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| County: [[Knox_County,_Ohio|Knox]] | | County: [[Knox_County,_Ohio|Knox]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Pleasant Township,_Knox_County,_Ohio|Pleasant Township]] |
|- | |- | ||
| Operator Name: [[KNOX ENERGY INC.]] | | Operator Name: [[KNOX ENERGY INC.]] |
Well ID: 34-083-24433 | Loading map...
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Country: United States | |
State: Ohio | |
County: Knox | |
Municipality: Pleasant Township | |
Operator Name: KNOX ENERGY INC. | |
Well Pad ID: | |
Farm/Lease Name: PRUSHING G | |
License Status: Producing | |
License Date: 2010-07-08 | |
Spud Date: 2010-10-19 | |
Spud Drilling Contractor: KILBARGER DRLG | |
Final Drill Date: 2010-10-22 | |
Well Total Depth: 2604 ft | |
Configuration: Vertical | |
Latitude: 40.320571641 | |
Longitude: -82.43043163 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
APP | 2009-01-15 | Proposed Formations:OHIO SHALE THRU CLINTON, Issued Date:1/15/2009, Expired Date:1/15/2010 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:EOUT |
APP | 2010-07-08 | Proposed Formations:OHIO SHALE THRU CLINTON, Issued Date:7/8/2010, Expired Date:7/8/2011 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class:POOL |
Reached Total Depth | 2010-10-22 | |
Completion Report Received | 2011-01-27 | |
Construction Permit Expires | 2011-07-08 | |
Record Last Modified | 2017-10-24 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
2011-05-13 | 2449 | 2469 | 21 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
2010-12-03 | H2O | 15 | 49000 Gal | 13000 | Producers Service Corporation |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
2010 | KNOX ENERGY INC. | 0 | 0 | 14 |
2011 | KNOX ENERGY INC. | 4378 | 0 | 289 |
2012 | KNOX ENERGY INC. | 4420 | 0 | 366 |
2013 | KNOX ENERGY INC. | 3852 | 0 | 365 |
2014 | KNOX ENERGY INC. | 3366 | 0 | 365 |
2015 | KNOX ENERGY INC. | 3400 | 0 | 365 |
2016 | KNOX ENERGY INC. | 2365 | 0 | 365 |
2017 | KNOX ENERGY INC. | 2362 | 0 | 365 |
2018 | KNOX ENERGY INC. | 2195 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
2010 | KNOX ENERGY INC. | Brine | 190 | 14 |
2011 | KNOX ENERGY INC. | Brine | 295 | 289 |
2012 | KNOX ENERGY INC. | Brine | 70 | 366 |
2013 | KNOX ENERGY INC. | Brine | 0 | 365 |
2014 | KNOX ENERGY INC. | Brine | 0 | 365 |
2015 | KNOX ENERGY INC. | Brine | 0 | 365 |
2016 | KNOX ENERGY INC. | Brine | 0 | 365 |
2017 | KNOX ENERGY INC. | Brine | 0 | 365 |
2018 | KNOX ENERGY INC. | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0062424589 | 2013-08-26 | Preliminary Restoration | No Violations | Well is equipped with a motor and a pumping unit and proves capable of production. All drilling equipment has been removed and vegetation has been restored. Water is coming up around casing implying a potential leak. Inspector Mark McCombs has been informed and has contacted the company. Identification can be found at the tank battery. Tank battery consists of one 100 barrel tank within an earthen dike. Restoration passes. |
0191684407 | 2013-08-28 | Production Wells | No Violations | during my inspection found water standing around the well head and between the conductor and 8 inch. Teat found the water to be brine. The 4 inch seemed to be leaking around the threads. Called Knox energy to notify them. |
0736378399 | 2010-10-20 | Drill / Deepen / Reopen | No Violations | I witnessed this surface cement job today. |
For data sources see[9]