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| County: [[Licking_County,_Ohio|Licking]] | | County: [[Licking_County,_Ohio|Licking]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Eden Township,_Licking_County,_Ohio|Eden Township]] |
|- | |- | ||
| Operator Name: [[LBJ DRILLING CO INC]] | | Operator Name: [[LBJ DRILLING CO INC]] |
Well ID: 34-089-23970 | Loading map...
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Country: United States | |
State: Ohio | |
County: Licking | |
Municipality: Eden Township | |
Operator Name: LBJ DRILLING CO INC | |
Well Pad ID: | |
Farm/Lease Name: DUDGEON CAREY & KAREN | |
License Status: Producing | |
License Date: 1980-10-08 | |
Spud Date: 1980-12-08 | |
Spud Drilling Contractor: | |
Final Drill Date: 1981-01-03 | |
Well Total Depth: 2827 ft | |
Configuration: Vertical | |
Latitude: 40.222739829 | |
Longitude: -82.28909277 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
CO | 1980-10-08 | 286 McKEE DON DRILL CO INC GeoDate 10/8/80 |
Original Spud | 1980-12-08 | |
Completed | 1981-01-03 | |
Reached Total Depth | 1981-01-03 | |
Change of Owner | 2003-01-29 | Operator changed from 286, McKEE DON DRILL CO INC to 576, HARDESTY PRODUCTION |
Change of Owner | 2017-05-22 | Operator changed from 576, HARDESTY PRODUCTION to 226, LBJ DRILLING CO INC |
Record Last Modified | 2017-05-22 |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 88000 Gal | 19000 |
For data sources see[3]
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
1985 | McKEE DON DRILL CO INC | Brine | 362 | 365 |
1986 | McKEE DON DRILL CO INC | Brine | 527 | 365 |
1987 | McKEE DON DRILL CO INC | Brine | 201 | 365 |
1988 | McKEE DON DRILL CO INC | Brine | 165 | 365 |
1990 | McKEE DON DRILL CO INC | Brine | 165 | 365 |
1991 | McKEE DON DRILL CO INC | Brine | 158 | 365 |
1992 | McKEE DON DRILL CO INC | Brine | 163 | 365 |
1993 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
1994 | McKEE DON DRILL CO INC | Brine | 87 | 365 |
1995 | McKEE DON DRILL CO INC | Brine | 145 | 365 |
1997 | McKEE DON DRILL CO INC | Brine | 78 | 365 |
1998 | McKEE DON DRILL CO INC | Brine | 40 | 365 |
1999 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
2000 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
2001 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
2002 | McKEE DON DRILL CO INC | Brine | 0 | 365 |
2003 | HARDESTY PRODUCTION | Brine | 0 | 365 |
2004 | HARDESTY PRODUCTION | Brine | 35 | 365 |
2005 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2006 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2007 | HARDESTY PRODUCTION | Brine | 60 | 365 |
2008 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2009 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2010 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2011 | HARDESTY PRODUCTION | Brine | 50 | 365 |
2012 | HARDESTY PRODUCTION | Brine | 0 | 366 |
2013 | HARDESTY PRODUCTION | Brine | 32 | 365 |
2014 | HARDESTY PRODUCTION | Brine | 0 | 365 |
2015 | HARDESTY PRODUCTION | Brine | 0 | 365 |
2016 | HARDESTY PRODUCTION | Brine | 45 | 365 |
2017 | LBJ DRILLING CO INC | Brine | 0 | 150 |
2018 | LBJ DRILLING CO INC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
00CENT1329 | 1996-07-08 | Production Wells | No Violations | 1501:9-9-05 |
0416263726 | 2016-06-13 | Production Wells | Violations Noted | This inspection was conducted as a status check. The well was equipped with a pumping unit and motor. Identification was observed on the pumping unit. It was not pumping during inspection. The tank battery consists of (2) 100 barrel tanks and (1) 1000 gallon plastic brine tank inside an earthen dike. This well produces into a shared tank battery with API#3971. Identification was posted at the tank battery. The inspection revealed that oil has appeared to have spilled inside the dike at one time as the soil was stained with oil. A leak was observed on the plastic brine tank from the bottom bung. I observed 1 drip/8 seconds from that tank. A small gas leak was also observed on a gas line that is connected to a tank heater. I took (5) photos of the tank battery during inspection. A phone call was placed to Mark Hardesty regarding inspection. Mr. Hardesty was advised to do the following: 1) Clean/remove oil stained soil 2) Fix leak on tank or replace tank 3) Fix gas leak. Mr. Hardesty agreed and said he would get started as soon as possible. Time of inspection: 2:00 PM. Weather: 76*F, Sunny |
0640465677 | 2016-06-27 | Production Wells | No Violations | Inspect tank battery as a compliance notice follow-up. Fresh soil has been brought in. The dike has been cleaned up. The plastic tank has been removed. A small gas leak was still observed. Time of inspection: 11:50 AM. Weather: 81*F, Sunny |
0844722544 | 2016-07-07 | Administrative Inspection | No Violations | I received a phone call at 8:12 AM from Mr. Hardesty regarding the leaking tank. Mr. Hardesty said he plans on removing tank. The tank battery will be in compliance when tank is removed or leak is fixed. |
1279209779 | 2016-07-19 | Production Wells | No Violations | Inspect tank battery as a follow-up. The tank was no longer leaking as it was repaired. Tank battery ok. Violation resolved. Time of inspection: 1:30 PM. Weather: 86*F, Sunny |
1485356843 | 2017-01-18 | Production Wells | No Violations | Inspect well as a compliance notice follow-up. Identification has not been posted at the well. A card was left at the well advising identification needs to be posted. Time of inspection: 2:00 PM. |
1758692492 | 2017-03-22 | Production Wells | No Violations | Identification has been posted at the well and tank battery. Well and tank battery are in compliance. Time of inspection: 2:50 PM. Weather: 36*F, Sunny |
2031067181 | 2016-06-20 | Production Wells | No Violations | Inspect tank battery as a compliance notice follow-up. The inspection revealed that the plastic brine tank has been drained and was no longer dripping water. No other work has been done yet. Time of inspection: 3:30 PM. Weather: 88*F, Sunny |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0416263726 | US-OH-124426 | 2016-06-23 | Well operation causing pollution and contamination |
For data sources see[8]