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Difference between revisions of "34-067-21001"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-067-21001
 
| Well ID: 34-067-21001
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.39621512, -81.04622559 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.396149617, -81.04640639 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Harrison County, Ohio|Harrison]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Harrison_County,_Ohio|Harrison]]
 +
|-
 +
| Municipality: [[Rumley_Township,_Harrison_County,_Ohio|Rumley Township]]
 
|-
 
|-
 
| Operator Name: [[UTE OIL COMPANY]]
 
| Operator Name: [[UTE OIL COMPANY]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: RUMBLE
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2016-06-30
 
|-
 
|-
 
| Spud Date: 2007-01-03
 
| Spud Date: 2007-01-03
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 
|-
 
|-
| Configuration: Vertical
+
| Final Drill Date: 2007-02-21
 
|-
 
|-
| Well Status: Plugged and Abandoned
+
| Well Total Depth: 950 ft
 
|-
 
|-
| Violations: 0
+
| Configuration: Vertical
|-
 
| Latitude: 40.39621512
 
 
|-
 
|-
| Longitude: -81.04622559
+
| Latitude: 40.396149617
 
|-
 
|-
 +
| Longitude: -81.04640639
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Well Status
!scope="col" | DATE
+
!scope="col" style="width: 15%;text-align: center"| Well Status Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Comment
!scope="col" | COMMENT
 
!scope="col" | VIOLATION ID
 
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1021969692
+
| APP
| 2007-02-11
+
| 2006-10-19
|  
+
| Proposed Formations:THRU POTTSVILLE COALS, Issued Date:10/19/2006, Expired Date:10/19/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:O
| On site to witness the plug back of the bottom hole . The drilling rig ( Boart-Longyear) batch mixed the cement and pumped it in stages. While coming out of the hole after pumping one of the stages, the drill string / tubing got hung in the hole. Decide to wait until tomorrow to decide on a course of action . No violations at this time.
 
|
 
|
 
|
 
 
|-
 
|-
 +
| Reached Total Depth
 +
| 2007-02-21
 +
| STRAT TEST (NO. 2 COAL).
 
|-
 
|-
| 1218790319
+
| APP
| 2007-02-06
+
| 2011-06-01
|
+
| Proposed Formations:KITTANNING COAL, Issued Date:6/1/2011, Expired Date:5/31/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
| Inspection revealed that Boart-Longyear drilling is drilling the surface hole. No violations at this time.
 
|
 
|
 
|  
 
 
|-
 
|-
 +
| Plugged/Abandoned
 +
| 2011-07-16
 +
| STRAT TEST (NO. 2 COAL).
 
|-
 
|-
| 1222714133
+
| Construction Permit Expires
| 2008-09-25
+
| 2013-05-31
|  
+
| STRAT TEST (NO. 2 COAL).
| Inspection revealed that the preliminary restoration can be approved at this time. No violations at this time.
 
|
 
|
 
|
 
 
|-
 
|-
 +
| Record Last Modified
 +
| 2019-06-05
 +
| STRAT TEST (NO. 2 COAL).
 
|-
 
|-
| -1431239804
+
|}
| 2013-07-23
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Well and WellHistry Tables
| Everthing passed according to 1509.072B.
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07  
|  
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|  
+
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 
|-
 
|-
 +
| 2012-04-20
 +
| style="text-align: right;" | 508
 +
| style="text-align: right;" | 511
 +
| style="text-align: right;" | 13
 
|-
 
|-
| 1495618557
+
|}
| 2007-01-29
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Perfs Table
| Inspection revealed that Boart-Longyear Drilling is moving onto location . The rig is moving from the Hinton NOI well in Carroll County. No violations at this time.
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
|  
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|  
+
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 
|-
 
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 
|-
 
|-
| -1931150280
+
|}-->
| 2007-01-31
+
<!--== Stimulations Data ==
|  
+
{| class="wikitable sortable" width="95%"
| Inspection revealed that Boart-Longyear is app. 25' deep . The drilling rig is having trouble with stuff freezing due to the extreme cold temperature. No violations at this time.
+
!scope="col" style="text-align: center"| Stimulation Date
|  
+
!scope="col" style="text-align: center"| Chemical Agent
|  
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
|  
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
 +
|}-->
 +
<!--== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
| 1960486361
+
|}-->
| 2007-02-01
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| Inspection revealed that the drilling rig is still at 25' and still having trouble with stuff freezing . Also discussed the casing programs with Ray Mazza .
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 2096868725
+
| 0054858106
| 2007-02-06
+
| 2007-01-30
|  
+
| Drill / Deepen /  Reopen
| Inspection revealed that Boart-Longyear Drilling is drilling the surface hole ( coring the hole). No violations at this time.
+
| No Violations
|
+
| Inspection revealed that Boart-Longyear Drilling is finishing rigging up and getting ready to drill. No violations at this time. Inspection of the drilling revealed that the pit has been lined and the liners is intact at this time.
|
 
|
 
|-
 
 
|-
 
|-
| -243708457
+
| 0243708457
 
| 2007-02-21
 
| 2007-02-21
|  
+
| Drill / Deepen /  Reopen
| On site to witness the running of the 2 7/8 casing . Boart-Longyear Drilling ran 637' of 2 7/8 casing . Omega is going to cement the casing to surface. I left location to witness the surface job on permit number 2001 Carroll County. I decided to witness the cementing on permit number 2001 Carroll County because the well is located in an area where the Berea Formation blows out. No violations at this time.
+
| No Violations
|
+
| On site to witness the running of the 2 7/8 casing . Boart-Longyear Drilling ran 637 of 2 7/8 casing . Omega is going to cement the casing to surface. I left location to witness the surface job on permit number 2001 Carroll County. I decided to witness the cementing on permit number 2001 Carroll County because the well is located in an area where the Berea Formation blows out. No violations at this time.
|
 
|
 
|-
 
 
|-
 
|-
| -251537204
+
| 0251537204
 
| 2007-02-22
 
| 2007-02-22
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspection revealed that the cement has stayed at ground level on the backside of the 2 7/8 casing. No violations at this time.
 
| Inspection revealed that the cement has stayed at ground level on the backside of the 2 7/8 casing. No violations at this time.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0377442486
| 377442486
 
 
| 2007-04-11
 
| 2007-04-11
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspection of the drilling pit revealed that the pit liner is intact and the fluid level is acceptable. No violations at this time.
 
| Inspection of the drilling pit revealed that the pit liner is intact and the fluid level is acceptable. No violations at this time.
|
 
|
 
|
 
|-
 
|-
 
| 54858106
 
| 2007-01-30
 
|
 
| Inspection revealed that Boart-Longyear Drilling is finishing rigging up and getting ready to drill. No violations at this time. Inspection of the drilling revealed that the pit has been lined and the liners is intact at this time.
 
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0714646336
| -714646336
 
 
| 2007-02-20
 
| 2007-02-20
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspection revealed that the drilling rig is using washover pipe and a soring type bit and they are trying to drill the cement on the backside of the drill string/ tubing . No violations at this time.
 
| Inspection revealed that the drilling rig is using washover pipe and a soring type bit and they are trying to drill the cement on the backside of the drill string/ tubing . No violations at this time.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0747151190
| -747151190
 
 
| 2007-02-12
 
| 2007-02-12
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspection revealed that the pipe is still hung in the hole . Nobody on site at this time. No violations at this time.
 
| Inspection revealed that the pipe is still hung in the hole . Nobody on site at this time. No violations at this time.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 0883671234
| 883671234
 
 
| 2007-02-14
 
| 2007-02-14
|  
+
| Drill / Deepen /  Reopen
 +
| No Violations
 
| Inspection revealed that nobody is on site today and the rig is shut down. No violations at this time.
 
| Inspection revealed that nobody is on site today and the rig is shut down. No violations at this time.
|
 
|
 
|
 
 
|-
 
|-
 +
| 0887467367
 +
| 2007-02-09
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Inspection revealed that Boart-Longyear Drilling is coring the hole at 830. No violations at this time.
 +
|-
 +
| 1021969692
 +
| 2007-02-11
 +
| Plug / Plug Back
 +
| No Violations
 +
| On site to witness the plug back of the bottom hole . The drilling rig ( Boart-Longyear) batch mixed the cement and pumped it in stages. While coming out of the hole after pumping one of the stages, the drill string / tubing got hung in the hole. Decide to wait until tomorrow to decide on a course of action . No violations at this time.
 +
|-
 +
| 1218790319
 +
| 2007-02-06
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
|  Inspection revealed that Boart-Longyear drilling is drilling the surface hole. No violations at this time.
 +
|-
 +
| 1222714133
 +
| 2008-09-25
 +
| Preliminary Restoration
 +
| No Violations
 +
| Inspection revealed that the preliminary restoration can be approved at this time. No violations at this time.
 +
|-
 +
| 1431239804
 +
| 2013-07-23
 +
| Preliminary Restoration
 +
| No Violations
 +
| Everthing passed according to 1509.072B.
 +
|-
 +
| 1467738398
 +
| 2016-06-30
 +
| Final Restoration
 +
| No Violations
 +
| On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B).
 +
|-
 +
| 1495618557
 +
| 2007-01-29
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Inspection revealed that Boart-Longyear Drilling is moving onto location . The rig is moving from the Hinton NOI well in Carroll County. No violations at this time.
 +
|-
 +
| 1931150280
 +
| 2007-01-31
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Inspection revealed that Boart-Longyear is app. 25 deep . The drilling rig is having trouble with stuff freezing due to the extreme cold temperature. No violations at this time.
 
|-
 
|-
| 887467367
+
| 1960486361
| 2007-02-09
+
| 2007-02-01
|  
+
| Drill / Deepen /  Reopen
| Inspection revealed that Boart-Longyear Drilling is coring the hole at 830'. No violations at this time.
+
| No Violations
|
+
|  Inspection revealed that the drilling rig is still at 25 and still having trouble with stuff freezing . Also discussed the casing programs with Ray Mazza .
|
+
|-
|
+
| 2096868725
 +
| 2007-02-06
 +
| Drill / Deepen /  Reopen
 +
| No Violations
 +
| Inspection revealed that Boart-Longyear Drilling is drilling the surface hole ( coring the hole). No violations at this time.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 23:53, 23 July 2019

Well Details

Well ID: 34-067-21001
Loading map...
Country: United States
State: Ohio
County: Harrison
Municipality: Rumley Township
Operator Name: UTE OIL COMPANY
Well Pad ID:
Farm/Lease Name: RUMBLE
License Status: Final Restoration
License Date: 2016-06-30
Spud Date: 2007-01-03
Spud Drilling Contractor:
Final Drill Date: 2007-02-21
Well Total Depth: 950 ft
Configuration: Vertical
Latitude: 40.396149617
Longitude: -81.04640639

For data sources see[1]

Well History

Well Status Well Status Date Comment
APP 2006-10-19 Proposed Formations:THRU POTTSVILLE COALS, Issued Date:10/19/2006, Expired Date:10/19/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:ST, Proposed Well Class:O
Reached Total Depth 2007-02-21 STRAT TEST (NO. 2 COAL).
APP 2011-06-01 Proposed Formations:KITTANNING COAL, Issued Date:6/1/2011, Expired Date:5/31/2013 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2011-07-16 STRAT TEST (NO. 2 COAL).
Construction Permit Expires 2013-05-31 STRAT TEST (NO. 2 COAL).
Record Last Modified 2019-06-05 STRAT TEST (NO. 2 COAL).

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2012-04-20 508 511 13

For data sources see[3]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0054858106 2007-01-30 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear Drilling is finishing rigging up and getting ready to drill. No violations at this time. Inspection of the drilling revealed that the pit has been lined and the liners is intact at this time.
0243708457 2007-02-21 Drill / Deepen / Reopen No Violations On site to witness the running of the 2 7/8 casing . Boart-Longyear Drilling ran 637 of 2 7/8 casing . Omega is going to cement the casing to surface. I left location to witness the surface job on permit number 2001 Carroll County. I decided to witness the cementing on permit number 2001 Carroll County because the well is located in an area where the Berea Formation blows out. No violations at this time.
0251537204 2007-02-22 Drill / Deepen / Reopen No Violations Inspection revealed that the cement has stayed at ground level on the backside of the 2 7/8 casing. No violations at this time.
0377442486 2007-04-11 Drill / Deepen / Reopen No Violations Inspection of the drilling pit revealed that the pit liner is intact and the fluid level is acceptable. No violations at this time.
0714646336 2007-02-20 Drill / Deepen / Reopen No Violations Inspection revealed that the drilling rig is using washover pipe and a soring type bit and they are trying to drill the cement on the backside of the drill string/ tubing . No violations at this time.
0747151190 2007-02-12 Drill / Deepen / Reopen No Violations Inspection revealed that the pipe is still hung in the hole . Nobody on site at this time. No violations at this time.
0883671234 2007-02-14 Drill / Deepen / Reopen No Violations Inspection revealed that nobody is on site today and the rig is shut down. No violations at this time.
0887467367 2007-02-09 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear Drilling is coring the hole at 830. No violations at this time.
1021969692 2007-02-11 Plug / Plug Back No Violations On site to witness the plug back of the bottom hole . The drilling rig ( Boart-Longyear) batch mixed the cement and pumped it in stages. While coming out of the hole after pumping one of the stages, the drill string / tubing got hung in the hole. Decide to wait until tomorrow to decide on a course of action . No violations at this time.
1218790319 2007-02-06 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear drilling is drilling the surface hole. No violations at this time.
1222714133 2008-09-25 Preliminary Restoration No Violations Inspection revealed that the preliminary restoration can be approved at this time. No violations at this time.
1431239804 2013-07-23 Preliminary Restoration No Violations Everthing passed according to 1509.072B.
1467738398 2016-06-30 Final Restoration No Violations On the day of my inspection, I found that the final restoration has been complete. The site passed final restoration according to ORC 1509.072(B).
1495618557 2007-01-29 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear Drilling is moving onto location . The rig is moving from the Hinton NOI well in Carroll County. No violations at this time.
1931150280 2007-01-31 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear is app. 25 deep . The drilling rig is having trouble with stuff freezing due to the extreme cold temperature. No violations at this time.
1960486361 2007-02-01 Drill / Deepen / Reopen No Violations Inspection revealed that the drilling rig is still at 25 and still having trouble with stuff freezing . Also discussed the casing programs with Ray Mazza .
2096868725 2007-02-06 Drill / Deepen / Reopen No Violations Inspection revealed that Boart-Longyear Drilling is drilling the surface hole ( coring the hole). No violations at this time.

For data sources see[4]

References