If you find this page useful and would like to be notified of changes made to this page, start by inputting your email below.
powered by ChangeDetection
m |
m |
||
Line 11: | Line 11: | ||
| County: [[Coshocton_County,_Ohio|Coshocton]] | | County: [[Coshocton_County,_Ohio|Coshocton]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Monroe Township,_Coshocton_County,_Ohio|Monroe Township]] |
|- | |- | ||
| Operator Name: [[KNOX ENERGY INC.]] | | Operator Name: [[KNOX ENERGY INC.]] | ||
Line 33: | Line 33: | ||
| Configuration: Vertical | | Configuration: Vertical | ||
|- | |- | ||
− | | Latitude: | + | | Latitude: <Latitude> |
|- | |- | ||
| Longitude: -82.06597015 | | Longitude: -82.06597015 |
Well ID: 34-031-24945 | Loading map...
{"type":"SATELLITE","minzoom":false,"maxzoom":false,"types":["ROADMAP","SATELLITE","HYBRID","TERRAIN"],"mappingservice":"googlemaps3","width":"100%","height":"350px","centre":false,"title":"","label":"","icon":"","visitedicon":"","lines":[],"polygons":[],"circles":[],"rectangles":[],"wmsoverlay":false,"copycoords":false,"static":false,"zoom":14,"layers":[],"controls":["pan","zoom","type","scale","streetview","rotate"],"zoomstyle":"DEFAULT","typestyle":"DEFAULT","autoinfowindows":false,"resizable":false,"kmlrezoom":false,"poi":true,"markercluster":false,"clustergridsize":60,"clustermaxzoom":20,"clusterzoomonclick":true,"clusteraveragecenter":true,"clusterminsize":2,"imageoverlays":[],"kml":[],"gkml":[],"searchmarkers":"","enablefullscreen":false,"scrollwheelzoom":false,"locations":[{"text":"","title":"","link":"","lat":40.422125912,"lon":-82.06597015,"icon":""}]} |
Country: United States | |
State: Ohio | |
County: Coshocton | |
Municipality: Monroe Township | |
Operator Name: KNOX ENERGY INC. | |
Well Pad ID: | |
Farm/Lease Name: DUNHAM KARL | |
License Status: Final Restoration | |
License Date: 2009-05-07 | |
Spud Date: 1983-06-27 | |
Spud Drilling Contractor: DUGAN DRILLING | |
Final Drill Date: 1983-08-22 | |
Well Total Depth: 3353 ft | |
Configuration: Vertical | |
Latitude: <Latitude> | |
Longitude: -82.06597015 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1982-11-10 | Issued Date 11/10/82 Expired Date 5/9/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1983-01-12 | 1336 AKRON OIL CORP GeoDate 1/12/83 |
Oil and Gas | 1983-01-12 | Issued Date 12/30/82 Expired Date 6/28/83 Acres 0020000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03353 Proposed Drill Depth 03353 |
Original Spud | 1983-06-27 | |
Completed | 1983-08-22 | |
Reached Total Depth | 1983-08-22 | |
CO | 1983-09-07 | 7 JONSU OIL CORP GeoDate 11/10/82 |
Completion Report Received | 1983-09-28 | |
Change of Owner | 2003-06-16 | Operator changed from 1336, AKRON OIL CORP to 6295, KNOX ENERGY INC. |
APP | 2007-09-06 | Proposed Formations:CLINTON, Issued Date:9/6/2007, Expired Date:9/5/2008 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
APP | 2009-05-07 | Proposed Formations:CLINTON, Issued Date:5/7/2009, Expired Date:5/7/2010 6:00:00 AM, Drilling unit acres:20, Proposed Well Type:OG, Proposed Well Class: |
Plugged/Abandoned | 2009-06-18 | |
Construction Permit Expires | 2010-05-07 | |
Record Last Modified | 2019-04-03 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3284 | 3328 | 0 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
0 | 0 | 0 | FRAC, WATER & SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AKRON OIL CORP | 416 | 79 | 0 |
1985 | AKRON OIL CORP | 112 | 0 | 0 |
1986 | AKRON OIL CORP | 0 | 69 | 365 |
1987 | AKRON OIL CORP | 0 | 0 | 0 |
1988 | GREENWOOD OIL R F D | 0 | 95 | 120 |
1989 | GREENWOOD OIL R F D | 0 | 160 | 300 |
1990 | GREENWOOD OIL R F D | 0 | 160 | 300 |
2003 | KNOX ENERGY INC. | 0 | 0 | 365 |
2004 | KNOX ENERGY INC. | 0 | 0 | 366 |
2005 | KNOX ENERGY INC. | 0 | 0 | 365 |
2006 | KNOX ENERGY INC. | 0 | 0 | 0 |
2007 | KNOX ENERGY INC. | 0 | 48 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | AKRON OIL CORP | Brine | 10 | 0 |
1985 | AKRON OIL CORP | Brine | 10 | 0 |
1986 | AKRON OIL CORP | Brine | 70 | 365 |
1987 | AKRON OIL CORP | Brine | 65 | 0 |
1988 | GREENWOOD OIL R F D | Brine | 10 | 120 |
1989 | GREENWOOD OIL R F D | Brine | 10 | 300 |
1990 | GREENWOOD OIL R F D | Brine | 20 | 300 |
2003 | KNOX ENERGY INC. | Brine | 0 | 365 |
2004 | KNOX ENERGY INC. | Brine | 0 | 366 |
2005 | KNOX ENERGY INC. | Brine | 0 | 365 |
2006 | KNOX ENERGY INC. | Brine | 0 | 0 |
2007 | KNOX ENERGY INC. | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000UIC467 | 1987-10-01 | Salt Water Injection Well | No Violations | 1501:9-3-11 (A)(1) |
0001252i15 | 2011-12-20 | Orphan | Violations Noted | checked well for violations, george shidaker thinking about buying wells. |
0001595626 | 2011-12-20 | Orphan | No Violations | checked well for violations, george shidaker thinking about buying wells. |
0111525605 | 2009-06-17 | Plug / Plug Back | No Violations | 8 casing welded and starting to try and pull . |
0298105390 | 2011-12-20 | Orphan | No Violations | FOLLOW UP TO NOV # 1252i15 checked well for violations, george shidaker thinking about buying wells. |
0501980850 | 2007-02-21 | Production Wells | No Violations | Motor removed from pumping unit , company notified they would be bring a rig in to service well . |
0705187018 | 2013-03-12 | Production Wells | No Violations | FOLLOW UP TO CA # 1252i15: On the day of my inspection I found that the site was reclaimed. There was no evidence of well casing. This well was reported as being plugged on 6/18/2009, and the final restoration was passed on 10/7/2009. The violation for defective casing is resolved, as the casing was pulled when the well was plugged. |
1179935192 | 2007-05-23 | Production Wells | No Violations | Berry well service on well , steaming tubing , well will be back in production this week . N.O.V. compliance . |
1245254559 | 2009-06-16 | Plug / Plug Back | No Violations | Bottom and Lime plug set , circulated approx. 3 bl. Of oil from hole before pulling 4.5 casing . |
1245339943 | 2009-06-18 | Plug / Plug Back | No Violations | Plugging completed . |
1254932172 | 2009-10-07 | Final Restoration | No Violations | Restoration passed . |
1421092878 | 2006-12-01 | Production Wells | No Violations | Motor removed from pumping unit , Company called and said they were working to get well back in production . |
1669612391 | 2008-01-14 | Production Wells | No Violations | Surface equipment removed from well site , plugging permit has been issued . |
1903133351 | 2006-09-06 | Production Wells | Violations Noted | Well not capable of production , belt of motor , weeds grown up around pumping unit . No production reported since 1990 . |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
0001252i15 | US-OH-106780 | 2001-10-17 | Defective casing, leaking well | |
1903133351 | US-OH-119129 | 2006-09-06 | Well shall be plugged |
For data sources see[9]