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| License Status: Active Injection | | License Status: Active Injection | ||
|- | |- | ||
− | | License Date: | + | | License Date: 1986-07-14 |
|- | |- | ||
| Spud Date: 1986-07-30 | | Spud Date: 1986-07-30 |
Well ID: 34-005-22515 | Loading map...
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Country: United States | |
State: Ohio | |
County: Ashland | |
Municipality: Jackson Township | |
Operator Name: DEEP RESOURCES LLC | |
Well Pad ID: | |
Farm/Lease Name: BROWN UNIT | |
License Status: Active Injection | |
License Date: 1986-07-14 | |
Spud Date: 1986-07-30 | |
Spud Drilling Contractor: P&N DRLG | |
Final Drill Date: 1987-01-15 | |
Well Total Depth: 748 ft | |
Configuration: Vertical | |
Latitude: 40.901972611 | |
Longitude: -82.14671376 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1986-07-07 | 133 QUAKER STATE OIL REF CORP GeoDate 7/7/86 |
Enhanced Recovery | 1986-07-07 | Issued Date 7/14/86 Expired Date 7/14/87 Acres 0150047 Tool Type NT Proposed Formation BEREA Proposed Depth 00748 Proposed Drill Depth 00748 |
Original Spud | 1986-07-30 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
First Injection | 1986-12-03 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Completion Report Received | 1987-01-12 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Completed | 1987-01-15 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Reached Total Depth | 1987-01-15 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Construction Permit Expires | 1987-07-14 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 7/7/86 |
Annulus Pressure Monitoring Approved | 1998-06-09 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Last Compliance Report | 2000-01-14 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
Change of Owner | 2002-02-07 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 2491, MILLER ROY/RA MILLER ENER |
Change of Owner | 2008-04-24 | Operator changed from 2491, MILLER ROY/RA MILLER ENER to 8227, DEEP RESOURCES LLC |
Record Last Modified | 2017-02-15 | CONVERT 7-12-86, LOG TYPE=(X-Y) INJECTION RATE : 20 BPD |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2000-05-23 | 670 | 720 | 0 |
2000-05-23 | 675 | 705 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 40 Qts | 0 | FOR ERP | ||
NITR | 0 | 100 Qts | 0 | FOR PRODUCTION |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | QUAKER STATE OIL REF CORP | 0 | 0 | 0 |
1985 | QUAKER STATE OIL REF CORP | 0 | 0 | 0 |
1986 | QUAKER STATE OIL REF CORP | 0 | 7 | 365 |
1987 | QUAKER STATE OIL REF CORP | 0 | 20 | 365 |
1988 | QUAKER STATE OIL REF CORP | 0 | 49 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | QUAKER STATE OIL REF CORP | Brine | 0 | 0 |
1985 | QUAKER STATE OIL REF CORP | Brine | 0 | 0 |
1986 | QUAKER STATE OIL REF CORP | Brine | 0 | 365 |
1987 | QUAKER STATE OIL REF CORP | Brine | 46 | 365 |
1988 | QUAKER STATE OIL REF CORP | Brine | 48 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0016078257 | 2016-11-01 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0096674668 | 2014-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0098663015 | 2005-12-01 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0142504724 | 2018-05-02 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0187265422 | 2017-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0209075839 | 2010-12-16 | Enhanced Recovery Project | Violations Noted | Injection and annulus pressure test. ERP# 19, W-6. |
0257465535 | 2009-04-27 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0358586615 | 2012-05-31 | Enhanced Recovery Project | No Violations | Inspect Well. |
0370412118 | 2012-12-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0453286750 | 2010-04-06 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0468045381 | 2008-12-18 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0509274170 | 2017-11-14 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0770744265 | 2003-08-07 | Enhanced Recovery Project | No Violations | CANNOT ACCESS INJECTION PSI, NEED TO REPLACE WITH 1/2 OR 1/4 VALVE FOR GAUGE |
0875210395 | 2009-10-07 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
0906784221 | 2015-05-18 | Enhanced Recovery Project | No Violations | The well is an injection well in the waterflood enhanced recovery project. ID posted. |
0943677300 | 2010-12-17 | Enhanced Recovery Project | No Violations | Pressured up annulus to 280 psi. No drop in pressure in 15 minutes. W-6 |
0944436228 | 2014-03-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0980994820 | 2012-03-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
0981320109 | 2004-11-17 | Enhanced Recovery Project | No Violations | Injection pressure test. |
1011304060 | 2006-08-21 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. Sun, 75 degrees. |
1018852456 | 2017-01-05 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1062308488 | 2008-03-13 | Enhanced Recovery Project | No Violations | Annulus and injection pressure test. |
1166552149 | 2006-12-19 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1230778509 | 2005-04-27 | Enhanced Recovery Project | No Violations | Injection well test. |
1285411367 | 2014-07-17 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1445429518 | 2015-10-20 | Enhanced Recovery Project | No Violations | Notified by operator the well was serviced and worked over. Inspected well for compliance. The 2-3/8 inch casing failed at the well head. A hanger bracket caused the casing to rust through. The casing was cut off below grade and new casing was welded in place. The tubing packer was not released during the workover. The compliance order of 8/28/2015 was released. |
1446048412 | 2015-10-26 | Enhanced Recovery Project | No Violations | On June 11, 1998 a total of 24 joints of one inch tubing at 25 feet long were set in the hole at 600 feet. On October 9, 2015 notified by operator the well was serviced and worked over. The 2-3/8 inch casing split open and failed at the well head. A hanger bracket caused the casing to rust through. The well head was excavated and the casing was cut off below grade. The casing was threaded and new casing was installed and reassembled. The tubing and packer set in compression was not released during the workover. One inch of the one inch injection tubing was cut off and re-threaded. The compliance order of 8/28/2015 was resolved. Conduct a mechanical integrity test on well. Well annulus was pressured to 360 psi and held for 15 minutes with zero pressure loss. Well passes. Well is put into production. Compliance notice has been resolved. |
1453264915 | 2012-09-11 | Enhanced Recovery Project | No Violations | Inspect Well. Site ok. |
1568085131 | 2018-08-20 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1592563039 | 2014-05-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1607016907 | 2017-04-24 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1626257319 | 2018-10-10 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1684121092 | 2016-01-06 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1752943849 | 2007-10-17 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1756283585 | 2013-04-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. Conduct fifteen minute pressure test on well. Passed test. |
1803023632 | 2016-04-15 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1832805483 | 2013-10-29 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1853055022 | 2019-01-04 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1867454530 | 2015-03-19 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
1886404824 | 2007-05-24 | Enhanced Recovery Project | No Violations | Injection and annulus pressure test. |
1943737110 | 2012-02-06 | Enhanced Recovery Project | No Violations | inspect well. |
1953276135 | 2011-07-11 | Enhanced Recovery Project | No Violations | inspect well. |
1998582579 | 2015-05-20 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The injection valve is leaking. |
2010575679 | 2011-10-18 | Enhanced Recovery Project | No Violations | Inspect well. |
2033086035 | 2015-08-28 | Enhanced Recovery Project | Violations Noted | Inspect well for integrity and pressure. The well is shut in. the injection tubing valve is broken. |
2044282527 | 2018-01-18 | Enhanced Recovery Project | No Violations | Inspect well for integrity and pressure. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0209075839 | US-OH-121353 | 2010-12-16 | Failure to conduct or pass mech. integrity test | |
1998582579 | US-OH-120287 | 2015-07-17 | Mechanical failure/contamination | |
2033086035 | US-OH-120669 | 2015-12-15 | Violation of injection tubing/fitting requirements |
For data sources see[9]