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| State: Ohio | | State: Ohio | ||
|- | |- | ||
− | | County: | + | | County: <County> |
|- | |- | ||
| Municipality: [[Aurelius Township,_Washington_County,_Ohio|Aurelius Township]] | | Municipality: [[Aurelius Township,_Washington_County,_Ohio|Aurelius Township]] |
Well ID: 34-167-28519 | Loading map...
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Country: United States | |
State: Ohio | |
County: <County> | |
Municipality: Aurelius Township | |
Operator Name: SPECTRUM OIL CORPORATION | |
Well Pad ID: | |
Farm/Lease Name: GEORGIANA OIL CO | |
License Status: Orphan Well - Pending | |
License Date: 1987-08-25 | |
Spud Date: 1987-09-21 | |
Spud Drilling Contractor: DELANEY DRLG | |
Final Drill Date: 1987-10-08 | |
Well Total Depth: 1210 ft | |
Configuration: Vertical | |
Latitude: 39.606659086 | |
Longitude: -81.46773420 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1987-08-25 | Issued Date 8/25/87 Expired Date 8/24/88 Acres 0010000 Tool Type CT Proposed Formation KEENER/BIG I Proposed Depth 01210 Proposed Drill Depth 01210 |
Original Spud | 1987-09-21 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
Completed | 1987-10-08 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
Reached Total Depth | 1987-10-08 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
CO | 1987-10-30 | 1438 SPECTRUM OIL CORPORATION GeoDate 8/25/87 |
Completion Report Received | 1987-10-30 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
Construction Permit Expires | 1988-08-24 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
Changed to Orphan Well Pending | 2019-03-25 | Changed Well To Orphan Pending |
Record Last Modified | 2019-03-25 | FIELD REVIEW REQUEST TO INSPECTOR FOR ORPHAN WELL REFERRAL 12/16/03. PF=MACKSBURG 800' STATUS CHANGED FROM PR TO IA PER INSPECTION, WELL IS STILL CANDIDATE FOR ORPHAN 4/14/2016 ALE |
For data sources see[2]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
NITR | 0 | 135 Qts | 0 | SHOT W/135 QTS NITRO MACKSBURG/KEENER |
For data sources see[3]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | SPECTRUM OIL CORPORATION | 605 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1988 | SPECTRUM OIL CORPORATION | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0000007994 | Preliminary Restoration | No Violations | PASSED Y WITNESSED 6/16/88 INSPECTOR BOB ARMSTRONG DATE 06/1619/88 DATA FROM OLD VAX INFO | |
0000PL1369 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0008590355 | 2009-04-27 | Production Wells | No Violations | Inspection this day found no change - well still not producing. Owner is Sam Buckey, as he pulled rods and tubing out of well and logged it, then removed equipment from location. No IDs, no tank, well head sitting open. |
0058572897 | 2013-12-11 | Production Wells | No Violations | On this inspection, I found a well head on top of 4.5 in casing. There was no tubing in the well and the annulus had no lines connected to it either. There is no tank associated with this well. It is situated in a hay field and has round bales stored around it. |
0108503603 | 2006-07-20 | Production Wells | No Violations | FOLLOW UP TO NOV # 1153393096 Inspection this day found all equipment pulled out of well - about 1 year ago, Sam Buckey came in and pulled everything, logged well and left - have not seen a sight of since. Well standing open, rods and tubing gone. 8/28/2006 - |
0843228883 | 2009-11-03 | Production Wells | No Violations | Inspection this day found well still sitting idle, no IDs. According to source who wished to remain anonomous, Sam Buckey hired service rig to pull rods, tubing on this well, ran an electric log, then took the tubing and rods and left. He did not own well. 11/10/09 Talked to Sam this day regarding ownership of well - he says he was evaluating it for another party (would not say who) and that G-R Contracting appears to be owner, after reviewing courthouse records. Sam said he was willing to plug well but not until ownership issue resolved. Well is currently standing open. |
1153393096 | 2006-07-20 | Production Wells | Violations Noted | Inspection this day found all equipment pulled out of well - about 1 year ago, Sam Buckey came in and pulled everything, logged well and left - have not seen a sight of since. Well standing open, rods and tubing gone. 8/28/2006 - |
1328759558 | 2005-05-09 | Production Wells | No Violations | This is supposed to be idle/orphan but someone has come in and plugged rods and tubing. Have call in to Phil Case to see who has adopted it. |
1367602362 | 2013-05-03 | Orphan | No Violations | My inspection this day was to begin the process of entering the well into the orphan well program. This well is sitting idle, has never produced in the last 10 years, and consists of 40 of 10 with 382 of 7 surface casing. No record of any production casing having been run. I received an anonymous report in 2005 that Sam Buckey pulled the tubing and rods that were in the hole and ran an electric log but I did not witness it. A violation was wrote in 7/2006 to plug or produce and mailed to Sam Buckey, last person to work on well. Chiefs Orders were issued to Spectrum Oil Corp. in 1992 but I was not aware of. Pictures taken, SEM is 98. No hazard but not very expensive to plug and reclaim. |
1392319831 | 2014-02-13 | Orphan | No Violations | Visited site to get updated photos for orphan referral. The well is approximately 203 feet from the road. There is 7 in. casing exposed with a well head threaded on it. Approximately 48 ft. Northwest of the well, there is a piece of 2 in steel with a brass valve and a hammer union on it sticking straight out of the ground about 4 ft. high. |
1394453934 | 2014-03-05 | Administrative Inspection | No Violations | Received e-mail from Idle and Orphan Inspector 3 Cindy VanDyke. She stated that she had entered this well in the Idle and Ophan program. |
1571268665 | 2009-11-09 | Production Wells | No Violations | Talked to Sam Buckey - he admitted to working on well, logging it and he would ask Northwood Energy, now the landowner, if they would take it. Reports his cell number id 561-222-9557 and that he is working on getting additional 6 wells out of his name and transferred to current operator. |
1571271548 | 2004-10-08 | Orphan | No Violations | Inspection this day per Sherry Young. Well is idle but shut-in, tanks, separator, meter have been removed but tank pad remains. I had asked G-R Contracting to take a look and see if they might be interested - no response |
1589161940 | 2016-04-01 | Orphan | No Violations | Performed an inspection of this well in response to a request from DOGRM Permitting Section. Upon inspection, it was observed that this well is idle and incapable of production. Spectrum Oil Corp. is a defunct company. This well is likely orphan. The well consists of 7 surface casing with a well head with fittings open to the atmosphere. No gas or oil was leaking from the well at the time of inspection. Previous inspections indicate that this well has been referred to the Orphan Well Program in the past. Updated photos were taken of the location. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1153393096 | US-OH-103987 | 2013-05-03 | Failure to legibly identify well | |
1153393096 | US-OH-103988 | 2013-05-03 | Well shall be plugged |
For data sources see[8]