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Difference between revisions of "34-073-22042"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-073-22042
 
| Well ID: 34-073-22042
| style="height=100%; align=center" rowspan="15" | {{#display_map: 39.49673391, -82.21620526 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 39.496664367, -82.21633441 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Hocking County, Ohio|Hocking]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 
|-
 
|-
| Operator Name: [[FOLEY CHARLES E]]
+
| County: [[Hocking_County,_Ohio|Hocking]]
 +
|-
 +
| Municipality: [[Ward_Township,_Hocking_County,_Ohio|Ward Township]]
 +
|-
 +
| Operator Name: [[FOLEY CANDACE]]
 
|-
 
|-
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: HUTCHISON HELEN
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2016-02-25
 
|-
 
|-
 
| Spud Date: 1978-04-24
 
| Spud Date: 1978-04-24
 
|-
 
|-
| Unconventional:  
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1978-07-13
 +
|-
 +
| Well Total Depth: 3282 ft
 +
|-
 +
| Configuration: Vertical
 
|-
 
|-
| Configuration:  
+
| Latitude: 39.496664367
 
|-
 
|-
| Well Status: Domestic Well
+
| Longitude: -82.21633441
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| CO
 +
| 1977-12-21
 +
| 420  BELL DRILLING & PROD CO  GeoDate  12/21/77
 
|-
 
|-
| Latitude: 39.49673391
+
| Original Spud
 +
| 1978-04-24
 +
| CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
 
|-
 
|-
| Longitude: -82.21620526
+
| Completed
 +
| 1978-07-13
 +
| CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
 +
|-
 +
| Reached Total Depth
 +
| 1978-07-13
 +
| CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
 +
|-
 +
| CO
 +
| 1992-09-16
 +
| 456  SCHMELZER MARK  GeoDate  12/21/77
 +
|-
 +
| Change of Owner
 +
| 2008-01-15
 +
| Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC
 +
|-
 +
| Change of Owner
 +
| 2008-01-24
 +
| Operator changed from 8268, JEANIE ENTERPISES LLC to 8339, FOLEY CHARLES E
 +
|-
 +
| Change of Owner
 +
| 2016-02-25
 +
| Operator changed from 8339, FOLEY CHARLES E to 9636, FOLEY CANDACE
 +
|-
 +
| Record Last Modified
 +
| 2016-02-25
 +
| CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1984-0
 
| style="text-align:right;" | 4191.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 1800 Bbl
 +
| style="text-align: right;" | 10000
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 77.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1984
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 4191
 +
| style="text-align: right;" | 77
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1985
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 3415
 +
| style="text-align: right;" | 125
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1987
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 2920
 +
| style="text-align: right;" | 73
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1988
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 2812
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1989
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 2412
 +
| style="text-align: right;" | 70
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1990
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 2308
 +
| style="text-align: right;" | 54
 +
| style="text-align: right;" | 267
 +
|-
 +
| 1991
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 2539
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1992
 +
| [[BELL DRILLING & PROD CO]]
 +
| style="text-align: right;" | 1434
 +
| style="text-align: right;" | 55
 +
| style="text-align: right;" | 243
 +
|-
 +
| 1995
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 1447
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1996
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 673
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1997
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 1892
 +
| style="text-align: right;" | 43
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1998
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 1960
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1999
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 1005
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 604
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1985-0
+
| 2002
| style="text-align:right;" | 3415.0
+
| [[SCHMELZER MARK]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 125.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1987-0
+
| 2004
| style="text-align:right;" | 2920.0
+
| [[SCHMELZER MARK]]
|  
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 73.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[SCHMELZER MARK]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1988-0
+
|}
| style="text-align:right;" | 2812.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 70.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1984
 +
| [[BELL DRILLING & PROD CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 1989-0
+
| 1985
| style="text-align:right;" | 2412.0
+
| [[BELL DRILLING & PROD CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 88
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 70.0
 
|
 
 
|-
 
|-
 +
| 1987
 +
| [[BELL DRILLING & PROD CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1990-0
+
| 1988
| style="text-align:right;" | 2308.0
+
| [[BELL DRILLING & PROD CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 54.0
 
|
 
 
|-
 
|-
 +
| 1989
 +
| [[BELL DRILLING & PROD CO]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1991-0
+
| 1990
| style="text-align:right;" | 2539.0
+
| [[BELL DRILLING & PROD CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 35
|
+
| style="text-align: right;" | 267
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1991
 +
| [[BELL DRILLING & PROD CO]]
 +
| Brine
 +
| style="text-align: right;" | 30
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1992-0
+
| 1992
| style="text-align:right;" | 1434.0
+
| [[BELL DRILLING & PROD CO]]
|
+
| Brine
|
+
| style="text-align: right;" | 20
|
+
| style="text-align: right;" | 243
| style="text-align:right;" | 55.0
 
|
 
 
|-
 
|-
 +
| 1995
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 50
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1995-0
+
| 1996
| style="text-align:right;" | 1447.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 50
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1997
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 1998
| style="text-align:right;" | 673.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1999
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1997-0
+
| 2000
| style="text-align:right;" | 1892.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 43.0
 
|
 
 
|-
 
|-
 +
| 2001
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 2002
| style="text-align:right;" | 1960.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2003
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2004
| style="text-align:right;" | 1005.0
+
| [[SCHMELZER MARK]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2005
 +
| [[SCHMELZER MARK]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
|}
| style="text-align:right;" | 604.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Brine Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
 +
| 0267197186
 +
| 2018-07-11
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed the pollution and contamination has not been removed. A portion of the contaminated soil has been removed, but approximately 75 percent remain. New pictures were taken.
 
|-
 
|-
| 2001-0
+
| 0595536981
| style="text-align:right;" | 0.0
+
| 2019-04-18
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| I conducted a compliance notice follow-up on this well today. My inspection revealed that the oil has not been cleaned up. It appeared that there was more oil on the ground than my previous inspection. I took five photos during the inspection. I left a voicemail message with the owners phone number that is listed in RBDMS. I also left a business card at the landowners house. Time of inspection: 1:15 PM. Weather: 78 degrees F, Sunny
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 0670267417
 +
| 2017-11-09
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed the well consists of a pumping unit, 1-100 barrel tank, and separator. There is a 1 inch diameter plastic line hooked to the casing. The 1 inch diameter line has leaked oil. the oil spill is approximately 8 feet by 14 feet., I will follow-up on 11.13.17.
 
|-
 
|-
| 2002-0
+
| 0977720875
| style="text-align:right;" | 0.0
+
| 2017-12-20
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| My inspection revealed the well is not in compliance. The oil that was released is being cleaned up. Not all of the oil has been removed. I have contacted the owner of the well to find out when the clean up will be done.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1034352545
 +
| 2018-02-27
 +
| Production Wells
 +
| No Violations
 +
| My inspection revealed the pollution and contamination is not fully cleaned up. I spoke with John Payne who does not own the well but is cleaning up the pollution and contamination. Mr. Payne stated he is buying a tractor to aid in removing the contaminated soil. The size of the contamination is approximately 8 feet by 14 feet. The well was written up on 11.13.2017. The well is not in compliance.
 
|-
 
|-
| 2003-0
+
| 1241384692
| style="text-align:right;" | 0.0
+
| 2017-12-05
|  
+
| Production Wells
|  
+
| No Violations
|  
+
| My inspection today was to determine if the well had been brought into compliance. The landowner has made progress. The 1 inch diameter plastic line that is connected to the casing has been plumbed into a 55 gallon plastic barrel. There were bags of oil soaked sawdust at the site. Additional saw dust has been placed on the oil to absorb the oil. The well is not in compliance, but progress is being made.
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1370185711
 +
| 2017-11-13
 +
| Production Wells
 +
| Violations Noted
 +
| I met well owner John Payne. I gave John phone number for Central office to obtain well ownership. The oil spill next to the well will be cleaned up by Johns neighbor George Godenschwager. I suggested they take the oil saturated soil to a approved landfill that will accept the waste. I asked to be informed when the clean up took place so I can witness the clean up.
 
|-
 
|-
| 2004-0
+
| 1755486328
| style="text-align:right;" | 0.0
+
| 2018-09-20
|
+
| Production Wells
|  
+
| No Violations
|  
+
| I conducted a compliance notice follow-up inspection in regards to Inspector Kip Thompsons compliance notice issued on 11/13/2017 for pollution and contamination. My inspection revealed that oil has not been completely cleaned up. I observed several pockets of oil below the well location. Time of inspection: 10:35 AM. Weather: 78 degrees F, Sunny
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| 2005-0
+
| 1370185711
| style="text-align:right;" | 0.0
+
| US-OH-110927
|  
+
| 2017-11-21
|  
+
| 9-1-07
|
+
| Well operation causing pollution and contamination
| style="text-align:right;" | 0.0
 
|  
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 13:08, 24 July 2019

Well Details

Well ID: 34-073-22042
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Country: United States
State: Ohio
County: Hocking
Municipality: Ward Township
Operator Name: FOLEY CANDACE
Well Pad ID:
Farm/Lease Name: HUTCHISON HELEN
License Status: Producing
License Date: 2016-02-25
Spud Date: 1978-04-24
Spud Drilling Contractor:
Final Drill Date: 1978-07-13
Well Total Depth: 3282 ft
Configuration: Vertical
Latitude: 39.496664367
Longitude: -82.21633441

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1977-12-21 420 BELL DRILLING & PROD CO GeoDate 12/21/77
Original Spud 1978-04-24 CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
Completed 1978-07-13 CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
Reached Total Depth 1978-07-13 CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.
CO 1992-09-16 456 SCHMELZER MARK GeoDate 12/21/77
Change of Owner 2008-01-15 Operator changed from 456, SCHMELZER MARK to 8268, JEANIE ENTERPISES LLC
Change of Owner 2008-01-24 Operator changed from 8268, JEANIE ENTERPISES LLC to 8339, FOLEY CHARLES E
Change of Owner 2016-02-25 Operator changed from 8339, FOLEY CHARLES E to 9636, FOLEY CANDACE
Record Last Modified 2016-02-25 CHANGED STATUS OF WELL FROM DM TO PR PER TRANSFER OF WELL FROM CHARLES E. FOLEY #8339 TO OWNER ON 2/25/2016 CM.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1800 Bbl 10000

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1984 BELL DRILLING & PROD CO 4191 77 0
1985 BELL DRILLING & PROD CO 3415 125 365
1987 BELL DRILLING & PROD CO 2920 73 365
1988 BELL DRILLING & PROD CO 2812 70 365
1989 BELL DRILLING & PROD CO 2412 70 365
1990 BELL DRILLING & PROD CO 2308 54 267
1991 BELL DRILLING & PROD CO 2539 0 365
1992 BELL DRILLING & PROD CO 1434 55 243
1995 SCHMELZER MARK 1447 0 365
1996 SCHMELZER MARK 673 0 365
1997 SCHMELZER MARK 1892 43 365
1998 SCHMELZER MARK 1960 0 365
1999 SCHMELZER MARK 1005 0 365
2000 SCHMELZER MARK 604 0 365
2001 SCHMELZER MARK 0 0 365
2002 SCHMELZER MARK 0 0 365
2003 SCHMELZER MARK 0 0 365
2004 SCHMELZER MARK 0 0 365
2005 SCHMELZER MARK 0 0 365

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1984 BELL DRILLING & PROD CO Brine 0 0
1985 BELL DRILLING & PROD CO Brine 88 365
1987 BELL DRILLING & PROD CO Brine 0 365
1988 BELL DRILLING & PROD CO Brine 0 365
1989 BELL DRILLING & PROD CO Brine 0 365
1990 BELL DRILLING & PROD CO Brine 35 267
1991 BELL DRILLING & PROD CO Brine 30 365
1992 BELL DRILLING & PROD CO Brine 20 243
1995 SCHMELZER MARK Brine 50 365
1996 SCHMELZER MARK Brine 50 365
1997 SCHMELZER MARK Brine 0 365
1998 SCHMELZER MARK Brine 0 365
1999 SCHMELZER MARK Brine 0 365
2000 SCHMELZER MARK Brine 0 365
2001 SCHMELZER MARK Brine 0 365
2002 SCHMELZER MARK Brine 0 365
2003 SCHMELZER MARK Brine 0 365
2004 SCHMELZER MARK Brine 0 365
2005 SCHMELZER MARK Brine 0 365

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0267197186 2018-07-11 Production Wells No Violations My inspection revealed the pollution and contamination has not been removed. A portion of the contaminated soil has been removed, but approximately 75 percent remain. New pictures were taken.
0595536981 2019-04-18 Production Wells No Violations I conducted a compliance notice follow-up on this well today. My inspection revealed that the oil has not been cleaned up. It appeared that there was more oil on the ground than my previous inspection. I took five photos during the inspection. I left a voicemail message with the owners phone number that is listed in RBDMS. I also left a business card at the landowners house. Time of inspection: 1:15 PM. Weather: 78 degrees F, Sunny
0670267417 2017-11-09 Production Wells No Violations My inspection revealed the well consists of a pumping unit, 1-100 barrel tank, and separator. There is a 1 inch diameter plastic line hooked to the casing. The 1 inch diameter line has leaked oil. the oil spill is approximately 8 feet by 14 feet., I will follow-up on 11.13.17.
0977720875 2017-12-20 Production Wells No Violations My inspection revealed the well is not in compliance. The oil that was released is being cleaned up. Not all of the oil has been removed. I have contacted the owner of the well to find out when the clean up will be done.
1034352545 2018-02-27 Production Wells No Violations My inspection revealed the pollution and contamination is not fully cleaned up. I spoke with John Payne who does not own the well but is cleaning up the pollution and contamination. Mr. Payne stated he is buying a tractor to aid in removing the contaminated soil. The size of the contamination is approximately 8 feet by 14 feet. The well was written up on 11.13.2017. The well is not in compliance.
1241384692 2017-12-05 Production Wells No Violations My inspection today was to determine if the well had been brought into compliance. The landowner has made progress. The 1 inch diameter plastic line that is connected to the casing has been plumbed into a 55 gallon plastic barrel. There were bags of oil soaked sawdust at the site. Additional saw dust has been placed on the oil to absorb the oil. The well is not in compliance, but progress is being made.
1370185711 2017-11-13 Production Wells Violations Noted I met well owner John Payne. I gave John phone number for Central office to obtain well ownership. The oil spill next to the well will be cleaned up by Johns neighbor George Godenschwager. I suggested they take the oil saturated soil to a approved landfill that will accept the waste. I asked to be informed when the clean up took place so I can witness the clean up.
1755486328 2018-09-20 Production Wells No Violations I conducted a compliance notice follow-up inspection in regards to Inspector Kip Thompsons compliance notice issued on 11/13/2017 for pollution and contamination. My inspection revealed that oil has not been completely cleaned up. I observed several pockets of oil below the well location. Time of inspection: 10:35 AM. Weather: 78 degrees F, Sunny

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1370185711 US-OH-110927 2017-11-21 9-1-07 Well operation causing pollution and contamination

For data sources see[8]

References