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Difference between revisions of "34-143-60219"

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__TOC__
+
__TOC__
 
== Well Details ==
 
== Well Details ==
 
{| class="wikitable welldetails" width="95%"
 
{| class="wikitable welldetails" width="95%"
 
| Well ID: 34-143-60219
 
| Well ID: 34-143-60219
| style="height=100%; align=center" rowspan="15" | {{#display_map: 41.29422733, -83.38780397 | width=100% | height=100% }}  
+
| style="height=100%; align=center" rowspan="17" | {{#display_map: 41.297058326, -83.38605855 | width=100% | height=100% }}
 
|-
 
|-
| County: [[Sandusky County, Ohio|Sandusky]]
+
| Country: United States
 
|-
 
|-
| Municipality:  
+
| State: Ohio
 +
|-
 +
| County: [[Sandusky_County,_Ohio|Sandusky]]
 +
|-
 +
| Municipality: [[Scott_Township,_Sandusky_County,_Ohio|Scott Township]]
 
|-
 
|-
 
| Operator Name: [[ORPHAN WELL PROGRAM]]
 
| Operator Name: [[ORPHAN WELL PROGRAM]]
Line 13: Line 17:
 
| Well Pad ID:  
 
| Well Pad ID:  
 
|-
 
|-
| Farm/Lease Name:  
+
| Farm/Lease Name: SAUTTER TIM (BRINKERHOFF)
 
|-
 
|-
| First Permit Date:  
+
| License Status: Final Restoration
 
|-
 
|-
| Last Permit Date:  
+
| License Date: 2012-10-26
 
|-
 
|-
 
| Spud Date:  
 
| Spud Date:  
 
|-
 
|-
| Unconventional: No
+
| Spud Drilling Contractor:
 +
|-
 +
| Final Drill Date:
 +
|-
 +
| Well Total Depth:  
 
|-
 
|-
 
| Configuration: Vertical
 
| Configuration: Vertical
 
|-
 
|-
| Well Status: Final Restoration
+
| Latitude: 41.297058326
 
|-
 
|-
| Violations: 0
+
| Longitude: -83.38605855
 +
|}
 +
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well, tblLocational, tblPlugWell, tblInspection, tblCivilTownships and tblPad Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
== Well History ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Well Status
 +
!scope="col" style="width: 15%;text-align: center"| Well Status Date
 +
!scope="col" style="text-align: center"| Comment
 
|-
 
|-
| Latitude: 41.29422733
+
| Well Added to System
 +
| 2007-10-17
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" &  7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
| Longitude: -83.38780397
+
| Change of Owner
 +
| 2012-10-18
 +
| Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
 +
|-
 +
| APP
 +
| 2012-10-26
 +
| Proposed Formations:, Issued Date:10/26/2012, Expired Date:10/26/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
 +
|-
 +
| Plugged by Orphan Well Program
 +
| 2013-05-06
 +
| Plugged by Orphan Well Program
 +
|-
 +
| Plugged/Abandoned
 +
| 2013-05-06
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" &  7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 +
|-
 +
| Construction Permit Expires
 +
| 2014-10-26
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" &  7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 +
|-
 +
| Record Last Modified
 +
| 2019-06-14
 +
| NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL  HAS 10" &  7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
 
|-
 
|-
 
|}
 
|}
== Inspection Data ==
+
For data sources see<ref>{{cite web
 +
| title = Risk Based Data Management System - Well and WellHistry Tables
 +
|publisher = [[Ohio Department of Natural Resources]]
 +
| date =  2019-05-07
 +
| url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
 +
| accessdate = 2019-05-21 }}</ref>
 +
<!--== Perforation Treatments ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Perforation Date
 +
!scope="col" style="text-align: center"| Interval Top (ft)
 +
!scope="col" style="text-align: center"| Interval Base (ft)
 +
!scope="col" style="text-align: center"| Number of Shots
 +
|-
 +
|}-->
 +
<!--== Fracking Activities ==
 +
==== Fracking Jobs ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Job Start Date
 +
!scope="col" style="text-align: center"| Job End Date
 +
!scope="col" style="text-align: center"| True Vertical Depth (ft)
 +
!scope="col" style="text-align: center"| Total Water Volume (gal)
 +
!scope="col" style="text-align: center"| Total Non-Water Volume (gal)
 +
|-
 +
|}-->
 +
<!--==== Fluid Composition Data ====
 +
{| class="wikitable sortable" style="width: 100%"
 +
!scope="col" style="text-align: center"| Job Number
 +
!scope="col" style="text-align: center"| Trade Name
 +
!scope="col" style="text-align: center"| Supplier
 +
!scope="col" style="text-align: center"| Purpose
 +
!scope="col" style="text-align: center"| Ingredient Name
 +
!scope="col" style="white-space: nowrap;text-align: center"| CAS Number
 +
!scope="col" style="text-align: center"| Additive Percentage by Mass
 +
!scope="col" style="text-align: center"| Job Percentage by Mass
 +
!scope="col" style="text-align: center"| Mass Used (lb)
 +
|-
 +
|}-->
 +
<!--== Stimulations Data ==
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Stimulation Date
 +
!scope="col" style="text-align: center"| Chemical Agent
 +
!scope="col" style="text-align: center"| Chemical Agent Concentration (%)
 +
!scope="col" style="text-align: center"| Fracking Fluid Volume
 +
!scope="col" style="text-align: center"| Mass of Proppant Used (lb)
 +
!scope="col" style="text-align: center"| Fracking Company
 +
!scope="col" style="text-align: center"| Comments
 +
|-
 +
|}-->
 +
<!--== Production Data ==
 
{| class="wikitable sortable" width="95%"
 
{| class="wikitable sortable" width="95%"
!scope="col" | INSPECTION ID
+
!scope="col" style="text-align: center"| Period
!scope="col" | DATE
+
!scope="col" style="text-align: center"| Operator Name
!scope="col" | DESCRIPTION
+
!scope="col" style="text-align: center"| Gas Quantity (mcf)
!scope="col" | COMMENT
+
!scope="col" style="text-align: center"| Oil Quantity (bbl)
!scope="col" | VIOLATION ID
+
!scope="col" style="text-align: center"| Production Days
!scope="col" | VIOLATION CODE
 
!scope="col" | VIOLATION COMMENT
 
 
|-
 
|-
| 1290545113
+
|}-->
| 2013-05-07
+
<!--== Waste Data ==
|  
+
{| class="wikitable sortable"
| An inspection of the wellbore revealed the presence of an identification plate and no visible signs of leakage at the surface.  The cement had settled from surface and will be topped off by the contractor.
+
!scope="col" style="text-align: center"| Period
|  
+
!scope="col" style="text-align: center"| Operator Name
|  
+
!scope="col" style="text-align: center"| Waste Type
|  
+
!scope="col" style="text-align: center"| Quantity (bbl)
 +
!scope="col" style="text-align: center"| Production Days
 
|-
 
|-
 +
|}-->
 +
== Inspection Data ==
 +
==== Inspections Performed ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Inspection Date
 +
!scope="col" style="text-align: center"| Inspection Type
 +
!scope="col" style="text-align: center"| Inspection Result
 +
!scope="col" style="text-align: center"| Inspection Comments
 
|-
 
|-
| 131233671
+
| 0131233671
 
| 2013-05-16
 
| 2013-05-16
|  
+
| Final Restoration
 +
| No Violations
 
| At the time of the inspection the area had been graded back for farm use by the plugging contractor. The site is currently being planted by the landowner. Final Restoration Passed.
 
| At the time of the inspection the area had been graded back for farm use by the plugging contractor. The site is currently being planted by the landowner. Final Restoration Passed.
|
 
|
 
|
 
 
|-
 
|-
 +
| 0491189008
 +
| 2013-04-25
 +
| Plug / Plug Back
 +
| No Violations
 +
| At the time of the inspection there was no activity on site and the well is static, waiting to be plugged.
 +
|-
 +
| 0548853871
 +
| 2013-07-16
 +
| Final Restoration
 +
| No Violations
 +
| An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072.  The well site was situated on a location designated as agricultural field.  An interview conducted with the landowner, Mr. Tim Sautter, at his residence confirmed that he was satisfied with the restoration of the property to include wells located within field crop.
 +
|-
 +
| 0550989745
 +
| 2012-11-27
 +
| Orphan
 +
| No Violations
 +
| At the time of my inspection there was no activity on site but a steel tank had been placed on site in preperation of the plugging of the well.
 +
|-
 +
| 0973224100
 +
| 2013-01-07
 +
| Orphan
 +
| No Violations
 +
| At the time of my inspection there was no activity but a new rig was brought on site and set up on the well over the weekend. Fishing started around 4 pm according to Tony Kryder of Second Oil Lt.
 
|-
 
|-
| -1332211534
+
| 0992569367
 +
| 2012-12-17
 +
| Orphan
 +
| No Violations
 +
| At the time of my inspection there was no activity on site and the contractor indicated there would be no activity till after the New Year.
 +
|-
 +
| 1290545113
 +
| 2013-05-07
 +
| Plug / Plug Back
 +
| No Violations
 +
| An inspection of the wellbore revealed the presence of an identification plate and no visible signs of leakage at the surface.  The cement had settled from surface and will be topped off by the contractor.
 +
|-
 +
| 1332211534
 
| 2012-12-11
 
| 2012-12-11
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection fishing with an overshot had begun at 8:30 am with an overshot tool. The tubing was grabbed at 9:00 am and attempts to get the tubing to move continued until 10:30 am with almost no progress. The decision was made to leave tension on the tubing overnight for a total of 2 hours of fishing time.
 
| At the time of my inspection fishing with an overshot had begun at 8:30 am with an overshot tool. The tubing was grabbed at 9:00 am and attempts to get the tubing to move continued until 10:30 am with almost no progress. The decision was made to leave tension on the tubing overnight for a total of 2 hours of fishing time.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1332957289
 
| 1332957289
 
| 2012-03-27
 
| 2012-03-27
|  
+
| Orphan
 +
| No Violations
 
| Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing broken below collar at casing head ring. Rods still inside tubing and bent 15 degrees to the west. Small pile of rocks and debris around wellhead. No sign of fluids leaking from well.
 
| Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing broken below collar at casing head ring. Rods still inside tubing and bent 15 degrees to the west. Small pile of rocks and debris around wellhead. No sign of fluids leaking from well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1334766134
 
| 1334766134
 
| 2013-01-29
 
| 2013-01-29
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection there was no activity on site.
 
| At the time of my inspection there was no activity on site.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1360260921
 
| 1360260921
 
| 2013-01-02
 
| 2013-01-02
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection the contractor was making an attempt to fish out the tubing but issues with the rig prevented any work.
 
| At the time of my inspection the contractor was making an attempt to fish out the tubing but issues with the rig prevented any work.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1367863934
 
| 1367863934
 
| 2013-05-06
 
| 2013-05-06
|  
+
| Orphan
| At the time of the inspection the well was bailed clean to a Total Depth (TD) of 1200' and filled from the surface with approximately 7 yards of 9 sack grout.
+
| No Violations
|
+
| At the time of the inspection the well was bailed clean to a Total Depth (TD) of 1200 and filled from the surface with approximately 7 yards of 9 sack grout.
|
 
|
 
|-
 
 
|-
 
|-
 
| 1428487047
 
| 1428487047
 
| 2013-02-05
 
| 2013-02-05
|  
+
| Orphan
 +
| No Violations
 
| At the time of the inspection there was no activity on site. All fishing of the tubing has been completed and all the tubing has been removed.
 
| At the time of the inspection there was no activity on site. All fishing of the tubing has been completed and all the tubing has been removed.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1558342825
 
| 1558342825
 
| 2013-03-01
 
| 2013-03-01
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection there was no activity on site.
 
| At the time of my inspection there was no activity on site.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1676790148
| -1676790148
 
 
| 2013-02-19
 
| 2013-02-19
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection all rods and tubing have been removed from the well. The rig has been moved off the location and the well is ready to be plugged.
 
| At the time of my inspection all rods and tubing have been removed from the well. The rig has been moved off the location and the well is ready to be plugged.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 1699855610
| -1699855610
 
 
| 2013-01-04
 
| 2013-01-04
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection there was no activity on site.
 
| At the time of my inspection there was no activity on site.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1935290517
 
| 1935290517
 
| 2012-12-13
 
| 2012-12-13
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection there was no activity on site.
 
| At the time of my inspection there was no activity on site.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 1955092452
 
| 1955092452
 
| 2012-12-10
 
| 2012-12-10
|  
+
| Orphan
| At the time of my inspection fishing of the 2 had begun at 9:00 am with nothing but debris (mud and stone) till 100'. The deris was cleared and fishing continued with a tubing spear to 120' with no success in retrieving the tubing. A total of 2.5 hours was spent fishing.
+
| No Violations
|
+
| At the time of my inspection fishing of the 2 had begun at 9:00 am with nothing but debris (mud and stone) till 100. The deris was cleared and fishing continued with a tubing spear to 120 with no success in retrieving the tubing. A total of 2.5 hours was spent fishing.
|
 
|
 
|-
 
 
|-
 
|-
| -1955780729
+
| 1955780729
 
| 2012-12-14
 
| 2012-12-14
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection no progress had been made in the fishing of the 2 tubing after leaving tension on it for two days. The contractor has decided to bring in a different rig before any further attempts to pull the tubing are made.
 
| At the time of my inspection no progress had been made in the fishing of the 2 tubing after leaving tension on it for two days. The contractor has decided to bring in a different rig before any further attempts to pull the tubing are made.
|
 
|
 
|
 
 
|-
 
|-
|-
+
| 2043640120
| -2043640120
 
 
| 2013-01-28
 
| 2013-01-28
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection the tubing was successfully fished from the well and placed in the slips. Then all tubing, including the barrell and mud anchor, had been removed from the well.
 
| At the time of my inspection the tubing was successfully fished from the well and placed in the slips. Then all tubing, including the barrell and mud anchor, had been removed from the well.
|
 
|
 
|
 
|-
 
 
|-
 
|-
 
| 2146323221
 
| 2146323221
 
| 2012-12-05
 
| 2012-12-05
|  
+
| Orphan
 +
| No Violations
 
| At the time of my inspection all the rods had been removed from the well with approximatly 2/3 of them being wooden rods.
 
| At the time of my inspection all the rods had been removed from the well with approximatly 2/3 of them being wooden rods.
|
 
|
 
|
 
|-
 
|-
 
| 491189008
 
| 2013-04-25
 
|
 
| At the time of the inspection there was no activity on site and the well is static, waiting to be plugged.
 
|
 
|
 
|
 
|-
 
|-
 
| 548853871
 
| 2013-07-16
 
|
 
| An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072.  The well site was situated on a location designated as agricultural field.  An interview conducted with the landowner, Mr. Tim Sautter, at his residence confirmed that he was satisfied with the restoration of the property to include wells located within field crop.
 
|
 
|
 
|
 
|-
 
|-
 
| -550989745
 
| 2012-11-27
 
|
 
| At the time of my inspection there was no activity on site but a steel tank had been placed on site in preperation of the plugging of the well.
 
|
 
|
 
|
 
|-
 
|-
 
| 973224100
 
| 2013-01-07
 
|
 
| At the time of my inspection there was no activity but a new rig was brought on site and set up on the well over the weekend. Fishing started around 4 pm according to Tony Kryder of Second Oil Lt.
 
|
 
|
 
|
 
 
|-
 
|-
 +
|}
 +
<!--==== Violations Commited ====
 +
{| class="wikitable sortable" width="95%"
 +
!scope="col" style="text-align: center"| Inspection ID
 +
!scope="col" style="text-align: center"| Violation ID
 +
!scope="col" style="text-align: center"| Violation Date
 +
!scope="col" style="text-align: center"| Violation Code
 +
!scope="col" style="text-align: center"| Violation Comments
 
|-
 
|-
| -992569367
+
|}-->
| 2012-12-17
 
|
 
| At the time of my inspection there was no activity on site and the contractor indicated there would be no activity till after the New Year.
 
|
 
|
 
|
 
|-
 
|}
 
 
For data sources see<ref>{{cite web
 
For data sources see<ref>{{cite web
  | title = Ohio Department of Natural Resources RBDMS
+
  | title = Risk Based Data Management System - tblInspection, tblInspFail and tblinspFlDesc Tables
  | publisher = [http://oilandgas.ohiodnr.gov/]
+
  |publisher = [[Ohio Department of Natural Resources]]
  | date = 2015-06-19
+
  | date = 2019-05-07
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources#Inspection
+
  | url = http://wellwiki.org/wiki/Ohio_Oil_and_Gas_Data_Sources
  | accessdate = 2015-06-20 }}</ref>
+
  | accessdate = 2019-05-21 }}</ref>
== References ==
+
==References==
{{reflist}}
+
<references/>
 
__NOEDITSECTION__
 
__NOEDITSECTION__
[[Category:Wells]]
+
[[Category:Ohio Wells]]

Revision as of 06:39, 31 July 2019

Well Details

Well ID: 34-143-60219
Loading map...
Country: United States
State: Ohio
County: Sandusky
Municipality: Scott Township
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name: SAUTTER TIM (BRINKERHOFF)
License Status: Final Restoration
License Date: 2012-10-26
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.297058326
Longitude: -83.38605855

For data sources see[1]

Well History

Well Status Well Status Date Comment
Well Added to System 2007-10-17 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Change of Owner 2012-10-18 Operator changed from 9998, HISTORIC OWNER to 8318, ORPHAN WELL PROGRAM
APP 2012-10-26 Proposed Formations:, Issued Date:10/26/2012, Expired Date:10/26/2014 12:00:00 PM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2013-05-06 Plugged by Orphan Well Program
Plugged/Abandoned 2013-05-06 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Construction Permit Expires 2014-10-26 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.
Record Last Modified 2019-06-14 NO PREVIOUS RECORD OF WELL. INSPECTION ON 2/19/1993 REVEALED WELL HAS 10" & 7" CASING WITH TUBING & RODS. ALSO THE WELL HAS A BLACK RUBBER LINE COMING FROM TUBING AND GOING INTO THE GROUND, POSSIBLE GAS LINE TO THE HOUSE BUT NOT IN USE. I&O CASE # 1993 07 054. EXHIBIT B ON TITLE INSURANCE SHOWS THAT THERE WAS A LEASE FOR OIL & GAS FROM SAMUEL BRINKERHOFF TO J M SHERMAN IN 1898 (RECORDED 3/1/1905). WILL NEED TO CORRECT THE LOCATION WHEN GET A GPS LOCATION.

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0131233671 2013-05-16 Final Restoration No Violations At the time of the inspection the area had been graded back for farm use by the plugging contractor. The site is currently being planted by the landowner. Final Restoration Passed.
0491189008 2013-04-25 Plug / Plug Back No Violations At the time of the inspection there was no activity on site and the well is static, waiting to be plugged.
0548853871 2013-07-16 Final Restoration No Violations An inspection of the Final Restoration revealed compliance with Ohio Revised Code 1509.072. The well site was situated on a location designated as agricultural field. An interview conducted with the landowner, Mr. Tim Sautter, at his residence confirmed that he was satisfied with the restoration of the property to include wells located within field crop.
0550989745 2012-11-27 Orphan No Violations At the time of my inspection there was no activity on site but a steel tank had been placed on site in preperation of the plugging of the well.
0973224100 2013-01-07 Orphan No Violations At the time of my inspection there was no activity but a new rig was brought on site and set up on the well over the weekend. Fishing started around 4 pm according to Tony Kryder of Second Oil Lt.
0992569367 2012-12-17 Orphan No Violations At the time of my inspection there was no activity on site and the contractor indicated there would be no activity till after the New Year.
1290545113 2013-05-07 Plug / Plug Back No Violations An inspection of the wellbore revealed the presence of an identification plate and no visible signs of leakage at the surface. The cement had settled from surface and will be topped off by the contractor.
1332211534 2012-12-11 Orphan No Violations At the time of my inspection fishing with an overshot had begun at 8:30 am with an overshot tool. The tubing was grabbed at 9:00 am and attempts to get the tubing to move continued until 10:30 am with almost no progress. The decision was made to leave tension on the tubing overnight for a total of 2 hours of fishing time.
1332957289 2012-03-27 Orphan No Violations Inspection to update GPS and well status for a potential Orphan Well Package. At the time of my inspection the well had 8conductor casing, 6 surface casing with casing head, 2 tubing broken below collar at casing head ring. Rods still inside tubing and bent 15 degrees to the west. Small pile of rocks and debris around wellhead. No sign of fluids leaking from well.
1334766134 2013-01-29 Orphan No Violations At the time of my inspection there was no activity on site.
1360260921 2013-01-02 Orphan No Violations At the time of my inspection the contractor was making an attempt to fish out the tubing but issues with the rig prevented any work.
1367863934 2013-05-06 Orphan No Violations At the time of the inspection the well was bailed clean to a Total Depth (TD) of 1200 and filled from the surface with approximately 7 yards of 9 sack grout.
1428487047 2013-02-05 Orphan No Violations At the time of the inspection there was no activity on site. All fishing of the tubing has been completed and all the tubing has been removed.
1558342825 2013-03-01 Orphan No Violations At the time of my inspection there was no activity on site.
1676790148 2013-02-19 Orphan No Violations At the time of my inspection all rods and tubing have been removed from the well. The rig has been moved off the location and the well is ready to be plugged.
1699855610 2013-01-04 Orphan No Violations At the time of my inspection there was no activity on site.
1935290517 2012-12-13 Orphan No Violations At the time of my inspection there was no activity on site.
1955092452 2012-12-10 Orphan No Violations At the time of my inspection fishing of the 2 had begun at 9:00 am with nothing but debris (mud and stone) till 100. The deris was cleared and fishing continued with a tubing spear to 120 with no success in retrieving the tubing. A total of 2.5 hours was spent fishing.
1955780729 2012-12-14 Orphan No Violations At the time of my inspection no progress had been made in the fishing of the 2 tubing after leaving tension on it for two days. The contractor has decided to bring in a different rig before any further attempts to pull the tubing are made.
2043640120 2013-01-28 Orphan No Violations At the time of my inspection the tubing was successfully fished from the well and placed in the slips. Then all tubing, including the barrell and mud anchor, had been removed from the well.
2146323221 2012-12-05 Orphan No Violations At the time of my inspection all the rods had been removed from the well with approximatly 2/3 of them being wooden rods.

For data sources see[3]

References