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Difference between revisions of "34-099-20430"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-099-20430
 
| Well ID: 34-099-20430
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.05585192, -80.8521138 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.055854693, -80.85173363 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Mahoning County, Ohio|Mahoning]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Mahoning_County,_Ohio|Mahoning]]
 +
|-
 +
| Municipality: [[Ellsworth_Township,_Mahoning_County,_Ohio|Ellsworth Township]]
 
|-
 
|-
 
| Operator Name: [[SAMURAI OPERATING COMPANY]]
 
| Operator Name: [[SAMURAI OPERATING COMPANY]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: WR MILLER UNIT
 
|-
 
|-
| First Permit Date:  
+
| License Status: Producing
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2006-09-12
 
|-
 
|-
 
| Spud Date: 1974-01-08
 
| Spud Date: 1974-01-08
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:  
 +
|-
 +
| Final Drill Date: 1974-01-15
 +
|-
 +
| Well Total Depth: 5191 ft
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Producing
+
| Latitude: 41.055854693
 +
|-
 +
| Longitude: -80.85173363
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Violations: 0
+
| Original Spud
 +
| 1974-01-08
 +
 
|-
 
|-
| Latitude: 41.05585192
+
| Completed
 +
| 1974-01-15
 +
 
|-
 
|-
| Longitude: -80.8521138
+
| Reached Total Depth
 +
| 1974-01-15
 +
 +
|-
 +
| CO
 +
| 1984-10-17
 +
| 1757    EDISTO RESOURCES CORP
 +
|-
 +
| CO
 +
| 1991-12-10
 +
| 4178  EASTERN AMER ENERGY CORP  GeoDate 
 +
|-
 +
| Change of Owner
 +
| 2006-03-15
 +
| Operator changed from 4178, EASTERN AMER ENERGY CORP to 8002, LAKE FORK RESOURCES OPER LLC
 +
|-
 +
| Change of Owner
 +
| 2008-11-21
 +
| Operator changed from 8002, LAKE FORK RESOURCES OPER LLC to 8453, SAMURAI OPERATING COMPANY
 +
|-
 +
| Record Last Modified
 +
| 2019-06-04
 +
 
|-
 
|-
 
|}
 
|}
== Production Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
| 2006-09-11
 +
| style="text-align: right;" | 5013
 +
| style="text-align: right;" | 5104
 +
| style="text-align: right;" | 7
 +
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Perfs Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
== Stimulations Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | PERIOD
+
!scope="col" style="text-align: center"| Stimulation Date
!scope="col" | GAS QUANTITY
+
!scope="col" style="text-align: center"| Chemical Agent
!scope="col" | GAS PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
!scope="col" | CONDENSATE QUANTITY
+
!scope="col" style="text-align: center"| Fracking Fluid Volume
!scope="col" | CONDENSATE PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
!scope="col" | OIL QUANTITY
+
!scope="col" style="text-align: center"| Fracking Company
!scope="col" | OIL PRODUCTION DAYS
+
!scope="col" style="text-align: center"| Comments
 
|-
 
|-
| 1992-0
 
| style="text-align:right;" | 550.0
 
 
|  
 
|  
 +
| H2O
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 1406 Bbl
 +
| style="text-align: right;" | 64000
 
|  
 
|  
 
|  
 
|  
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - tblStimulation Table
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Production Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Gas Quantity (mcf)
 +
!scope="col" style="text-align: center"| Oil Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 +
|-
 +
| 1992
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 550
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1993
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 3447
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1994
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 6807
 +
| style="text-align: right;" | 69
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1995
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 5637
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 1996
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 2385
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
|-
 +
| 1997
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 1766
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 334
 +
|-
 +
| 1998
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 4257
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 334
 +
|-
 +
| 1999
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 3848
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2000
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 3756
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2001
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 4572
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 +
|-
 +
| 2002
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 4823
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 330
 +
|-
 +
| 2003
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| style="text-align: right;" | 5593
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1993-0
+
| 2004
| style="text-align:right;" | 3447.0
+
| [[EASTERN AMER ENERGY CORP]]
|  
+
| style="text-align: right;" | 4868
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2006
 +
| [[LAKE FORK RESOURCES OPER LLC]]
 +
| style="text-align: right;" | 3290
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1994-0
+
| 2007
| style="text-align:right;" | 6807.0
+
| [[LAKE FORK RESOURCES OPER LLC]]
|  
+
| style="text-align: right;" | 3190
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 69.0
 
|
 
 
|-
 
|-
 +
| 2008
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 1875
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 151
 
|-
 
|-
| 1995-0
+
| 2009
| style="text-align:right;" | 5637.0
+
| [[SAMURAI OPERATING COMPANY]]
|  
+
| style="text-align: right;" | 3957
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2010
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 3894
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1996-0
+
| 2011
| style="text-align:right;" | 2385.0
+
| [[SAMURAI OPERATING COMPANY]]
|  
+
| style="text-align: right;" | 4287
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2012
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 4008
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 366
 
|-
 
|-
| 1997-0
+
| 2013
| style="text-align:right;" | 1766.0
+
| [[SAMURAI OPERATING COMPANY]]
|  
+
| style="text-align: right;" | 3770
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2014
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 3602
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1998-0
+
| 2015
| style="text-align:right;" | 4257.0
+
| [[SAMURAI OPERATING COMPANY]]
|  
+
| style="text-align: right;" | 5177
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2016
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 3033
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 1999-0
+
| 2017
| style="text-align:right;" | 3848.0
+
| [[SAMURAI OPERATING COMPANY]]
|  
+
| style="text-align: right;" | 78
|
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2018
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2000-0
+
|}
| style="text-align:right;" | 3756.0
+
For data sources see<ref>{{cite web
|  
+
| title = Risk Based Data Management System - Production Table - Oil and Gas Data
|  
+
|publisher = [[Ohio Department of Natural Resources]]
|  
+
| date =  2019-05-07
| style="text-align:right;" | 0.0
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
|
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Oil and Gas Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date = 2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Waste Data ==
 +
{| class="wikitable sortable"
 +
!scope="col" style="text-align: center"| Period
 +
!scope="col" style="text-align: center"| Operator Name
 +
!scope="col" style="text-align: center"| Waste Type
 +
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
| 1992
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" |
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2001-0
+
| 1993
| style="text-align:right;" | 4572.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1994
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2002-0
+
| 1995
| style="text-align:right;" | 4823.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" |  
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1996
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 0
 
|-
 
|-
| 2003-0
+
| 1997
| style="text-align:right;" | 5593.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 334
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 1998
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 334
 
|-
 
|-
| 2004-0
+
| 1999
| style="text-align:right;" | 4868.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2000
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2006-0
+
| 2001
| style="text-align:right;" | 3290.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2002
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 330
 
|-
 
|-
| 2007-0
+
| 2003
| style="text-align:right;" | 3190.0
+
| [[EASTERN AMER ENERGY CORP]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2004
 +
| [[EASTERN AMER ENERGY CORP]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2008-0
+
| 2006
| style="text-align:right;" | 1875.0
+
| [[LAKE FORK RESOURCES OPER LLC]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2007
 +
| [[LAKE FORK RESOURCES OPER LLC]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2009-0
+
| 2008
| style="text-align:right;" | 3957.0
+
| [[SAMURAI OPERATING COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 151
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2009
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2010-0
+
| 2010
| style="text-align:right;" | 3894.0
+
| [[SAMURAI OPERATING COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2011
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2011-0
+
| 2012
| style="text-align:right;" | 4287.0
+
| [[SAMURAI OPERATING COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 62
|
+
| style="text-align: right;" | 366
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2013
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2012-0
+
| 2014
| style="text-align:right;" | 4008.0
+
| [[SAMURAI OPERATING COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2015
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2013-0
+
| 2016
| style="text-align:right;" | 3770.0
+
| [[SAMURAI OPERATING COMPANY]]
|
+
| Brine
|
+
| style="text-align: right;" | 0
|
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
|
 
 
|-
 
|-
 +
| 2017
 +
| [[SAMURAI OPERATING COMPANY]]
 +
| Brine
 +
| style="text-align: right;" | 0
 +
| style="text-align: right;" | 365
 
|-
 
|-
| 2014-0
+
| 2018
| style="text-align:right;" | 3602.0
+
| [[SAMURAI OPERATING COMPANY]]
| style="text-align:right;" | 365.0
+
| Brine
|  
+
| style="text-align: right;" | 0
|  
+
| style="text-align: right;" | 365
| style="text-align:right;" | 0.0
 
| style="text-align:right;" | 365.0
 
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - Production Table - Brine Data
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
|publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date =  2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Production
+
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
| accessdate = 2019-05-21 }}</ref>
 +
<ref>{{cite web
 +
| title = Combined Production - Brine Data
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
  | date = 2019-05-07
 +
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
  | accessdate = 2019-05-21 }}</ref>
 
== Inspection Data ==
 
== Inspection Data ==
 +
==== Inspections Performed ====
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Inspection ID
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Inspection Date
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Inspection Type
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Inspection Result
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Inspection Comments
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
 
| 1250159758
 
| 1250159758
 
| 2009-08-12
 
| 2009-08-12
|  
+
| Production Wells
 +
| Violations Noted
 
| I was called out on 8/11/09 at 10:00PM by Kurt Kollar of the Ohio EPA(216-789-9282. Lightening had struck the stock tank and blow out the bottom third of the tank.  The Ellsworth Fire Department were on the scene.  I tried to find an ID sign on the stock tank.  It was only half there.  I finally called Dick  Heldman ( 330-807-4224) who was the pumper contractor for Samurai Operating Company.  I needed the well shut down.  Mr. Heldman did come out and shut the well in.   
 
| I was called out on 8/11/09 at 10:00PM by Kurt Kollar of the Ohio EPA(216-789-9282. Lightening had struck the stock tank and blow out the bottom third of the tank.  The Ellsworth Fire Department were on the scene.  I tried to find an ID sign on the stock tank.  It was only half there.  I finally called Dick  Heldman ( 330-807-4224) who was the pumper contractor for Samurai Operating Company.  I needed the well shut down.  Mr. Heldman did come out and shut the well in.   
 
Mr. Larry Bynum from Houston(713-771-5500), Field Superintendent, called to make sure everything was going good.  EPA had the spill contained with 4 booms in the North Fork Creek.  Mr. Kollar decided to wait till day light before we start the clean up.  I arrived  at the site and found that there was no dike. I called Mr. Bynum to let him know that there was no emergency phone number on the ID sign and there was no dike around the stock tank. He agreed to install a dike when the repair work is finished.  The clean up is at 80%. The 100 tank had less than 3 barrels of oil in it.  Less than 10 gallons went into North Fork Creek.  The paper and TV reported that the spill was 10,000 gallons.  This report was not correct.  This case continues.
 
Mr. Larry Bynum from Houston(713-771-5500), Field Superintendent, called to make sure everything was going good.  EPA had the spill contained with 4 booms in the North Fork Creek.  Mr. Kollar decided to wait till day light before we start the clean up.  I arrived  at the site and found that there was no dike. I called Mr. Bynum to let him know that there was no emergency phone number on the ID sign and there was no dike around the stock tank. He agreed to install a dike when the repair work is finished.  The clean up is at 80%. The 100 tank had less than 3 barrels of oil in it.  Less than 10 gallons went into North Fork Creek.  The paper and TV reported that the spill was 10,000 gallons.  This report was not correct.  This case continues.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1250706844
 
| 1250706844
 
| 2009-08-19
 
| 2009-08-19
|  
+
| Production Wells
 +
| No Violations
 
| The dike and the 50 barrel plastic stock tank were installed.  The ID sign was posted.  This NOV is resolved.
 
| The dike and the 50 barrel plastic stock tank were installed.  The ID sign was posted.  This NOV is resolved.
|
 
|
 
|
 
 
|-
 
|-
 +
| 1780184640
 +
| 2009-08-13
 +
| Production Wells
 +
| No Violations
 +
| The cleanup is 95% done.  The dike is up and the new 50 barrel plastic stock tank has been installed.  The diapers and booms are still in the creek.  The old dirt and oil from the dike has not been hauled away yet.  This case continues.
 +
|-
 +
|}
 +
==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -1780184640
+
| 1250159758
 +
| US-OH-106690
 
| 2009-08-13
 
| 2009-08-13
 
|  
 
|  
| The cleanup is 95% done.  The dike is up and the new 50 barrel plastic stock tank has been installed.  The diapers and booms are still in the creek.  The old dirt and oil from the dike has not been hauled away yet.  This case continues.
+
| Failure to legibly identify well
|  
+
|-
|  
+
| 1250159758
 +
| US-OH-106691
 +
| 2009-08-13
 
|  
 
|  
 +
| No SPCC dike/or failure to keep dike free of water or oil
 
|-
 
|-
 
|}
 
|}
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 20:50, 24 July 2019

Well Details

Well ID: 34-099-20430
Loading map...
Country: United States
State: Ohio
County: Mahoning
Municipality: Ellsworth Township
Operator Name: SAMURAI OPERATING COMPANY
Well Pad ID:
Farm/Lease Name: WR MILLER UNIT
License Status: Producing
License Date: 2006-09-12
Spud Date: 1974-01-08
Spud Drilling Contractor:
Final Drill Date: 1974-01-15
Well Total Depth: 5191 ft
Configuration: Vertical
Latitude: 41.055854693
Longitude: -80.85173363

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1974-01-08
Completed 1974-01-15
Reached Total Depth 1974-01-15
CO 1984-10-17 1757 EDISTO RESOURCES CORP
CO 1991-12-10 4178 EASTERN AMER ENERGY CORP GeoDate
Change of Owner 2006-03-15 Operator changed from 4178, EASTERN AMER ENERGY CORP to 8002, LAKE FORK RESOURCES OPER LLC
Change of Owner 2008-11-21 Operator changed from 8002, LAKE FORK RESOURCES OPER LLC to 8453, SAMURAI OPERATING COMPANY
Record Last Modified 2019-06-04

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 5013 5104 7

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 1406 Bbl 64000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1992 EASTERN AMER ENERGY CORP 550 0 365
1993 EASTERN AMER ENERGY CORP 3447 0 365
1994 EASTERN AMER ENERGY CORP 6807 69 365
1995 EASTERN AMER ENERGY CORP 5637 0 365
1996 EASTERN AMER ENERGY CORP 2385 0 0
1997 EASTERN AMER ENERGY CORP 1766 0 334
1998 EASTERN AMER ENERGY CORP 4257 0 334
1999 EASTERN AMER ENERGY CORP 3848 0 365
2000 EASTERN AMER ENERGY CORP 3756 0 365
2001 EASTERN AMER ENERGY CORP 4572 0 365
2002 EASTERN AMER ENERGY CORP 4823 0 330
2003 EASTERN AMER ENERGY CORP 5593 0 365
2004 EASTERN AMER ENERGY CORP 4868 0 365
2006 LAKE FORK RESOURCES OPER LLC 3290 0 365
2007 LAKE FORK RESOURCES OPER LLC 3190 0 365
2008 SAMURAI OPERATING COMPANY 1875 0 151
2009 SAMURAI OPERATING COMPANY 3957 0 365
2010 SAMURAI OPERATING COMPANY 3894 0 365
2011 SAMURAI OPERATING COMPANY 4287 0 365
2012 SAMURAI OPERATING COMPANY 4008 0 366
2013 SAMURAI OPERATING COMPANY 3770 0 365
2014 SAMURAI OPERATING COMPANY 3602 0 365
2015 SAMURAI OPERATING COMPANY 5177 0 365
2016 SAMURAI OPERATING COMPANY 3033 0 365
2017 SAMURAI OPERATING COMPANY 78 0 365
2018 SAMURAI OPERATING COMPANY 0 0 365

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1992 EASTERN AMER ENERGY CORP Brine 365
1993 EASTERN AMER ENERGY CORP Brine 0 365
1994 EASTERN AMER ENERGY CORP Brine 0 365
1995 EASTERN AMER ENERGY CORP Brine 365
1996 EASTERN AMER ENERGY CORP Brine 0 0
1997 EASTERN AMER ENERGY CORP Brine 0 334
1998 EASTERN AMER ENERGY CORP Brine 0 334
1999 EASTERN AMER ENERGY CORP Brine 0 365
2000 EASTERN AMER ENERGY CORP Brine 0 365
2001 EASTERN AMER ENERGY CORP Brine 0 365
2002 EASTERN AMER ENERGY CORP Brine 0 330
2003 EASTERN AMER ENERGY CORP Brine 0 365
2004 EASTERN AMER ENERGY CORP Brine 0 365
2006 LAKE FORK RESOURCES OPER LLC Brine 0 365
2007 LAKE FORK RESOURCES OPER LLC Brine 0 365
2008 SAMURAI OPERATING COMPANY Brine 0 151
2009 SAMURAI OPERATING COMPANY Brine 0 365
2010 SAMURAI OPERATING COMPANY Brine 0 365
2011 SAMURAI OPERATING COMPANY Brine 0 365
2012 SAMURAI OPERATING COMPANY Brine 62 366
2013 SAMURAI OPERATING COMPANY Brine 0 365
2014 SAMURAI OPERATING COMPANY Brine 0 365
2015 SAMURAI OPERATING COMPANY Brine 0 365
2016 SAMURAI OPERATING COMPANY Brine 0 365
2017 SAMURAI OPERATING COMPANY Brine 0 365
2018 SAMURAI OPERATING COMPANY Brine 0 365

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1250159758 2009-08-12 Production Wells Violations Noted I was called out on 8/11/09 at 10:00PM by Kurt Kollar of the Ohio EPA(216-789-9282. Lightening had struck the stock tank and blow out the bottom third of the tank. The Ellsworth Fire Department were on the scene. I tried to find an ID sign on the stock tank. It was only half there. I finally called Dick Heldman ( 330-807-4224) who was the pumper contractor for Samurai Operating Company. I needed the well shut down. Mr. Heldman did come out and shut the well in.

Mr. Larry Bynum from Houston(713-771-5500), Field Superintendent, called to make sure everything was going good. EPA had the spill contained with 4 booms in the North Fork Creek. Mr. Kollar decided to wait till day light before we start the clean up. I arrived at the site and found that there was no dike. I called Mr. Bynum to let him know that there was no emergency phone number on the ID sign and there was no dike around the stock tank. He agreed to install a dike when the repair work is finished. The clean up is at 80%. The 100 tank had less than 3 barrels of oil in it. Less than 10 gallons went into North Fork Creek. The paper and TV reported that the spill was 10,000 gallons. This report was not correct. This case continues.

1250706844 2009-08-19 Production Wells No Violations The dike and the 50 barrel plastic stock tank were installed. The ID sign was posted. This NOV is resolved.
1780184640 2009-08-13 Production Wells No Violations The cleanup is 95% done. The dike is up and the new 50 barrel plastic stock tank has been installed. The diapers and booms are still in the creek. The old dirt and oil from the dike has not been hauled away yet. This case continues.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1250159758 US-OH-106690 2009-08-13 Failure to legibly identify well
1250159758 US-OH-106691 2009-08-13 No SPCC dike/or failure to keep dike free of water or oil

For data sources see[9]

References