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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-127-21114 | | Well ID: 34-127-21114 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.584159823, -82.10104328 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | Municipality: | + | | State: Ohio |
+ | |- | ||
+ | | County: [[Perry_County,_Ohio|Perry]] | ||
+ | |- | ||
+ | | Municipality: [[Monroe_Township,_Perry_County,_Ohio|Monroe Township]] | ||
|- | |- | ||
| Operator Name: [[BURNS WILLARD & FRANCES]] | | Operator Name: [[BURNS WILLARD & FRANCES]] | ||
Line 13: | Line 17: | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: SUNDAY CREEK COAL CO |
|- | |- | ||
− | | | + | | License Status: Final Restoration |
|- | |- | ||
− | | | + | | License Date: 2014-11-18 |
|- | |- | ||
| Spud Date: 1948-03-20 | | Spud Date: 1948-03-20 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
− | |||
− | |||
|- | |- | ||
− | | | + | | Final Drill Date: 1948-04-10 |
|- | |- | ||
− | | | + | | Well Total Depth: 1167 ft |
|- | |- | ||
− | | | + | | Configuration: Vertical |
|- | |- | ||
− | | | + | | Latitude: 39.584159823 |
|- | |- | ||
+ | | Longitude: -82.10104328 | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | + | !scope="col" style="text-align: center"| Well Status |
− | + | !scope="col" style="width: 15%;text-align: center"| Well Status Date | |
− | !scope="col" | + | !scope="col" style="text-align: center"| Comment |
− | |||
− | !scope="col" | ||
− | |||
− | |||
|- | |- | ||
− | | | + | | Oil and Gas |
− | | | + | | 1802-01-01 |
| | | | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 1948-03-20 | ||
| | | | ||
+ | |- | ||
+ | | Completed | ||
+ | | 1948-04-10 | ||
| | | | ||
− | | | + | |- |
+ | | Reached Total Depth | ||
+ | | 1948-04-10 | ||
| | | | ||
|- | |- | ||
+ | | CO | ||
+ | | 1995-10-24 | ||
+ | | 137 ALTHEIRS OIL INC | ||
+ | |- | ||
+ | | CO | ||
+ | | 1995-10-24 | ||
+ | | 4999 BURNS WILLIARD & FRANCES GeoDate | ||
+ | |- | ||
+ | | APP | ||
+ | | 2014-07-15 | ||
+ | | Proposed Formations:BEREA, Issued Date:7/15/2014, Expired Date:7/14/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: | ||
|- | |- | ||
− | | | + | | Plugged/Abandoned |
− | | | + | | 2014-08-25 |
| | | | ||
+ | |- | ||
+ | | Construction Permit Expires | ||
+ | | 2016-07-14 | ||
| | | | ||
+ | |- | ||
+ | | Record Last Modified | ||
+ | | 2017-02-10 | ||
| | | | ||
− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--== Stimulations Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Stimulation Date | ||
+ | !scope="col" style="text-align: center"| Chemical Agent | ||
+ | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) | ||
+ | !scope="col" style="text-align: center"| Fracking Fluid Volume | ||
+ | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) | ||
+ | !scope="col" style="text-align: center"| Fracking Company | ||
+ | !scope="col" style="text-align: center"| Comments | ||
+ | |- | ||
+ | |}--> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 222 | ||
+ | | style="text-align: right;" | 180 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 79 | ||
+ | | style="text-align: right;" | 85 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 81 | ||
+ | | style="text-align: right;" | 80 | ||
+ | |- | ||
+ | | 2014 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 2010 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 14 | ||
+ | | style="text-align: right;" | 180 | ||
+ | |- | ||
+ | | 2011 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 85 | ||
+ | |- | ||
+ | | 2012 | ||
+ | | [[BURNS WILLARD & FRANCES]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 80 | ||
|- | |- | ||
− | | | + | | 2014 |
− | | style="text-align:right;" | | + | | [[BURNS WILLARD & FRANCES]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 0 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = Ohio Department of Natural Resources | + | | title = Risk Based Data Management System - Production Table - Brine Data |
− | | | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2019-05-07 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2019-05-21 }}</ref> |
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
== Inspection Data == | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection ID |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Inspection Type |
− | !scope="col" | + | !scope="col" style="text-align: center"| Inspection Result |
− | + | !scope="col" style="text-align: center"| Inspection Comments | |
− | !scope="col" | + | |- |
− | + | | 0492792830 | |
+ | | 2006-12-21 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | Follow-up on NOV, In-Compliance. | ||
+ | |- | ||
+ | | 0903837778 | ||
+ | | 2014-11-18 | ||
+ | | Final Restoration | ||
+ | | No Violations | ||
+ | | The final restoration meets 1509.072. | ||
|- | |- | ||
| 1162990102 | | 1162990102 | ||
| 2006-11-02 | | 2006-11-02 | ||
− | | | + | | Production Wells |
+ | | Violations Noted | ||
| An inspection of the well revealed wrond owner name on ID. | | An inspection of the well revealed wrond owner name on ID. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1408987571 | | 1408987571 | ||
| 2014-08-25 | | 2014-08-25 | ||
− | | | + | | Plug / Plug Back |
+ | | No Violations | ||
| I returned to this well to check to see if the clay was still at the surface. The clay was still there so I informed Willard that he is able to cut the wellhead off and start reclaiming this location. | | I returned to this well to check to see if the clay was still at the surface. The clay was still there so I informed Willard that he is able to cut the wellhead off and start reclaiming this location. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1456667602 | | 1456667602 | ||
| 2014-08-20 | | 2014-08-20 | ||
− | | | + | | Plug / Plug Back |
+ | | No Violations | ||
| I was on location today to witness the plugging of this well. Willard will be using plugging clay to plug the well from the Berea to surface. He has rigged up on the well and is running his tools to find bottom. He tagged bottom at 1079ft. The 5.5 casing was left in the hole to protect the fresh water zone. The well will be left open to make sure the clay does not settle. If it does it will be topped off. | | I was on location today to witness the plugging of this well. Willard will be using plugging clay to plug the well from the Berea to surface. He has rigged up on the well and is running his tools to find bottom. He tagged bottom at 1079ft. The 5.5 casing was left in the hole to protect the fresh water zone. The well will be left open to make sure the clay does not settle. If it does it will be topped off. | ||
− | |||
− | |||
− | |||
− | |||
|- | |- | ||
| 1900297438 | | 1900297438 | ||
| 2014-08-11 | | 2014-08-11 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| I met with Willard Burns to discuss when he would be plugging this well. He stated he would have a service rig in on the well within the next couple of weeks to plug it. Willard said he would contact me to let me know when he moves in on the well. | | I met with Willard Burns to discuss when he would be plugging this well. He stated he would have a service rig in on the well within the next couple of weeks to plug it. Willard said he would contact me to let me know when he moves in on the well. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | | 1905559945 | ||
+ | | 2016-05-24 | ||
+ | | Final Restoration | ||
+ | | No Violations | ||
+ | | Mr. Burns received a compliance notice for the production on this well. The well was plugged in 2014. I was on location to witness the plugging of the well. Prior to that the well did not make anything thats why they decided to plug it. | ||
|- | |- | ||
− | | | + | | 2131449375 |
| 2014-02-03 | | 2014-02-03 | ||
− | | | + | | Production Wells |
+ | | No Violations | ||
| I did an inspection on this well and found that the tubing and rods have been removed. There is just casing left in the well with a wellhead on it. I stopped at Willard Burns shop to see what he is doing to this well. He let me know that he had a rig on there to replace the casing but they could not pull it. He informed me that he is going to run a packer in the well to fix the casing. We talked about how to do it and he said he plans on doing it in the spring when the weather is better. | | I did an inspection on this well and found that the tubing and rods have been removed. There is just casing left in the well with a wellhead on it. I stopped at Willard Burns shop to see what he is doing to this well. He let me know that he had a rig on there to replace the casing but they could not pull it. He informed me that he is going to run a packer in the well to fix the casing. We talked about how to do it and he said he plans on doing it in the spring when the weather is better. | ||
− | |||
− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | ==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
|- | |- | ||
− | | | + | | 1162990102 |
− | | | + | | US-OH-104339 |
− | + | | 2006-11-08 | |
− | |||
− | |||
− | |||
− | |||
− | | | ||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
− | |||
| | | | ||
+ | | Failure to legibly identify well | ||
|- | |- | ||
|} | |} | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2019-05-07 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2019-05-21 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-127-21114 | Loading map...
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Country: United States | |
State: Ohio | |
County: Perry | |
Municipality: Monroe Township | |
Operator Name: BURNS WILLARD & FRANCES | |
Well Pad ID: | |
Farm/Lease Name: SUNDAY CREEK COAL CO | |
License Status: Final Restoration | |
License Date: 2014-11-18 | |
Spud Date: 1948-03-20 | |
Spud Drilling Contractor: | |
Final Drill Date: 1948-04-10 | |
Well Total Depth: 1167 ft | |
Configuration: Vertical | |
Latitude: 39.584159823 | |
Longitude: -82.10104328 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1802-01-01 | |
Original Spud | 1948-03-20 | |
Completed | 1948-04-10 | |
Reached Total Depth | 1948-04-10 | |
CO | 1995-10-24 | 137 ALTHEIRS OIL INC |
CO | 1995-10-24 | 4999 BURNS WILLIARD & FRANCES GeoDate |
APP | 2014-07-15 | Proposed Formations:BEREA, Issued Date:7/15/2014, Expired Date:7/14/2016 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2014-08-25 | |
Construction Permit Expires | 2016-07-14 | |
Record Last Modified | 2017-02-10 |
For data sources see[2]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2010 | BURNS WILLARD & FRANCES | 0 | 222 | 180 |
2011 | BURNS WILLARD & FRANCES | 0 | 79 | 85 |
2012 | BURNS WILLARD & FRANCES | 0 | 81 | 80 |
2014 | BURNS WILLARD & FRANCES | 0 | 0 | 0 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2010 | BURNS WILLARD & FRANCES | Brine | 14 | 180 |
2011 | BURNS WILLARD & FRANCES | Brine | 10 | 85 |
2012 | BURNS WILLARD & FRANCES | Brine | 10 | 80 |
2014 | BURNS WILLARD & FRANCES | Brine | 0 | 0 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0492792830 | 2006-12-21 | Production Wells | No Violations | Follow-up on NOV, In-Compliance. |
0903837778 | 2014-11-18 | Final Restoration | No Violations | The final restoration meets 1509.072. |
1162990102 | 2006-11-02 | Production Wells | Violations Noted | An inspection of the well revealed wrond owner name on ID. |
1408987571 | 2014-08-25 | Plug / Plug Back | No Violations | I returned to this well to check to see if the clay was still at the surface. The clay was still there so I informed Willard that he is able to cut the wellhead off and start reclaiming this location. |
1456667602 | 2014-08-20 | Plug / Plug Back | No Violations | I was on location today to witness the plugging of this well. Willard will be using plugging clay to plug the well from the Berea to surface. He has rigged up on the well and is running his tools to find bottom. He tagged bottom at 1079ft. The 5.5 casing was left in the hole to protect the fresh water zone. The well will be left open to make sure the clay does not settle. If it does it will be topped off. |
1900297438 | 2014-08-11 | Production Wells | No Violations | I met with Willard Burns to discuss when he would be plugging this well. He stated he would have a service rig in on the well within the next couple of weeks to plug it. Willard said he would contact me to let me know when he moves in on the well. |
1905559945 | 2016-05-24 | Final Restoration | No Violations | Mr. Burns received a compliance notice for the production on this well. The well was plugged in 2014. I was on location to witness the plugging of the well. Prior to that the well did not make anything thats why they decided to plug it. |
2131449375 | 2014-02-03 | Production Wells | No Violations | I did an inspection on this well and found that the tubing and rods have been removed. There is just casing left in the well with a wellhead on it. I stopped at Willard Burns shop to see what he is doing to this well. He let me know that he had a rig on there to replace the casing but they could not pull it. He informed me that he is going to run a packer in the well to fix the casing. We talked about how to do it and he said he plans on doing it in the spring when the weather is better. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1162990102 | US-OH-104339 | 2006-11-08 | Failure to legibly identify well |
For data sources see[7]