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Difference between revisions of "34-119-26717"

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| County: [[Muskingum_County,_Ohio|Muskingum]]
 
| County: [[Muskingum_County,_Ohio|Muskingum]]
 
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| Municipality: [[Wayne_Township,_Muskingum_County,_Ohio|Wayne Township]]
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| Municipality: [[Wayne Township,_Muskingum_County,_Ohio|Wayne Township]]
 
|-
 
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| Operator Name: [[S & S OIL CO]]
 
| Operator Name: [[S & S OIL CO]]

Revision as of 20:48, 12 August 2019

Well Details

Well ID: 34-119-26717
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Country: United States
State: Ohio
County: Muskingum
Municipality: Wayne Township
Operator Name: S & S OIL CO
Well Pad ID:
Farm/Lease Name: S & S OIL CO
License Status: Final Restoration
License Date: 2018-06-08
Spud Date: 1983-08-31
Spud Drilling Contractor: CAMERON BROS.
Final Drill Date: 1983-10-05
Well Total Depth: 3835 ft
Configuration: Vertical
Latitude: 39.874135207
Longitude: -81.94948345

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 1983-07-11 Issued Date 7/11/83 Expired Date 1/7/84 Acres 0040000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03835 Proposed Drill Depth 03835
Original Spud 1983-08-31 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
Completed 1983-10-05 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
Reached Total Depth 1983-10-05 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
CO 1983-10-19 288 S & S OIL CO GeoDate 7/11/83
Completion Report Received 1983-11-03 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
APP 2018-06-08 Proposed Formations:CLINTON, Issued Date:6/8/2018, Expired Date:6/7/2020 12:00:00 PM, Drilling unit acres:40, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2018-11-21 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
Record Last Modified 2019-05-21 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.
Construction Permit Expires 2020-06-07 UPDATE LOCATION PER DOGRM SURVEYOR COORDINATES.

For data sources see[2]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
0 0 0 NATURAL

For data sources see[3]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1990 S & S OIL CO 57167 64 365
1991 S & S OIL CO 43678 0 365
1992 S & S OIL CO 54 0 365
2007 S & S OIL CO 0 0 365
2008 S & S OIL CO 0 0 365
2013 S & S OIL CO 0 0 0
2014 S & S OIL CO 0 0 0
2015 S & S OIL CO 0 0 0
2016 S & S OIL CO 0 0 0
2017 S & S OIL CO 0 0 0

For data sources see[4] [5]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1990 S & S OIL CO Brine 60 365
1991 S & S OIL CO Brine 165 365
1992 S & S OIL CO Brine 380 365
2007 S & S OIL CO Brine 0 365
2008 S & S OIL CO Brine 0 365
2013 S & S OIL CO Brine 0 0
2014 S & S OIL CO Brine 0 0
2015 S & S OIL CO Brine 0 0
2016 S & S OIL CO Brine 0 0
2017 S & S OIL CO Brine 0 0

For data sources see[6] [7]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0000PL8343 Preliminary Restoration No Violations Preliminary Restoration done information from Data Point
0011392920 2019-02-22 Plug / Plug Back No Violations On the day of my inspection the Final Restoration did not pass. The location does not meet the 1509.072. There are several areas in need of good vegetation. The tanks and equipment have been removed.
0211098847 2019-04-10 Final Restoration No Violations The inspection revealed the Final Restoration was completed. The area had been graded back. The vegetation is starting to come in and there will be no chance for erosion to occur. All the equipment has been removed.
0255404801 2018-11-19 Plug / Plug Back No Violations The inspection was conducted under Plugging operations and a Compliance Notice follow-up to number -524644817. The Appalachian wireline surveys company had just left after perforating 10 holes at a 10-foot section from 2650-2660. The 2 3/8-inch 10 round tubing had been shot off at 2655 feet. Chipco is running the 2 3/8-inch 10 round tubing in with a stinger on the end to set the 200-foot plug at the top of the Big Lime.
0452679628 2018-11-23 Plug / Plug Back No Violations The inspection was conducted as a follow-up the plugging operations. The well was plugged and did not drop back. The rig was rigging down.
0524644817 2018-03-23 Production Wells Violations Noted

[

0717901529 2018-11-21 Plug / Plug Back No Violations The inspection is conducted under plugging operations and Compliance Notice follow-up to number --inch tubing 10 round to 1000 feet. Chipco set a plug at the Berea from 1000-800 feet with 60 sacks of regular class A cement, then displaced the plug down with 3 barrels of fresh water. Chipco set a plug at the Bottom of the surface from 576-376 feet with 60 sacks of regular class A cement, then displaced the plug down with 1.4 barrels of fresh water. Chipco pulled all the tubing out and hooked an 8 5/8-inch center spear and pulled 35,000 lbs. per foot on the 8 5/8-inch casing. The string weight weighs approximately 11,424 lbs. The pipe did not stretch. The center spear was backed out and the welder showed up to weld a nipple on the casing. The tension was placed on the casing approximately 2,000 lbs. of weight applied and backed off the first joint of casing. There was 20 feet of 8 5/8-inch casing pulled out. Chipco then ran 7 joints of 2 3/8inch 10 round tubing and a stinger in the well. The top plug was set from 231-0. They ran 75 sacks of regular class A cement. The cement was circulated back to surface. All plugs circulated, and the decision was made to leave the well set open until 11-23-18 before plating the well. The Compliance Notice has been resolved due to the well being plugged.
1094200838 2004-02-11 Production Wells No Violations Well used for gas for the plant.
1542821009 2018-11-20 Plug / Plug Back No Violations The inspection was conducted under plugging operations and Compliance Notice follow-up to number -524644817. Chipco had ran 2 3/8- inch 10 round tubing to 2650 feet and set a cement plug of 60 sacks of regular class A cement from 2650-2450 over the Big Lime. The displacement was 10 barrels of fresh water.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0524644817 US-OH-125734 2018-04-11 Failure to have required locks, bull plugs
0524644817 US-OH-125735 2018-04-11 Well shall be plugged

For data sources see[8]

References