been leaking from under the production string casing hanger out of the surface casing. The surface casing was loaded with water to kill the gas. A hole was drilled in the surface casing to monitor for gas. During my inspection there was no gas present. Petrox will evaluate the leak and then repair the casing or plug the well. I informed the Massillon Fire Department of my findings. I talked to Cindy (Rolling Hills Trailer Park) later that day and informed her of the situation.
 
| I received a call on 4-27-2009 from Steve Collins (Massillon Fire Department, 330-833-1053) regarding an odor complaint at a well located at 106 Rolling Park Dr., Massillon, OH. On 4-28-2009, I met with John Casper (Rolling Hills Trailer Park) at the well site. A gas leak was reported on Sunday 4-26-2009 and the Massillon Fire Department responded. Petrox was notified and addressed the leak. During my inspection on 4-28-2009, I called Bill Magrell (330-565-5873) with Petrox to get the details of the incident. Gas had been leaking from under the production string casing hanger out of the surface casing. The surface casing was loaded with water to kill the gas. A hole was drilled in the surface casing to monitor for gas. During my inspection there was no gas present. Petrox will evaluate the leak and then repair the casing or plug the well. I informed the Massillon Fire Department of my findings. I talked to Cindy (Rolling Hills Trailer Park) later that day and informed her of the situation.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| 710964767
+
| 0710964767
 
| 2009-05-05
 
| 2009-05-05
|  
+
| Production Wells
| The excavation at the wellhead is still open. There was no visible venting or odor coming from the port in the casing. I met with Justin (Cindy's son), who is in charge of maintenance.
+
| No Violations
|
+
| The excavation at the wellhead is still open. There was no visible venting or odor coming from the port in the casing. I met with Justin (Cindys son), who is in charge of maintenance.
|
 
|
 
 
|-
 
|-
|-
+
| 0738779186
| 738779186
 
 
| 2014-03-27
 
| 2014-03-27
|  
+
| Production Wells
 +
| No Violations
 
| I was on location to obtain updated GPS coordinates for this well. During my inspection I found a plunger lift well with a 100bbl production tank and separator all enclosed in a fence. The well is located in a manufactured home park. The wellhead is in good conditioned has proper I.D. signage with 55psi of pressure on the tubing. There are no violations at this time.
 
| I was on location to obtain updated GPS coordinates for this well. During my inspection I found a plunger lift well with a 100bbl production tank and separator all enclosed in a fence. The well is located in a manufactured home park. The wellhead is in good conditioned has proper I.D. signage with 55psi of pressure on the tubing. There are no violations at this time.
|
 
|
 
|
 
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 21:07, 23 July 2019

Well Details

Well ID: 34-151-22155
Loading map...
Country: United States
State: Ohio
County: Stark
Municipality: Tuscarawas Township
Operator Name: ENERVEST OPERATING LLC
Well Pad ID:
Farm/Lease Name: VETTE R& J
License Status: Producing
License Date: 1970-09-01
Spud Date: 1970-09-01
Spud Drilling Contractor:
Final Drill Date: 1970-09-16
Well Total Depth: 4271 ft
Configuration: Vertical
Latitude: 40.800296594
Longitude: -81.56087413

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1970-09-01 182 BELDEN & BLAKE CO GeoDate 9/1/70
Original Spud 1970-09-01 EB-1021.49, KB-1028.5, LOG TYPE=HI
Completed 1970-09-16 EB-1021.49, KB-1028.5, LOG TYPE=HI
Reached Total Depth 1970-09-16 EB-1021.49, KB-1028.5, LOG TYPE=HI
Change of Owner 2002-08-12 Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC
Change of Owner 2015-01-22 Operator changed from 1966, PETROX, INC to 7578, ENERVEST OPERATING L
Record Last Modified 2019-06-04 EB-1021.49, KB-1028.5, LOG TYPE=HI

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 4072 4200 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 23350 Gal 8000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BELDEN & BLAKE CORPORATION 5026 3 0
1985 BELDEN & BLAKE CORPORATION 4168 0 0
1986 BELDEN & BLAKE CORPORATION 4207 0 365
1987 BELDEN & BLAKE CORPORATION 4517 0 365
1988 BELDEN & BLAKE CORPORATION 3903 0 366
1990 BELDEN & BLAKE CORPORATION 3102 0 356
1991 BELDEN & BLAKE CORPORATION 2705 0 365
1992 BELDEN & BLAKE CORPORATION 2528 0 359
1993 BELDEN & BLAKE CORPORATION 2253 0 365
1994 BELDEN & BLAKE CORPORATION 2162 0 365
1995 BELDEN & BLAKE CORPORATION 1915 0 365
1996 BELDEN & BLAKE CORPORATION 1534 0 366
1997 BELDEN & BLAKE CORPORATION 1434 0 358
1998 BELDEN & BLAKE CORPORATION 1544 0 358
1999 BELDEN & BLAKE CORPORATION 1436 0 365
2000 BELDEN & BLAKE CORPORATION 1178 0 359
2001 BELDEN & BLAKE CORPORATION 1184 0 318
2002 BELDEN & BLAKE CORPORATION 716 12 140
2003 PETROX, INC 1055 0 365
2004 PETROX, INC 921 0 365
2005 PETROX, INC 1079 0 365
2006 PETROX, INC 1265 0 365
2007 PETROX, INC 1297 0 365
2008 PETROX, INC 1182 0 365
2009 PETROX, INC 666 0 324
2010 PETROX, INC 545 0 365
2011 PETROX, INC 597 0 365
2012 PETROX, INC 769 0 366
2013 PETROX, INC 640 0 365
2014 PETROX, INC 744 0 365
2015 PETROX, INC 190 0 60
2016 ENERVEST OPERATING LLC 837 0 366
2017 ENERVEST OPERATING LLC 696 0 365
2018 ENERVEST OPERATING LLC 876 0 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BELDEN & BLAKE CORPORATION Brine 0 0
1985 BELDEN & BLAKE CORPORATION Brine 2 0
1986 BELDEN & BLAKE CORPORATION Brine 0 365
1987 BELDEN & BLAKE CORPORATION Brine 0 365
1988 BELDEN & BLAKE CORPORATION Brine 0 366
1990 BELDEN & BLAKE CORPORATION Brine 0 356
1991 BELDEN & BLAKE CORPORATION Brine 0 365
1992 BELDEN & BLAKE CORPORATION Brine 0 359
1993 BELDEN & BLAKE CORPORATION Brine 0 365
1994 BELDEN & BLAKE CORPORATION Brine 0 365
1995 BELDEN & BLAKE CORPORATION Brine 0 365
1996 BELDEN & BLAKE CORPORATION Brine 0 366
1997 BELDEN & BLAKE CORPORATION Brine 0 358
1998 BELDEN & BLAKE CORPORATION Brine 0 358
1999 BELDEN & BLAKE CORPORATION Brine 0 365
2000 BELDEN & BLAKE CORPORATION Brine 0 359
2001 BELDEN & BLAKE CORPORATION Brine 0 318
2002 PETROX, INC Brine 0 28
2003 PETROX, INC Brine 0 365
2004 PETROX, INC Brine 0 365
2005 PETROX, INC Brine 0 365
2006 PETROX, INC Brine 0 365
2007 PETROX, INC Brine 365
2008 PETROX, INC Brine 0 365
2009 PETROX, INC Brine 0 324
2010 PETROX, INC Brine 0 365
2011 PETROX, INC Brine 0 365
2012 PETROX, INC Brine 0 366
2013 PETROX, INC Brine 0 365
2014 PETROX, INC Brine 0 365
2015 PETROX, INC Brine 0 60
2016 ENERVEST OPERATING LLC Brine 0 366
2017 ENERVEST OPERATING LLC Brine 0 365
2018 ENERVEST OPERATING LLC Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0256342955 2009-09-24 Production Wells No Violations The excavation around the wellhead is filled in. There is a swab rig on the well. The complaint is RESOLVED.
0692163391 2009-04-28 Production Wells No Violations I received a call on 4-27-2009 from Steve Collins (Massillon Fire Department, 330-833-1053) regarding an odor complaint at a well located at 106 Rolling Park Dr., Massillon, OH. On 4-28-2009, I met with John Casper (Rolling Hills Trailer Park) at the well site. A gas leak was reported on Sunday 4-26-2009 and the Massillon Fire Department responded. Petrox was notified and addressed the leak. During my inspection on 4-28-2009, I called Bill Magrell (330-565-5873) with Petrox to get the details of the incident. Gas had been leaking from under the production string casing hanger out of the surface casing. The surface casing was loaded with water to kill the gas. A hole was drilled in the surface casing to monitor for gas. During my inspection there was no gas present. Petrox will evaluate the leak and then repair the casing or plug the well. I informed the Massillon Fire Department of my findings. I talked to Cindy (Rolling Hills Trailer Park) later that day and informed her of the situation.
0710964767 2009-05-05 Production Wells No Violations The excavation at the wellhead is still open. There was no visible venting or odor coming from the port in the casing. I met with Justin (Cindys son), who is in charge of maintenance.
0738779186 2014-03-27 Production Wells No Violations I was on location to obtain updated GPS coordinates for this well. During my inspection I found a plunger lift well with a 100bbl production tank and separator all enclosed in a fence. The well is located in a manufactured home park. The wellhead is in good conditioned has proper I.D. signage with 55psi of pressure on the tubing. There are no violations at this time.

For data sources see[9]

References