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Difference between revisions of "34-005-22555"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-005-22555
 
| Well ID: 34-005-22555
| style="height=100%; align=center" rowspan="15" | {{#display_map: 40.80808227, -82.35322295 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 40.808025427, -82.35333754 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Ashland County, Ohio|Ashland]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[COLUMBIA GAS TRANSMISSION]]
+
| County: [[Ashland_County,_Ohio|Ashland]]
 +
|-
 +
| Municipality: [[Mifflin_Township,_Ashland_County,_Ohio|Mifflin Township]]
 +
|-
 +
| Operator Name: [[COLUMBIA GAS TRANSMISSION LLC]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: STAUFFER DONALD
 
|-
 
|-
| First Permit Date:  
+
| License Status: Storage Well
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2002-06-06
 
|-
 
|-
 
| Spud Date: 1966-12-05
 
| Spud Date: 1966-12-05
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1967-02-14
 +
|-
 +
| Well Total Depth: 2712 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Storage Well
+
| Latitude: 40.808025427
 +
|-
 +
| Longitude: -82.35333754
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 +
|-
 +
| Original Spud
 +
| 1966-12-05
 +
| STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
 
|-
 
|-
| Violations: 0
+
| Completed
 +
| 1967-02-14
 +
| STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
 
|-
 
|-
| Latitude: 40.80808227
+
| Reached Total Depth
 +
| 1967-02-14
 +
| STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
 
|-
 
|-
| Longitude: -82.35322295
+
| Record Last Modified
 +
| 2017-02-15
 +
| STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 2001-0
 
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 
|  
 
|  
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|  
 
|  
| style="text-align:right;" | 0.0
 
 
|  
 
|  
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 2001
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2002
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2003
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 2004
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2002-0
+
| 2005
| style="text-align:right;" | 0.0
+
| [[COLUMBIA GAS TRANSMISSION LLC]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2003-0
+
|}
| style="text-align:right;" | 0.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 2001
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2004-0
+
| 2002
| style="text-align:right;" | 0.0
+
| [[COLUMBIA GAS TRANSMISSION LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2005-0
+
| 2004
| style="text-align:right;" | 0.0
+
| [[COLUMBIA GAS TRANSMISSION LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[COLUMBIA GAS TRANSMISSION LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2006-0
+
| 2006
| style="text-align:right;" | 0.0
+
| [[COLUMBIA GAS TRANSMISSION LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
+
|-
!scope="col" | VIOLATION COMMENT
+
| 0012600972
 +
| 2016-08-18
 +
| Work Over Reconditioning
 +
| No Violations
 +
| Hagan Well Service is rigged up on the well.  The well is shut in on the 8.625 inch casing with a swage.  The operator advises that they have a problem with the 3.5 inch production casing but the casing is cemented to surface.  The well currently has a bridge plug in it and is killed.
 +
|-
 +
| 0522368896
 +
| 2018-03-28
 +
| Storage Well
 +
| No Violations
 +
| ID is posted and the location is maintained.  The annulus is open.  The well is equipped with a separator.
 +
|-
 +
| 1135282892
 +
| 2019-03-07
 +
| Storage Well
 +
| No Violations
 +
| Performed annual inspection for Columbia Gas Storage Well #10742 on 03/07/2019.  The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve, and a drip.  The well is equipped with satellite monitoring.  Well identification is clearly displayed.  No problems were noted at the time of the inspection.
 +
|-
 +
| 1196209947
 +
| 2016-09-26
 +
| Work Over Reconditioning
 +
| No Violations
 +
| Hagan Well Service has a service rig on the well.  The 3.5 inch casing has been milled out above the cut.  The well is going to be produced using the 5.5 inch casing which is also cemented to surface.  The 5.5 inch casing was pressure tested successfully.  Gas remains on the backside of the drive pipe.  There is no gas on the drive-surface annulus.  The well is currently killed with a bridge plug in the production casing.
 +
|-
 +
| 1311812140
 +
| 2017-04-24
 +
| Storage Well
 +
| No Violations
 +
| ID is posted and the location is maintained.  The annulus is open.  The well is equipped with a separator.
 +
|-
 +
| 1393042405
 +
| 2016-05-26
 +
| Storage Well
 +
| No Violations
 +
| ID is posted and the location is maintained.  The well is shut in and locked out.  There is a 25 barrel tank at the well.  The connection to the separator has been removed from the tank.  The tank is wrapped in a tarp.
 
|-
 
|-
| -1506330784
+
| 1506330784
 
| 2014-09-08
 
| 2014-09-08
|  
+
| Storage Well
 +
| No Violations
 
| ID posted, location maintained.  25 Bbl tank at the well site.  The side gate valve is closed.
 
| ID posted, location maintained.  25 Bbl tank at the well site.  The side gate valve is closed.
|
 
|
 
|
 
|-
 
 
|-
 
|-
| -1579329860
+
| 1579329860
 
| 2013-10-22
 
| 2013-10-22
|  
+
| Storage Well
 +
| No Violations
 
| ID posted, site maintained.  Gas on surface annulus registered LEL and CO sensors on the detector.  The well is equipped with a 50 Bbl tank.  Flow was audible from the separator to the tank and the tank was at 1/2 capacity.  There is also a leak from a gauge tap on the well head.  Columbia is being contacted.
 
| ID posted, site maintained.  Gas on surface annulus registered LEL and CO sensors on the detector.  The well is equipped with a 50 Bbl tank.  Flow was audible from the separator to the tank and the tank was at 1/2 capacity.  There is also a leak from a gauge tap on the well head.  Columbia is being contacted.
|  
+
|-
|  
+
| 1721764434
|  
+
| 2015-07-22
 +
| Storage Well
 +
| No Violations
 +
| ID is posted at the well.  The valves on the wellhead are open.  The backside valve is open.  There is a 25 barrel tank at the well.  The tank is not plumbed into the well.
 
|-
 
|-
 
|}
 
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 +
|-
 +
|}-->
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 04:57, 24 July 2019

Well Details

Well ID: 34-005-22555
Loading map...
Country: United States
State: Ohio
County: Ashland
Municipality: Mifflin Township
Operator Name: COLUMBIA GAS TRANSMISSION LLC
Well Pad ID:
Farm/Lease Name: STAUFFER DONALD
License Status: Storage Well
License Date: 2002-06-06
Spud Date: 1966-12-05
Spud Drilling Contractor:
Final Drill Date: 1967-02-14
Well Total Depth: 2712 ft
Configuration: Vertical
Latitude: 40.808025427
Longitude: -82.35333754

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1966-12-05 STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
Completed 1967-02-14 STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
Reached Total Depth 1967-02-14 STORAGE-47, RE-OPEN 12-22-66, GL=1265.07
Record Last Modified 2017-02-15 STORAGE-47, RE-OPEN 12-22-66, GL=1265.07

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
2001 COLUMBIA GAS TRANSMISSION LLC 0 0 0
2002 COLUMBIA GAS TRANSMISSION LLC 0 0 0
2003 COLUMBIA GAS TRANSMISSION LLC 0 0 0
2004 COLUMBIA GAS TRANSMISSION LLC 0 0 0
2005 COLUMBIA GAS TRANSMISSION LLC 0 0 0
2006 COLUMBIA GAS TRANSMISSION LLC 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
2001 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
2002 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
2003 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
2004 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
2005 COLUMBIA GAS TRANSMISSION LLC Brine 0 0
2006 COLUMBIA GAS TRANSMISSION LLC Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0012600972 2016-08-18 Work Over Reconditioning No Violations Hagan Well Service is rigged up on the well. The well is shut in on the 8.625 inch casing with a swage. The operator advises that they have a problem with the 3.5 inch production casing but the casing is cemented to surface. The well currently has a bridge plug in it and is killed.
0522368896 2018-03-28 Storage Well No Violations ID is posted and the location is maintained. The annulus is open. The well is equipped with a separator.
1135282892 2019-03-07 Storage Well No Violations Performed annual inspection for Columbia Gas Storage Well #10742 on 03/07/2019. The well is equipped with a flanged wellhead with 1-master valve and 1-wing valve, and a drip. The well is equipped with satellite monitoring. Well identification is clearly displayed. No problems were noted at the time of the inspection.
1196209947 2016-09-26 Work Over Reconditioning No Violations Hagan Well Service has a service rig on the well. The 3.5 inch casing has been milled out above the cut. The well is going to be produced using the 5.5 inch casing which is also cemented to surface. The 5.5 inch casing was pressure tested successfully. Gas remains on the backside of the drive pipe. There is no gas on the drive-surface annulus. The well is currently killed with a bridge plug in the production casing.
1311812140 2017-04-24 Storage Well No Violations ID is posted and the location is maintained. The annulus is open. The well is equipped with a separator.
1393042405 2016-05-26 Storage Well No Violations ID is posted and the location is maintained. The well is shut in and locked out. There is a 25 barrel tank at the well. The connection to the separator has been removed from the tank. The tank is wrapped in a tarp.
1506330784 2014-09-08 Storage Well No Violations ID posted, location maintained. 25 Bbl tank at the well site. The side gate valve is closed.
1579329860 2013-10-22 Storage Well No Violations ID posted, site maintained. Gas on surface annulus registered LEL and CO sensors on the detector. The well is equipped with a 50 Bbl tank. Flow was audible from the separator to the tank and the tank was at 1/2 capacity. There is also a leak from a gauge tap on the well head. Columbia is being contacted.
1721764434 2015-07-22 Storage Well No Violations ID is posted at the well. The valves on the wellhead are open. The backside valve is open. There is a 25 barrel tank at the well. The tank is not plumbed into the well.

For data sources see[8]

References