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| County: [[Monroe_County,_Ohio|Monroe]] | | County: [[Monroe_County,_Ohio|Monroe]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Wayne_Township,_Monroe_County,_Ohio|Wayne Township]] |
|- | |- | ||
| Operator Name: [[CISLER OIL AND GAS]] | | Operator Name: [[CISLER OIL AND GAS]] | ||
Line 37: | Line 37: | ||
| Longitude: -81.17951404 | | Longitude: -81.17951404 | ||
|} | |} | ||
− | For data sources see<ref | + | For data sources see<ref>{{cite web |
− | | title = | + | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables |
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2008-01-22 | ||
+ | | Operator changed from 5702, KRISHER EARLEY DRLG PTNSP to 5719, CISLER OIL AND GAS | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2018-02-12 | ||
+ | | NO RECORD. UPDATE LOCATION PER BILL STOLARIK-ALE 06/28/2016. UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
| date = 2019-05-07 | | date = 2019-05-07 | ||
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| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
<!--== Perforation Treatments == | <!--== Perforation Treatments == | ||
− | {| class="wikitable sortable" | + | {| class="wikitable sortable" width="95%" |
!scope="col" style="text-align: center"| Perforation Date | !scope="col" style="text-align: center"| Perforation Date | ||
!scope="col" style="text-align: center"| Interval Top (ft) | !scope="col" style="text-align: center"| Interval Top (ft) | ||
Line 51: | Line 72: | ||
|- | |- | ||
|}--> | |}--> | ||
− | + | <!--== Fracking Activities == | |
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
== Production Data == | == Production Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
Line 79: | Line 134: | ||
|- | |- | ||
|} | |} | ||
− | For data sources see<ref | + | For data sources see<ref>{{cite web |
− | | title = | + | | title = Risk Based Data Management System - Production Table - Oil and Gas Data |
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
|publisher = [[Ohio Department of Natural Resources]] | |publisher = [[Ohio Department of Natural Resources]] | ||
| date = 2019-05-07 | | date = 2019-05-07 | ||
− | | url = http://wellwiki.org/wiki/ | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
| accessdate = 2019-05-21 }}</ref> | | accessdate = 2019-05-21 }}</ref> | ||
== Waste Data == | == Waste Data == | ||
Line 112: | Line 173: | ||
|- | |- | ||
|} | |} | ||
− | For data sources see<ref | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
==== Inspections Performed ==== | ==== Inspections Performed ==== | ||
Line 193: | Line 265: | ||
|- | |- | ||
|} | |} | ||
− | For data sources see<ref | + | For data sources see<ref>{{cite web |
− | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables | |
− | + | |publisher = [[Ohio Department of Natural Resources]] | |
− | { | + | | date = 2019-05-07 |
− | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | |
− | + | | accessdate = 2019-05-21 }}</ref> | |
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==References== | ==References== | ||
<references/> | <references/> | ||
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
[[Category:Ohio Wells]] | [[Category:Ohio Wells]] |
Well ID: 34-111-65469 | Loading map...
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Country: United States | |
State: Ohio | |
County: Monroe | |
Municipality: Wayne Township | |
Operator Name: CISLER OIL AND GAS | |
Well Pad ID: | |
Farm/Lease Name: SLOAN SARAH E | |
License Status: Producing | |
License Date: 2006-09-12 | |
Spud Date: | |
Spud Drilling Contractor: | |
Final Drill Date: | |
Well Total Depth: | |
Configuration: Vertical | |
Latitude: 39.730313622 | |
Longitude: -81.17951404 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Change of Owner | 2008-01-22 | Operator changed from 5702, KRISHER EARLEY DRLG PTNSP to 5719, CISLER OIL AND GAS |
Record Last Modified | 2018-02-12 | NO RECORD. UPDATE LOCATION PER BILL STOLARIK-ALE 06/28/2016. UPDATE LOCATION PER DOGRM SURVEYOR, ALE 2/12/18. |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | CISLER OIL AND GAS | 0 | 0 | 0 |
2016 | CISLER OIL AND GAS | 0 | 0 | 0 |
2017 | CISLER OIL AND GAS | 0 | 0 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2014 | CISLER OIL AND GAS | Brine | 0 | 0 |
2016 | CISLER OIL AND GAS | Brine | 0 | 0 |
2017 | CISLER OIL AND GAS | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
1108846301 | 2005-02-17 | Production Wells | No Violations | No violations noted,well appears capable of producing.Well is equipped with pumpjack rods and tubing in place,electric motor on pumpjack.No production has ever been reported on said well. |
1265672195 | 2017-12-15 | Production Wells | No Violations | On this day, I accompanied ODNR Inspector William Stolarik. Please refer to his comments for a detailed report. I am conducting a follow-up inspection on Chiefs Order 2017-101. I found the well equipped with casing, tubing, and a cut flowline attached to the tubing. The well has a pumping unit with an electric motor and proper identification. Pictures were taken during inspection. |
1426378194 | 2015-03-14 | Production Wells | No Violations | Inspection on this day revealed that fresh water had filled up area between wooden conductor pipe and 7 surface casing and let oil escape onto the ground and it entered a small wet weather stream that feeds Rich Fork Creek and estimated release was 1-2 bbl of oil and the Monroe county EMA contacted local inspector Bill Stolarik and I received call from him at 12:00 pm asking if I would look into the matter and I arrived on site at 1:15 pm and located problem well and then contacted well owner requesting his presence at site to begin clean up efforts on spill, instructed owner to remove any contaminated soils and properly dispose of it at a EPA approved landfill.
Note: Equipment for clean up arrived on site and soils were placed onto plastic liner and covered for the night and then they started to work there way down stream to clean up small pockets of oil in creek. |
1426512539 | 2015-03-15 | Production Wells | No Violations | Inspection on this day indicated that contaminated soils were still on plastic containment and crew was trying to haul material up the hill and place into roll off container and I walked entire creek bed to check area for any free standing oil and on this day very little was found and I told cleanup crew to change out absorbent pads twice daily until given father notice. |
1693303309 | 2017-12-15 | Production Wells | No Violations | Order 2017-101 follow up inspection found the well equipped with casing tubing and pumping rods, the well is set up to be produced by the means of a pumping unit. There is a casing and tubing well head present with production valves in the closed position and no flow lines attached. There is no production tank present associated with the well and no commercial gas meter present on the lease. |
1746527227 | 2015-03-15 | Production Wells | No Violations | Administrative report to document the situation with a oil spill at the well head that entered the waters of the State. At 11:32 Am on 03/14/15 I was notified by Phil Keevert with the Monroe Co EMA that they had an oil spill of approximate 50 gallons that had entered the waters of the state and the EPA was also notified and enroot, I notified my Supervisor Brent Bear and contacted Inspector Dave Ball to respond. I also made contact with the Steve Sapio with the USDA who is the area inspector for the US Forest Service and reported the spill to Mr. Sapio on this day. I remained in contact with Inspector Ball and Supervisor Bear through the course of events of the day documenting the situation. 03/16/2015 The initial well identification reported by the County EMA Director was found to be incorrect- I have correctly identified the well as 3411165719. |
1837868187 | 2015-03-15 | Production Wells | Violations Noted | Status check inspection of the well head found the following equipment present at the well head 6.625 casing 2 tubing and pumping rods with no production lines attached to the well head. A small fuel type tank is located near the well head as a production tank but not in use. ODNR-RBDMS records show no reported production in the database. Instructions are as follows-Plug the said well within 180 days -ODNR Monroe County Inspector Bill Stolarik- 740-507-6592. |
1981067505 | 2017-11-13 | Production Wells | No Violations | Upon inspection of the well I used my State issued Garmin GPS device and took a GPS reading of the well of EPE 11-39.73039 X 81.17933 and confirmed the well identification as the Sloan # 3 owned by Cisler Oil & Gas ODNR owner # 5719. Also noted is Historically the well has a unresolved violation issued against it on 03/15/2015 with the violation identified as 1837868187. The well was observed to be equipped with at surface 6.625 diameter casing with a casing valve present and no flow line attached. The well has 2 diameter tubing inserted inside the production casing with a tubing production head present and no valve or production flow line attached to the tubing head, only a broken off piece of clear plastic sight tube. There is pumping rods inserted into the 2 diameter tubing and the well is set up to be produced by the means of a pumping unit with a electric motor present on the unit. Also noted is the absence of a production fluid tank or gas sales meter on the lease that can be identified as associated with the said well. Photographs were taken on this day and recent attempts to contact the registered producer identified as Scott Cisler has not been returned. |
2097318503 | 2012-07-16 | Production Wells | No Violations | Inspection of the well head found the following equipment, 6.188 surface casing, 2 tubing & rods, with the well equipped with a pumping unit and gasoline motor, no production lines hooked up and a 800 gallon vertical tank sitting next to the well head. Well identification present. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1837868187 | US-OH-118350 | 2015-03-31 | Well shall be plugged |
For data sources see[7]