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| License Status: Final Restoration | | License Status: Final Restoration | ||
|- | |- | ||
− | | License Date: 2017- | + | | License Date: 2017-04-05 |
|- | |- | ||
| Spud Date: 2017-06-02 | | Spud Date: 2017-06-02 |
Well ID: 34-075-24946 | Loading map...
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Country: United States | |
State: Ohio | |
County: Holmes | |
Municipality: Mechanic Township | |
Operator Name: TATUM PETROLEUM CO LLC | |
Well Pad ID: | |
Farm/Lease Name: ERB | |
License Status: Final Restoration | |
License Date: 2017-04-05 | |
Spud Date: 2017-06-02 | |
Spud Drilling Contractor: G & H DRLG | |
Final Drill Date: 2017-06-02 | |
Well Total Depth: 5980 ft | |
Configuration: Vertical | |
Latitude: 40.482529150 | |
Longitude: -81.87882741 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1990-10-11 | Issued Date 10/11/90 Expired Date 10/11/91 Acres 0160000 Tool Type RTA Proposed Formation ROSE RUN Proposed Depth 05980 Proposed Drill Depth 05980 |
Original Spud | 1990-11-02 | |
Completed | 1990-11-19 | |
CO | 1990-12-17 | 2547 TATUM PETROLEUM CORP GeoDate 10/11/90 |
Change of Owner | 2005-09-19 | Operator changed from 2547, TATUM PETROLEUM CORP to 7912, TATUM PETROLEUM CO LLC |
APP | 2017-04-05 | Proposed Formations:ROSE RUN, Issued Date:4/5/2017, Expired Date:4/5/2019 12:00:00 PM, Drilling unit acres:80, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2017-06-02 | |
Plugged/Abandoned | 2017-06-07 | |
Completion Report Received | 2017-06-15 | |
Record Last Modified | 2018-12-21 | |
Construction Permit Expires | 2019-04-05 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5950 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | NOT TREATED |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1991 | TATUM PETROLEUM CORP | 45447 | 247 | 311 |
1992 | TATUM PETROLEUM CORP | 18658 | 63 | 352 |
1993 | TATUM PETROLEUM CORP | 30080 | 7 | 334 |
1994 | TATUM PETROLEUM CORP | 24320 | 0 | 365 |
1995 | TATUM PETROLEUM CORP | 13817 | 0 | 365 |
1996 | TATUM PETROLEUM CORP | 12247 | 0 | 365 |
1997 | TATUM PETROLEUM CORP | 10953 | 0 | 364 |
1998 | TATUM PETROLEUM CORP | 9987 | 0 | 330 |
1999 | TATUM PETROLEUM CORP | 6081 | 0 | 365 |
2000 | TATUM PETROLEUM CORP | 6118 | 0 | 348 |
2001 | TATUM PETROLEUM CORP | 3993 | 0 | 365 |
2002 | TATUM PETROLEUM CORP | 38741 | 1081 | 365 |
2003 | TATUM PETROLEUM CORP | 33831 | 660 | 365 |
2004 | TATUM PETROLEUM CORP | 16645 | 476 | 365 |
2005 | TATUM PETROLEUM CORP | 3621 | 89 | 273 |
2006 | TATUM PETROLEUM CO LLC | 12956 | 392 | 365 |
2007 | TATUM PETROLEUM CO LLC | 11219 | 341 | 365 |
2008 | TATUM PETROLEUM CO LLC | 10681 | 604 | 333 |
2009 | TATUM PETROLEUM CO LLC | 6300 | 367 | 364 |
2010 | TATUM PETROLEUM CO LLC | 4422 | 346 | 365 |
2011 | TATUM PETROLEUM CO LLC | 2440 | 0 | 365 |
2012 | TATUM PETROLEUM CO LLC | 826 | 141 | 366 |
2013 | TATUM PETROLEUM CO LLC | 848 | 0 | 365 |
2014 | TATUM PETROLEUM CO LLC | 1857 | 19 | 346 |
2015 | TATUM PETROLEUM CO LLC | 2581 | 0 | 365 |
2016 | TATUM PETROLEUM CO LLC | 370 | 0 | 365 |
2017 | TATUM PETROLEUM CO LLC | 249 | 23 | 220 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL14971 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0056502763 | 2017-07-27 | Final Restoration | No Violations | Still no activity at the well for final reclamation. |
0443384790 | 2011-08-02 | Production Wells | No Violations | ID affixed as requested. |
1172642209 | 2015-09-02 | Production Wells | No Violations | This is a producing plunger lift well. There were no problems noted at the time of the inspection. |
1241139362 | 2017-06-01 | Drill / Deepen / Reopen | No Violations | Rigged up the power swivel and pump truck and started circulating to bottom. Tagged bottom at 6013 and drilled to 6019 and the well started taking fluid. Shut down and shut the well in. Rigged down the power swivel and pump truck. |
1473445897 | 2016-09-07 | Production Wells | No Violations | This is a producing swab well. There were no problems noted at the time of the inspection. |
1481593034 | 2017-06-05 | Drill / Deepen / Reopen | No Violations | The well was deepened but the new zone was dry or depleted. The well will be plugged. |
1485849684 | 2017-09-01 | Final Restoration | No Violations | Final restoration is passed. |
1496401648 | 2017-05-30 | Drill / Deepen / Reopen | No Violations | The service rig is pulling the tubing to remove the mud anchor and seating nipple. They will afix a bit and run back in the hole. |
1496919898 | 2017-06-07 | Plug / Plug Back | No Violations | The fluid level was at ~170 indicating that the plugged interval took fluid and cement after the diplacement of the bottom plug was shut down 2 bbls early because of high pressure. The tools sat down at 5269 . Whether because the knife sat down on a collar or there was a ring of cement there is impossible to tell. The casing was ripped at 3841 (first telegraph) and one joint was pulled and then the Clinton/rip plug was set thru the casing. The balance of the well was plugged out without incident this date. See the plugging report for the details. |
1500983139 | 2017-07-24 | Final Restoration | No Violations | |
1694763747 | 2011-07-18 | Production Wells | No Violations | Producing, no ID. No other problems noted. Called for ID. |
1844160340 | 2014-08-04 | Production Wells | No Violations | This is a producing plunger lift well. There were no problems noted at the time of the inspection. |
1881726965 | 2013-07-01 | Production Wells | No Violations | This is a producing automatic swab well. There were no problems noted at the time of the inspection. |
1996050557 | 2017-06-06 | Plug / Plug Back | No Violations | On location to witness the setting of the bottom cement plug on this well. Formation cementing bullheaded this 30 sack plug from 6020 to 5605. Displacement was stopped 2 bbls early (1000 psig) and the well continued to take fluid very slowly on vacuum. |
For data sources see[9]