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| License Status: Producing | | License Status: Producing | ||
|- | |- | ||
− | | License Date: | + | | License Date: 2001-12-03 |
|- | |- | ||
| Spud Date: 2002-01-03 | | Spud Date: 2002-01-03 |
Well ID: 34-101-20208 | Loading map...
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Country: United States | |
State: Ohio | |
County: Marion | |
Municipality: Grand Township | |
Operator Name: MAR OIL COMPANY | |
Well Pad ID: | |
Farm/Lease Name: ROSZMAN | |
License Status: Producing | |
License Date: 2001-12-03 | |
Spud Date: 2002-01-03 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2002-01-08 | |
Well Total Depth: 1982 ft | |
Configuration: Vertical | |
Latitude: 40.671383631 | |
Longitude: -83.38877756 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2001-12-03 | Proposed Formations:TRENTON - TREMPEALEAU, Issued Date:12/3/2001, Expired Date:12/3/2002 6:00:00 AM, Drilling unit acres:60, Proposed Well Type:OG, Proposed Well Class:EW |
Original Spud | 2002-01-03 | |
Completed | 2002-01-08 | |
Reached Total Depth | 2002-01-08 | |
Completion Report Received | 2002-06-11 | |
Correction to Well | 2002-06-21 | DRILL UNIT SIZE REDUCED TO 58.224 ACRES; X COORDINATE CHANGED TO 1,753,460 AND Y COORDINATE CHANGED TO 367,292. |
Construction Permit Expires | 2002-12-03 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
ACID | 15 | 6750 Gal | 0 |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2002 | MAR OIL COMPANY | 0 | 2528 | 259 |
2003 | MAR OIL COMPANY | 0 | 2012 | 365 |
2004 | MAR OIL COMPANY | 0 | 1193 | 270 |
2005 | MAR OIL COMPANY | 0 | 1042 | 295 |
2006 | MAR OIL COMPANY | 0 | 848 | 305 |
2007 | MAR OIL COMPANY | 0 | 728 | 330 |
2009 | MAR OIL COMPANY | 0 | 138 | 76 |
2010 | MAR OIL COMPANY | 0 | 622 | 200 |
2011 | MAR OIL COMPANY | 0 | 301 | 150 |
2012 | MAR OIL COMPANY | 0 | 571 | 280 |
2013 | MAR OIL COMPANY | 0 | 163 | 320 |
2014 | MAR OIL COMPANY | 0 | 0 | 0 |
2015 | MAR OIL COMPANY | 0 | 0 | 0 |
2016 | MAR OIL COMPANY | 0 | 1 | 1 |
2017 | MAR OIL COMPANY | 0 | 26 | 1 |
2018 | MAR OIL COMPANY | 0 | 120 | 1 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2002 | MAR OIL COMPANY | Brine | 1966 | 259 |
2003 | MAR OIL COMPANY | Brine | 1630 | 365 |
2004 | MAR OIL COMPANY | Brine | 1500 | 270 |
2005 | MAR OIL COMPANY | Brine | 1545 | 295 |
2006 | MAR OIL COMPANY | Brine | 2016 | 305 |
2007 | MAR OIL COMPANY | Brine | 1191 | 330 |
2009 | MAR OIL COMPANY | Brine | 546 | 76 |
2010 | MAR OIL COMPANY | Brine | 702 | 200 |
2011 | MAR OIL COMPANY | Brine | 1122 | 150 |
2012 | MAR OIL COMPANY | Brine | 670 | 280 |
2013 | MAR OIL COMPANY | Brine | 218 | 320 |
2014 | MAR OIL COMPANY | Brine | 0 | 0 |
2015 | MAR OIL COMPANY | Brine | 0 | 0 |
2016 | MAR OIL COMPANY | Brine | 13 | 1 |
2017 | MAR OIL COMPANY | Brine | 10 | 1 |
2018 | MAR OIL COMPANY | Brine | 110 | 1 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0014173572 | 2002-01-04 | Drill / Deepen / Reopen | No Violations | Drilling at 320, talk to toolpusher he said it will be about 5 hrs before they are ready to cement the surface casing. |
0026273662 | 2002-06-06 | Production Wells | No Violations | Chk well and storage OK. Preleminary restoration started, vegitative cover established. Trees, brush and stumps still on site. ( Not due yet.) |
0061358447 | 2012-11-01 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as a standard productive well status check. The well is pumping by a Alten gas powered pump jack and the well pad is clean and free of excess contamination. The storage consists of two tanks and a horizontal steel brine tank set in a gravel dike. The well identification and emergency contact information is marked at the pump jack. Status Ok. |
0074703140 | 2013-09-10 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard productive well status check. Check well, storage and identification. No change in status from previous inspection. Status: ok. |
0187214670 | 2014-09-15 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. |
0283941776 | 2017-11-21 | Production Wells | No Violations | Recent activity at the wellsite as the rods are pulled and stacked on a trailer next to the well. |
0288862493 | 2013-11-15 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard productive well status check. Check well, storage and identification, no change in status from previous inspection. Status: ok. |
0379257762 | 2008-07-01 | Production Wells | No Violations | Chk well and storage, Ok. |
0683337792 | 2018-06-15 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection. |
0720488076 | 2014-07-28 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. |
0776129561 | 2015-08-14 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: no change-in-status from previous inspection. |
0954907242 | 2006-01-17 | Production Wells | No Violations | Inspect Well. Pump jack running and flair. Four 210 bbl tanks. |
1023000954 | 2018-11-08 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection. |
1047657572 | 2003-03-14 | Preliminary Restoration | No Violations | Preliminary restoration done. |
1050341827 | 2003-04-14 | Preliminary Restoration | No Violations | Chk well and storage, Preliminary restoration done. |
1091024272 | 2004-07-28 | Preliminary Restoration | No Violations | Preliminary restoration done. The well is equipped to produce at this time. |
1110032897 | 2016-03-07 | Production Wells | No Violations | Inspect well and storage. No change-in-status from previous inspection. |
1127405062 | 2005-09-22 | Production Wells | No Violations | Chk well and storage, Ok. |
1137692977 | 2006-01-19 | Production Wells | No Violations | Chk well and storage, Ok. |
1224522682 | 2008-10-20 | Production Wells | No Violations | On site to chk report of a fatal accident. On 10-19-08 two men were attempting to weld a bracket to the side of a 210bbl storage tank. The tank was half full of oil and when one of the men struck an arc with the welder the vapors in the tank ignited. Causing the tank to explode. the explosion ripped the top almost off of the tank. The tank immediately to the west (empty of fluid) exploded also ripping the top off of it and sending it (the top) approx 300 foot to the north into the woods. A neighbor came to the site immediately after the first explosion and witnessed the second explosion as he made a failed attempt to remove one of the victims from the resulting fire.
Both men died from the explosions. |
1297662916 | 2014-09-08 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. |
1325155509 | 2018-02-12 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: no change-in-status from previous inspection. |
1453650002 | 2015-04-28 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. |
1587522198 | 2018-10-04 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. The well was pumping at the time of inspection. |
1600731243 | 2013-05-20 | Production Wells | No Violations | Check production well, storage and identification. The well is pumping. No Trespassing signs have been added at the entrance. Status: compliant. |
1906217802 | 2019-04-18 | Production Wells | No Violations | Inspected the Roszman #1 (#208) as part of a standard production well status check. Inspect well, storage and identification. Status: ok. |
1971093875 | 2014-09-08 | Production Wells | No Violations | Location Information for the Roszman #1 (#208). ENTRANCE: Lat. 40.67259 Long. -83.38927 / WELL HEAD: Lat. 40.67139 Long. -83.38875 / CENTER-OF-STORAGE: Lat. 40.67155 Long. -83.38873. |
1981271297 | 2009-02-18 | Production Wells | No Violations | Chk well and storage, the tanks that were damaged in the explosion have not been changed out yet. The site still has yellow ribbon at the entrance to the lease road. Gate is closed, not in production at this time. |
2075421393 | 2016-02-16 | Production Wells | No Violations | Inspect well and storage. Status: no change-in-status from previous inspection. |
2077525190 | 2015-02-19 | Production Wells | No Violations | The Roszman #1 is shut-in. |
For data sources see[8]