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− | __TOC__ | + | __TOC__ |
== Well Details == | == Well Details == | ||
{| class="wikitable welldetails" width="95%" | {| class="wikitable welldetails" width="95%" | ||
| Well ID: 34-167-24312 | | Well ID: 34-167-24312 | ||
− | | style="height=100%; align=center" rowspan=" | + | | style="height=100%; align=center" rowspan="17" | {{#display_map: 39.503526426, -81.51972505 | width=100% | height=100% }} |
|- | |- | ||
− | | | + | | Country: United States |
|- | |- | ||
− | | | + | | State: Ohio |
|- | |- | ||
− | | Operator Name: [[ENERVEST OPERATING | + | | County: [[Washington_County,_Ohio|Washington]] |
+ | |- | ||
+ | | Municipality: [[Adams_Township,_Washington_County,_Ohio|Adams Township]] | ||
+ | |- | ||
+ | | Operator Name: [[ENERVEST OPERATING LLC]] | ||
|- | |- | ||
| Well Pad ID: | | Well Pad ID: | ||
|- | |- | ||
− | | Farm/Lease Name: | + | | Farm/Lease Name: LANG FRANK & RUTH |
|- | |- | ||
− | | | + | | License Status: Final Restoration |
|- | |- | ||
− | | | + | | License Date: 2014-04-03 |
|- | |- | ||
| Spud Date: 1979-01-15 | | Spud Date: 1979-01-15 | ||
|- | |- | ||
− | | | + | | Spud Drilling Contractor: |
+ | |- | ||
+ | | Final Drill Date: 1979-01-25 | ||
+ | |- | ||
+ | | Well Total Depth: 2008 ft | ||
+ | |- | ||
+ | | Configuration: Vertical | ||
+ | |- | ||
+ | | Latitude: 39.503526426 | ||
+ | |- | ||
+ | | Longitude: -81.51972505 | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Well History == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Well Status | ||
+ | !scope="col" style="width: 15%;text-align: center"| Well Status Date | ||
+ | !scope="col" style="text-align: center"| Comment | ||
+ | |- | ||
+ | | Original Spud | ||
+ | | 1979-01-15 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
+ | |- | ||
+ | | Completed | ||
+ | | 1979-01-25 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
+ | |- | ||
+ | | Reached Total Depth | ||
+ | | 1979-01-25 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
+ | |- | ||
+ | | CO | ||
+ | | 1989-08-29 | ||
+ | | 2665 TMR OPERATING CO INC | ||
+ | |- | ||
+ | | CO | ||
+ | | 1992-06-09 | ||
+ | | 4205 TRANSFUEL RESOURCES CO GeoDate | ||
+ | |- | ||
+ | | CO | ||
+ | | 1995-10-27 | ||
+ | | 213 LOMAK OPERATING CO GeoDate | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 1997-12-02 | ||
+ | | Operator changed from 213, LOMAK OPERATING CO to 3793, ENERGY SEARCH INC | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2008-02-26 | ||
+ | | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC | ||
+ | |- | ||
+ | | Change of Owner | ||
+ | | 2009-12-14 | ||
+ | | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC | ||
+ | |- | ||
+ | | APP | ||
+ | | 2014-04-03 | ||
+ | | Proposed Formations:BEREA, Issued Date:4/3/2014, Expired Date:4/2/2016 12:00:00 PM, Drilling unit acres:62, Proposed Well Type:OG, Proposed Well Class: | ||
|- | |- | ||
− | | | + | | Plugged/Abandoned |
+ | | 2015-10-12 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
|- | |- | ||
− | | | + | | Construction Permit Expires |
+ | | 2016-04-02 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
|- | |- | ||
− | | | + | | Record Last Modified |
+ | | 2017-02-17 | ||
+ | | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT | ||
|- | |- | ||
− | | | + | |} |
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Well and WellHistry Tables | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Perforation Treatments == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Perforation Date | ||
+ | !scope="col" style="text-align: center"| Interval Top (ft) | ||
+ | !scope="col" style="text-align: center"| Interval Base (ft) | ||
+ | !scope="col" style="text-align: center"| Number of Shots | ||
|- | |- | ||
− | | | + | | 2006-09-11 |
+ | | style="text-align: right;" | 1959 | ||
+ | | style="text-align: right;" | 1969 | ||
+ | | style="text-align: right;" | 1 | ||
|- | |- | ||
|} | |} | ||
− | == | + | For data sources see<ref>{{cite web |
+ | | title = Risk Based Data Management System - Perfs Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <!--== Fracking Activities == | ||
+ | ==== Fracking Jobs ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Job Start Date | ||
+ | !scope="col" style="text-align: center"| Job End Date | ||
+ | !scope="col" style="text-align: center"| True Vertical Depth (ft) | ||
+ | !scope="col" style="text-align: center"| Total Water Volume (gal) | ||
+ | !scope="col" style="text-align: center"| Total Non-Water Volume (gal) | ||
+ | |- | ||
+ | |}--> | ||
+ | <!--==== Fluid Composition Data ==== | ||
+ | {| class="wikitable sortable" style="width: 100%" | ||
+ | !scope="col" style="text-align: center"| Job Number | ||
+ | !scope="col" style="text-align: center"| Trade Name | ||
+ | !scope="col" style="text-align: center"| Supplier | ||
+ | !scope="col" style="text-align: center"| Purpose | ||
+ | !scope="col" style="text-align: center"| Ingredient Name | ||
+ | !scope="col" style="white-space: nowrap;text-align: center"| CAS Number | ||
+ | !scope="col" style="text-align: center"| Additive Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Job Percentage by Mass | ||
+ | !scope="col" style="text-align: center"| Mass Used (lb) | ||
+ | |- | ||
+ | |}--> | ||
+ | == Stimulations Data == | ||
{| class="wikitable sortable" width="95%" | {| class="wikitable sortable" width="95%" | ||
− | !scope="col" | | + | !scope="col" style="text-align: center"| Stimulation Date |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Chemical Agent |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Chemical Agent Concentration (%) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Fracking Fluid Volume |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Mass of Proppant Used (lb) |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Fracking Company |
− | !scope="col" | | + | !scope="col" style="text-align: center"| Comments |
|- | |- | ||
− | |||
− | |||
| | | | ||
+ | | H2O | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 529 Bbl | ||
+ | | style="text-align: right;" | 62500 | ||
| | | | ||
| | | | ||
− | |||
− | |||
|- | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - tblStimulation Table | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Production Data == | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Gas Quantity (mcf) | ||
+ | !scope="col" style="text-align: center"| Oil Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
+ | |- | ||
+ | | 1991 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 1992 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | style="text-align: right;" | 384 | ||
+ | | style="text-align: right;" | 133 | ||
+ | | style="text-align: right;" | 182 | ||
+ | |- | ||
+ | | 1993 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | style="text-align: right;" | 10 | ||
+ | | style="text-align: right;" | 19 | ||
+ | | style="text-align: right;" | 359 | ||
+ | |- | ||
+ | | 1995 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 270 | ||
+ | |- | ||
+ | | 2001 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 26 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2002 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2003 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2004 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2005 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
+ | |- | ||
+ | | 2006 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2007 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | |- | ||
+ | | 2008 | ||
+ | | [[EXCO - NORTH COAST ENERGY INC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 366 | ||
|- | |- | ||
− | | | + | | 2009 |
− | | style="text-align:right;" | | + | | [[EXCO - NORTH COAST ENERGY INC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 0 | |
− | | | + | | style="text-align: right;" | 0 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2010 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2011 |
− | | style="text-align:right;" | | + | | [[ENERVEST OPERATING LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 0 | |
− | | | + | | style="text-align: right;" | 0 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2012 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2013 |
− | | style="text-align:right;" | | + | | [[ENERVEST OPERATING LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 0 | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2014 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2015 |
− | | style="text-align:right;" | | + | | [[ENERVEST OPERATING LLC]] |
− | | | + | | style="text-align: right;" | 0 |
− | + | | style="text-align: right;" | 0 | |
− | | | + | | style="text-align: right;" | 67 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Oil and Gas Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Waste Data == | ||
+ | {| class="wikitable sortable" | ||
+ | !scope="col" style="text-align: center"| Period | ||
+ | !scope="col" style="text-align: center"| Operator Name | ||
+ | !scope="col" style="text-align: center"| Waste Type | ||
+ | !scope="col" style="text-align: center"| Quantity (bbl) | ||
+ | !scope="col" style="text-align: center"| Production Days | ||
|- | |- | ||
− | | | + | | 1991 |
− | | style="text-align:right;" | 0 | + | | [[TRANSFUEL RESOURCES CO]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1992 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 25 | ||
+ | | style="text-align: right;" | 182 | ||
|- | |- | ||
− | | | + | | 1993 |
− | | style="text-align:right;" | | + | | [[TRANSFUEL RESOURCES CO]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 48 | |
− | + | | style="text-align: right;" | 359 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 1995 | ||
+ | | [[TRANSFUEL RESOURCES CO]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 270 | ||
|- | |- | ||
− | | | + | | 2001 |
− | | style="text-align:right;" | 0 | + | | [[ENERGY SEARCH INC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2002 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2003 |
− | | style="text-align:right;" | + | | [[ENERGY SEARCH INC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | | |
− | | | + | | style="text-align: right;" | 365 |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2004 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 365 | ||
|- | |- | ||
− | | | + | | 2005 |
− | | style="text-align:right;" | 0 | + | | [[ENERGY SEARCH INC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2006 | ||
+ | | [[ENERGY SEARCH INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | 2007 | + | | 2007 |
− | | style="text-align:right;" | 0 | + | | [[ENERGY SEARCH INC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 0 | |
− | | style="text-align:right;" | 0 | ||
− | |||
|- | |- | ||
+ | | 2008 | ||
+ | | [[EXCO - NORTH COAST ENERGY INC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 366 | ||
|- | |- | ||
− | | | + | | 2009 |
− | | style="text-align:right;" | 0 | + | | [[EXCO - NORTH COAST ENERGY INC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 0 | |
− | | style="text-align:right;" | 0 | ||
− | |||
|- | |- | ||
+ | | 2010 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2011 |
− | | style="text-align:right;" | 0 | + | | [[ENERVEST OPERATING LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | | |
− | | style="text-align:right;" | ||
− | | | ||
|- | |- | ||
+ | | 2012 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2013 |
− | | style="text-align:right;" | 0 | + | | [[ENERVEST OPERATING LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 365 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | | 2014 | ||
+ | | [[ENERVEST OPERATING LLC]] | ||
+ | | Brine | ||
+ | | style="text-align: right;" | 0 | ||
+ | | style="text-align: right;" | 0 | ||
|- | |- | ||
− | | | + | | 2015 |
− | | style="text-align:right;" | 0 | + | | [[ENERVEST OPERATING LLC]] |
− | + | | Brine | |
− | + | | style="text-align: right;" | 0 | |
− | + | | style="text-align: right;" | 67 | |
− | | style="text-align:right;" | | ||
− | |||
|- | |- | ||
+ | |} | ||
+ | For data sources see<ref>{{cite web | ||
+ | | title = Risk Based Data Management System - Production Table - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | <ref>{{cite web | ||
+ | | title = Combined Production - Brine Data | ||
+ | |publisher = [[Ohio Department of Natural Resources]] | ||
+ | | date = 2019-05-07 | ||
+ | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | ||
+ | | accessdate = 2019-05-21 }}</ref> | ||
+ | == Inspection Data == | ||
+ | ==== Inspections Performed ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Inspection Date | ||
+ | !scope="col" style="text-align: center"| Inspection Type | ||
+ | !scope="col" style="text-align: center"| Inspection Result | ||
+ | !scope="col" style="text-align: center"| Inspection Comments | ||
|- | |- | ||
− | | | + | | 0743465964 |
− | | | + | | 2015-10-08 |
− | | | + | | Plug / Plug Back |
− | | | + | | No Violations |
− | | | + | | On location to witness blowdown of this well in preparation for plugging activities. Knox Energys service rig is standing over the well. There is a 2 kelly hose leading from the valve on the 3.5-2 swedge to a half round tank. The well was blown down from 160 psi and flowed approximately 30 bbls of oil into the half round during the blowdown process before going static. The bottom plug for this well will be bullheaded down on 10/9/2015. |
− | |||
− | |||
|- | |- | ||
+ | | 0847640572 | ||
+ | | 2015-10-01 | ||
+ | | Production Wells | ||
+ | | No Violations | ||
+ | | Received call from Tim Mitten from Knox Energy in regard to the location of this well. Inspector Brian Sefcik and I met with Mr. Mitten on Lang Ridge Rd. to show him where this well is. Knox Energy will be moving a service rig onto this location tomorrow to plug and abandon the well. The visible casing consists of 3.5 production casing with a 3.5-2 swedge. Plugging activities will commence for the well early next week. | ||
|- | |- | ||
− | | | + | | 1659345021 |
− | | | + | | 2015-10-09 |
− | | | + | | Plug / Plug Back |
− | | | + | | No Violations |
− | | | + | | On location to witness plugging operations for this well. Cemenco Services is the cement contractor for this job. A 725 bottom plug was bullheaded down the 3.5 casing using 30 sks class A cement, 20 lbs LCM, and 10.5 bbls of freshwater displacement. The well was shut in after bullheading the plug down to lock it in place and prevent it from migrating uphole. Completion records for the well indicate that the production casing was cemented back to surface, however cement cannot be seen on the 3.5-8.625 annulus. Appalachian Well Surveys will be on location on 10/12/2015 to run a cement bond log to verify cement top and will shoot casing off at free point. |
− | |||
− | |||
|- | |- | ||
+ | | 1688050835 | ||
+ | | 2015-10-13 | ||
+ | | Plug / Plug Back | ||
+ | | No Violations | ||
+ | | This well is now plugged and abandoned. On location to verify cement top and witness installation of ID plate on the 8.625 casing. Cement is present approximately 18 from the top of the casing. Knox Energy was on location removing production equipment and flow lines in preparation for performing final restoration activities. | ||
|- | |- | ||
− | | | + | | 1719763096 |
− | | | + | | 2016-05-24 |
− | + | | Final Restoration | |
− | | | + | | No Violations |
− | | | + | | The purpose of my inspection today is a status check on a final restoration. During my inspection I witnessed no evidence of an oil and gas well and the site has been restored. Location has met 1509.072 B requirements. |
− | | | ||
− | |||
|- | |- | ||
|} | |} | ||
+ | <!--==== Violations Commited ==== | ||
+ | {| class="wikitable sortable" width="95%" | ||
+ | !scope="col" style="text-align: center"| Inspection ID | ||
+ | !scope="col" style="text-align: center"| Violation ID | ||
+ | !scope="col" style="text-align: center"| Violation Date | ||
+ | !scope="col" style="text-align: center"| Violation Code | ||
+ | !scope="col" style="text-align: center"| Violation Comments | ||
+ | |- | ||
+ | |}--> | ||
For data sources see<ref>{{cite web | For data sources see<ref>{{cite web | ||
− | | title = | + | | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables |
− | | publisher = [ | + | |publisher = [[Ohio Department of Natural Resources]] |
− | | date = | + | | date = 2019-05-07 |
− | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources | + | | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources |
− | | accessdate = | + | | accessdate = 2019-05-21 }}</ref> |
− | == References == | + | ==References== |
− | + | <references/> | |
__NOEDITSECTION__ | __NOEDITSECTION__ | ||
− | [[Category:Wells]] | + | [[Category:Ohio Wells]] |
Well ID: 34-167-24312 | Loading map...
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Country: United States | |
State: Ohio | |
County: Washington | |
Municipality: Adams Township | |
Operator Name: ENERVEST OPERATING LLC | |
Well Pad ID: | |
Farm/Lease Name: LANG FRANK & RUTH | |
License Status: Final Restoration | |
License Date: 2014-04-03 | |
Spud Date: 1979-01-15 | |
Spud Drilling Contractor: | |
Final Drill Date: 1979-01-25 | |
Well Total Depth: 2008 ft | |
Configuration: Vertical | |
Latitude: 39.503526426 | |
Longitude: -81.51972505 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Original Spud | 1979-01-15 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
Completed | 1979-01-25 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
Reached Total Depth | 1979-01-25 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
CO | 1989-08-29 | 2665 TMR OPERATING CO INC |
CO | 1992-06-09 | 4205 TRANSFUEL RESOURCES CO GeoDate |
CO | 1995-10-27 | 213 LOMAK OPERATING CO GeoDate |
Change of Owner | 1997-12-02 | Operator changed from 213, LOMAK OPERATING CO to 3793, ENERGY SEARCH INC |
Change of Owner | 2008-02-26 | Operator changed from 3793, ENERGY SEARCH INC to 1388, NORTH COAST ENERGY INC |
Change of Owner | 2009-12-14 | Operator changed from 1388, EXCO - NORTH COAST ENERGY INC to 7578, ENERVEST OPERATING LLC |
APP | 2014-04-03 | Proposed Formations:BEREA, Issued Date:4/3/2014, Expired Date:4/2/2016 12:00:00 PM, Drilling unit acres:62, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2015-10-12 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
Construction Permit Expires | 2016-04-02 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
Record Last Modified | 2017-02-17 | GMM WAS WAS CHANGED TO PA STATUS BASED ON PLUG REPORT |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2006-09-11 | 1959 | 1969 | 1 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 529 Bbl | 62500 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | TRANSFUEL RESOURCES CO | 0 | 0 | 365 |
1992 | TRANSFUEL RESOURCES CO | 384 | 133 | 182 |
1993 | TRANSFUEL RESOURCES CO | 10 | 19 | 359 |
1995 | TRANSFUEL RESOURCES CO | 0 | 0 | 270 |
2001 | ENERGY SEARCH INC | 26 | 0 | 365 |
2002 | ENERGY SEARCH INC | 0 | 0 | 365 |
2003 | ENERGY SEARCH INC | 0 | 0 | 365 |
2004 | ENERGY SEARCH INC | 0 | 0 | 365 |
2005 | ENERGY SEARCH INC | 0 | 0 | 365 |
2006 | ENERGY SEARCH INC | 0 | 0 | 0 |
2007 | ENERGY SEARCH INC | 0 | 0 | 0 |
2008 | EXCO - NORTH COAST ENERGY INC | 0 | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | 0 | 0 | 0 |
2010 | ENERVEST OPERATING LLC | 0 | 0 | 0 |
2011 | ENERVEST OPERATING LLC | 0 | 0 | 0 |
2012 | ENERVEST OPERATING LLC | 0 | 0 | 0 |
2013 | ENERVEST OPERATING LLC | 0 | 0 | 365 |
2014 | ENERVEST OPERATING LLC | 0 | 0 | 0 |
2015 | ENERVEST OPERATING LLC | 0 | 0 | 67 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | TRANSFUEL RESOURCES CO | Brine | 0 | 365 |
1992 | TRANSFUEL RESOURCES CO | Brine | 25 | 182 |
1993 | TRANSFUEL RESOURCES CO | Brine | 48 | 359 |
1995 | TRANSFUEL RESOURCES CO | Brine | 0 | 270 |
2001 | ENERGY SEARCH INC | Brine | 0 | 365 |
2002 | ENERGY SEARCH INC | Brine | 365 | |
2003 | ENERGY SEARCH INC | Brine | 365 | |
2004 | ENERGY SEARCH INC | Brine | 0 | 365 |
2005 | ENERGY SEARCH INC | Brine | 0 | 365 |
2006 | ENERGY SEARCH INC | Brine | 0 | 0 |
2007 | ENERGY SEARCH INC | Brine | 0 | 0 |
2008 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 366 |
2009 | EXCO - NORTH COAST ENERGY INC | Brine | 0 | 0 |
2010 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2011 | ENERVEST OPERATING LLC | Brine | 0 | |
2012 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2013 | ENERVEST OPERATING LLC | Brine | 0 | 365 |
2014 | ENERVEST OPERATING LLC | Brine | 0 | 0 |
2015 | ENERVEST OPERATING LLC | Brine | 0 | 67 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0743465964 | 2015-10-08 | Plug / Plug Back | No Violations | On location to witness blowdown of this well in preparation for plugging activities. Knox Energys service rig is standing over the well. There is a 2 kelly hose leading from the valve on the 3.5-2 swedge to a half round tank. The well was blown down from 160 psi and flowed approximately 30 bbls of oil into the half round during the blowdown process before going static. The bottom plug for this well will be bullheaded down on 10/9/2015. |
0847640572 | 2015-10-01 | Production Wells | No Violations | Received call from Tim Mitten from Knox Energy in regard to the location of this well. Inspector Brian Sefcik and I met with Mr. Mitten on Lang Ridge Rd. to show him where this well is. Knox Energy will be moving a service rig onto this location tomorrow to plug and abandon the well. The visible casing consists of 3.5 production casing with a 3.5-2 swedge. Plugging activities will commence for the well early next week. |
1659345021 | 2015-10-09 | Plug / Plug Back | No Violations | On location to witness plugging operations for this well. Cemenco Services is the cement contractor for this job. A 725 bottom plug was bullheaded down the 3.5 casing using 30 sks class A cement, 20 lbs LCM, and 10.5 bbls of freshwater displacement. The well was shut in after bullheading the plug down to lock it in place and prevent it from migrating uphole. Completion records for the well indicate that the production casing was cemented back to surface, however cement cannot be seen on the 3.5-8.625 annulus. Appalachian Well Surveys will be on location on 10/12/2015 to run a cement bond log to verify cement top and will shoot casing off at free point. |
1688050835 | 2015-10-13 | Plug / Plug Back | No Violations | This well is now plugged and abandoned. On location to verify cement top and witness installation of ID plate on the 8.625 casing. Cement is present approximately 18 from the top of the casing. Knox Energy was on location removing production equipment and flow lines in preparation for performing final restoration activities. |
1719763096 | 2016-05-24 | Final Restoration | No Violations | The purpose of my inspection today is a status check on a final restoration. During my inspection I witnessed no evidence of an oil and gas well and the site has been restored. Location has met 1509.072 B requirements. |
For data sources see[9]