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| License Status: Producing | | License Status: Producing | ||
|- | |- | ||
− | | License Date: | + | | License Date: |
|- | |- | ||
| Spud Date: 1955-11-08 | | Spud Date: 1955-11-08 |
Well ID: 34-009-21218 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Ames Township | |
Operator Name: KEITO GAS INC | |
Well Pad ID: | |
Farm/Lease Name: BALL PEARL | |
License Status: Producing | |
License Date: | |
Spud Date: 1955-11-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1955-11-22 | |
Well Total Depth: 1544 ft | |
Configuration: Vertical | |
Latitude: 39.453020723 | |
Longitude: -81.96366394 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1955-11-08 | |
Completed | 1955-11-22 | |
Reached Total Depth | 1955-11-22 | |
CO | 1991-06-20 | 3969 KAPLAN INTERESTS INC |
Change of Owner | 2004-07-08 | Operator changed from 3969, KAPLAN INTERESTS INC to 7671, KEITO GAS INC |
Record Last Modified | 2013-10-03 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | GLENEAYRE RESOURCES INC | 62 | 0 | 120 |
2002 | KAPLAN INTERESTS INC | 0 | 0 | 365 |
2003 | KAPLAN INTERESTS INC | 0 | 0 | 365 |
2004 | KEITO GAS INC | 0 | 0 | 180 |
2005 | KEITO GAS INC | 0 | 0 | 365 |
2006 | KEITO GAS INC | 0 | 0 | 365 |
2007 | KEITO GAS INC | 0 | 0 | 365 |
2008 | KEITO GAS INC | 0 | 0 | 365 |
2009 | KEITO GAS INC | 0 | 0 | 365 |
2010 | KEITO GAS INC | 0 | 0 | 365 |
2011 | KEITO GAS INC | 0 | 0 | 365 |
2012 | KEITO GAS INC | 0 | 0 | 366 |
2013 | KEITO GAS INC | 0 | 0 | 365 |
2014 | KEITO GAS INC | 0 | 0 | 365 |
2015 | KEITO GAS INC | 0 | 0 | 365 |
2016 | KEITO GAS INC | 0 | 0 | 365 |
2017 | KEITO GAS INC | 0 | 0 | 365 |
2018 | KEITO GAS INC | 0 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1987 | GLENEAYRE RESOURCES INC | Brine | 0 | 120 |
2002 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2003 | KAPLAN INTERESTS INC | Brine | 0 | 365 |
2004 | KEITO GAS INC | Brine | 0 | 180 |
2005 | KEITO GAS INC | Brine | 0 | 365 |
2006 | KEITO GAS INC | Brine | 0 | 365 |
2007 | KEITO GAS INC | Brine | 0 | 365 |
2008 | KEITO GAS INC | Brine | 0 | 365 |
2009 | KEITO GAS INC | Brine | 0 | 365 |
2010 | KEITO GAS INC | Brine | 0 | 365 |
2011 | KEITO GAS INC | Brine | 0 | 365 |
2012 | KEITO GAS INC | Brine | 0 | 366 |
2013 | KEITO GAS INC | Brine | 0 | 365 |
2014 | KEITO GAS INC | Brine | 0 | 365 |
2015 | KEITO GAS INC | Brine | 0 | 365 |
2016 | KEITO GAS INC | Brine | 0 | 365 |
2017 | KEITO GAS INC | Brine | 0 | 365 |
2018 | KEITO GAS INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0129121331 | 2019-03-20 | Production Wells | No Violations | My inspection revealed the gas leak has been repaired. The owner of the well has installed a new valve to replace the leaking valve that was located on 2 inch diameter steel production line. |
1083713094 | 2019-03-01 | Production Wells | No Violations | I received a call from Amesville assistant fire chief Mr. Brad Maxwell on 2.28.19. Mr. Maxwell responded to a house fire approximetly 1 week ago. Mr. Maxwell reported the apparent cause of the fire was leaking natural gas in the home. The home was using natural gas from a natural gas well on the property. In attempting to locate a valve to turn off the natural gas that was feeding the house fire, they discovered two natural gas leaks. I responded on 2.28.19 and found two 2 inch diameter ball valves that were part of the natural gas gathering system to be leaking. A member of Keito Gas met me on site today and was able to repair a leaking valve. The second leaking valve will need replaced and I was told By Amtec Oil owner Mr. Andrew Ulrich this valve would be replaced on 3.4.19. The gatering line is fed by Keito Gas and Amtec oil gas. |
For data sources see[8]