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Difference between revisions of "34-167-28396"

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| State: Ohio
 
| State: Ohio
 
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| County: [[Washington_County,_Ohio|Washington]]
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| County: <County>
 
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| Municipality: [[Newport Township,_Washington_County,_Ohio|Newport Township]]
 
| Municipality: [[Newport Township,_Washington_County,_Ohio|Newport Township]]

Revision as of 15:23, 13 August 2019

Well Details

Well ID: 34-167-28396
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Country: United States
State: Ohio
County: <County>
Municipality: Newport Township
Operator Name: MARTIN LARREY C
Well Pad ID:
Farm/Lease Name: HEARN ARTHUR
License Status: Producing
License Date: 2006-10-16
Spud Date: 1986-07-08
Spud Drilling Contractor:
Final Drill Date: 1986-08-06
Well Total Depth: 720 ft
Configuration: Vertical
Latitude: 39.413201732
Longitude: -81.29074989

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1986-07-08 FDT=CASING, PF=CASING
Completed 1986-08-06 FDT=CASING, PF=CASING
Reached Total Depth 1986-08-06 FDT=CASING, PF=CASING
Completion Report Received 1987-05-18 FDT=CASING, PF=CASING
APP 2006-10-16 Proposed Formations:MACKSBURG, Issued Date:10/16/2006, Expired Date:10/16/2007 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Construction Permit Expires 2007-10-16 FDT=CASING, PF=CASING
Change of Owner 2015-08-17 Operator changed from 409, A & R ENERGY INC to 2523, MARTIN LARREY C
Record Last Modified 2017-02-15 FDT=CASING, PF=CASING

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1999-07-06 706 710 3

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
ACID 0 0 0
ACID 0 0 0 24 HRS.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1987 A & R ENERGY INC 0 0 365
1988 A & R ENERGY INC 0 0 365
1989 A & R ENERGY INC 0 0 365
1990 A & R ENERGY INC 0 0 365
1991 A & R ENERGY INC 0 0 365
1995 A & R ENERGY INC 956 160 0
1998 A & R ENERGY INC 20 0 365
2000 A & R ENERGY INC 0 0 365
2001 A & R ENERGY INC 0 0 0
2002 A & R ENERGY INC 0 0 0
2003 A & R ENERGY INC 0 0 0
2005 A & R ENERGY INC 0 0 0
2007 A & R ENERGY INC 0 0 0
2008 A & R ENERGY INC 0 0 0
2011 A & R ENERGY INC 0 0 0
2012 A & R ENERGY INC 0 0 0
2013 A & R ENERGY INC 0 0 0
2016 MARTIN LARREY C 0 0 365
2017 MARTIN LARREY C 0 0 0
2018 MARTIN LARREY C 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1987 A & R ENERGY INC Brine 0 365
1988 A & R ENERGY INC Brine 0 365
1989 A & R ENERGY INC Brine 0 365
1990 A & R ENERGY INC Brine 0 365
1991 A & R ENERGY INC Brine 0 365
1995 A & R ENERGY INC Brine 0 0
1998 A & R ENERGY INC Brine 0 365
2000 A & R ENERGY INC Brine 0 365
2001 A & R ENERGY INC Brine 0 0
2002 A & R ENERGY INC Brine 0 0
2003 A & R ENERGY INC Brine 0 0
2005 A & R ENERGY INC Brine 0 0
2007 A & R ENERGY INC Brine 0 0
2008 A & R ENERGY INC Brine 0 0
2011 A & R ENERGY INC Brine 0 0
2012 A & R ENERGY INC Brine 0 0
2013 A & R ENERGY INC Brine 0 0
2016 MARTIN LARREY C Brine 0 365
2017 MARTIN LARREY C Brine 0 0
2018 MARTIN LARREY C Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0011316198 2015-01-15 Production Wells No Violations Upon inspection, it was observed that this well is still noncompliant and is incapable of production. The well consists of 4.5 with a 4-2 swedge and 2 ball valve. No lines are connected to the well. I will contact A&R Energy Inc. and inquire about plans to plug or produce this well.
0472257050 2010-12-03 Administrative Inspection No Violations Talked to Jim Zimmer - appologized for not getting Permit to Plug filed - said would be working on it. I had sent copy of original NOV to Pittsburgh office as felt they had forgot about it. Still needs plugged.
0884389490 2018-10-05 Production Wells Violations Noted On this day, I am conducting an inspection per request of Southeast Supervisor Dan Goins. I found the well equipped with 4.5 inch diameter casing with a 4x2 inch diameter reduction swage setup to be produced as an open-flow well, with the production valve closed. The 4.5 inch casing appears very loose within the surface casing, and standing fluid is present within the annular space between production and surface casing. There are no hook-ups connected and no production facility associated with the well. Updated pictures were taken. There is no identification present at the wellhead, and zeros (0) have been reported for production from 2000-2016. The well owner/operator shall submit a written plugging schedule to Tom Thomas at 5880 Memory Road Zanesville, OH 43701 within 30 days, per ORC 1509:13(B)(7), and plug the well within 180 days. The well owner/operator will be notified if the plugging schedule is approved or denied.
1144870925 2006-04-12 Production Wells Violations Noted My inspection this day found this well not in operation. The 4.5 production casing was hanging on a clamp. I was told that this well has not been cemented. No identification signs are posted. I called Larry Haynes who said he will plug well in the next 12 months. I agreed with his time frame and gave him a verbal Notice of Violation (NOV) at this time. 10/8/07- No change in well status, so I will issue a written NOV to produce or plug this well and post proper identification signs. Failure to comply may result in bond forfeiture. 6/10 - I contacted Jim Zimmer, now supervisor at A&R Energy, who requested the paperwork to file for a plugging permit. He plans to plug the well this summer. 12/6 - I spoke with Jim Zimmer who said he did not get the plugging permit filed. 1/20/12 - Larry Martin reported he has bought the shallow wells of A&R. He said this well probably will not be plugged until summer.
1342689919 2016-08-04 Production Wells No Violations The purpose of my inspection today is a follow up on a compliance notice. During my inspection the well was equipped with 8.625 inch surface casing, 4.5 inch production casing, 4.5 inch to 2 inch swage nipple, and a 2 inch ball valve in the closed position. No lines are attached to the well and there is not any production equipment. No identification is posted. No action has been taken to gain compliance.
1396536635 2006-04-12 Production Wells No Violations FOLLOW UP TO NOV # 1144870925 My inspection this day found this well not in operation. The 4.5 production casing was hanging on a clamp. I was told that this well has not been cemented. No identification signs are posted. I called Larry Haynes who said he will plug well in the next 12 months. I agreed with his time frame and gave him a verbal Notice of Violation (NOV) at this time. 10/8/07- No change in well status, so I will issue a written NOV to produce or plug this well and post proper identification signs. Failure to comply may result in bond forfeiture. 6/10 - I contacted Jim Zimmer, now supervisor at A&R Energy, who requested the paperwork to file for a plugging permit. He plans to plug the well this summer. 12/6 - I spoke with Jim Zimmer who said he did not get the plugging permit filed. 1/20/12 - Larry Martin reported he has bought the shallow wells of A&R. He said this well probably will not be plugged until summer.
1476734195 2012-08-08 Administrative Inspection No Violations Ben from Virco called to inquire how this well was to be plugged. We discussed plugs and he said A & R had hired them to plug. I also e-mailed Ron Nyswanger of A & R and asked that not only they plug this well but to work on several of their idle wells while had the service rig hired. Sale of leases must not have gone thru
1554988725 2019-04-11 Production Wells No Violations On this day, I am conducting a compliance notice follow-up inspection. No progress has been made to gain compliance. I found the well equipped with 4.5 inch diameter casing with a 4x2 inch diameter reduction swage and the production valve closed. There are no hook-ups connected and no production facility associated with the well. There is no identification present at the wellhead, and zeros (0) have been reported for production from 2000-2018. I spoke with Larry Martin on 4/11/2019 and he stated that he will be in the process of filing for a plugging permit.
1583241159 2015-12-15 Production Wells No Violations Upon inspection, it was observed that this well is still idle and is incapable of production. The well consists of 8.625 surface casing and 4.5 production casing with a 4-2 swedge and 2 ball valve in the closed position. The 4.5 casing is very loose in the well and previous inspection reports indicate that the casing may not be cemented. Fluid was observed approximately 10 down the 8.625 casing. No ID information is posted at the well. No tanks are assocaited with the well. No flow lines are attached to the well. RBDMS records indicate that Larrey C. Martin purchased this well from A&R Energy on 8/17/2015. I will contact Mr. Martin and inquire about plans to plug the well or to put it into production.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0884389490 US-OH-129977 2018-11-26 9-9-05(A)10 Failure to legibly identify well
0884389490 US-OH-129978 2018-11-26 NONE Well shall be plugged
1144870925 US-OH-103731 2006-04-12 Failure to legibly identify well
1144870925 US-OH-103732 2006-04-12 Well shall be plugged

For data sources see[9]

References