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Difference between revisions of "34-167-29081"

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| State: Ohio
 
| State: Ohio
 
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| County: [[Washington_County,_Ohio|Washington]]
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| County: <County>
 
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| Municipality: [[Wesley Township,_Washington_County,_Ohio|Wesley Township]]
 
| Municipality: [[Wesley Township,_Washington_County,_Ohio|Wesley Township]]

Revision as of 17:08, 13 August 2019

Well Details

Well ID: 34-167-29081
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Country: United States
State: Ohio
County: <County>
Municipality: Wesley Township
Operator Name: BROAD STREET SERV LLC
Well Pad ID:
Farm/Lease Name: KENEY-KING
License Status: Final Restoration
License Date: 2012-10-05
Spud Date: 1994-07-28
Spud Drilling Contractor: HIGHLAND DRLG
Final Drill Date: 1994-07-30
Well Total Depth: 5355 ft
Configuration: Vertical
Latitude: 39.417030225
Longitude: -81.80517548

For data sources see[1]

Well History

Well Status Well Status Date Comment
Original Spud 1994-07-28 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
CO 1994-07-29 4350 CENTURY WELL SERVICE GeoDate 7/29/94
Oil and Gas 1994-07-29 Issued Date 7/29/94 Expired Date 7/29/95 Acres 0045073 Tool Type RTA Proposed Formation ORISKANY/CLINTON Proposed Depth 05355 Proposed Drill Depth 05355
Completed 1994-07-30 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
Reached Total Depth 1994-07-30 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
Completion Report Received 1994-08-25 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
Change of Owner 2007-10-03 Operator changed from 4350, CENTURY WELL SERVICE to 7033, BROAD STREET ENERGY COMPANY
Change of Owner 2008-02-19 Operator changed from 7033, BROAD STREET ENERGY COMPANY to 8312, BROAD STREET SERV LLC
APP 2012-10-05 Proposed Formations:CLINTON/MEDINA, Issued Date:10/5/2012, Expired Date:10/5/2014 12:00:00 PM, Drilling unit acres:45.073, Proposed Well Type:OG, Proposed Well Class:
Plugged/Abandoned 2013-11-07 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
Construction Permit Expires 2014-10-05 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM
Record Last Modified 2015-10-01 CHANGED STATUS OF WELL FROM PA TO FR PER F_REST_PASS FACILITY REPORT FROM AUSTIN GUTRIDGE (SEE SURETY FILE) 9/29/2015 ON 10/1/2015 CM

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
1997-06-29 5104 5132 0
2006-09-11 5112 9
2006-09-11 5193 4

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 44000 Gal 60000 FRAC W/44M GAL WATER & 600 SX SAND
ACID 15 500 Gal 0 IRON, CONTROL ACID, FM BKDN.

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1994 MUTUAL OIL & GAS CO 0 0 0
1995 CENTURY WELL SERVICE 3317 0 314
1996 CENTURY WELL SERVICE 6657 0 365
1997 CENTURY WELL SERVICE 4715 0 365
1998 CENTURY WELL SERVICE 4621 0 365
1999 CENTURY WELL SERVICE 553 0 365
2000 CENTURY WELL SERVICE 0 0 365
2001 CENTURY WELL SERVICE 2681 0 365
2002 CENTURY WELL SERVICE 2576 0 365
2003 CENTURY WELL SERVICE 2422 0 365
2004 CENTURY WELL SERVICE 1134 0 365
2005 CENTURY WELL SERVICE 1001 0 365
2006 CENTURY WELL SERVICE 1186 0 365
2007 BROAD STREET SERV LLC 1120 0 365
2008 BROAD STREET SERV LLC 0 0 0
2009 BROAD STREET SERV LLC 0 0 0
2010 BROAD STREET SERV LLC 0 0 0
2011 BROAD STREET SERV LLC 0 0 0
2012 BROAD STREET SERV LLC 0 0 0
2013 BROAD STREET SERV LLC 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1994 MUTUAL OIL & GAS CO Brine 70 0
1995 CENTURY WELL SERVICE Brine 183 314
1996 CENTURY WELL SERVICE Brine 25 365
1997 CENTURY WELL SERVICE Brine 90 365
1998 CENTURY WELL SERVICE Brine 0 365
1999 CENTURY WELL SERVICE Brine 0 365
2000 CENTURY WELL SERVICE Brine 0 365
2001 CENTURY WELL SERVICE Brine 0 365
2002 CENTURY WELL SERVICE Brine 0 365
2003 CENTURY WELL SERVICE Brine 0 365
2004 CENTURY WELL SERVICE Brine 0 365
2005 CENTURY WELL SERVICE Brine 0 365
2006 CENTURY WELL SERVICE Brine 0 365
2007 BROAD STREET SERV LLC Brine 0 365
2008 BROAD STREET SERV LLC Brine 495 0
2009 BROAD STREET SERV LLC Brine 145 0
2010 BROAD STREET SERV LLC Brine 17 0
2011 BROAD STREET SERV LLC Brine 70 0
2012 BROAD STREET SERV LLC Brine 0 0
2013 BROAD STREET SERV LLC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0166028373 2010-04-08 Production Wells No Violations Leak now fixed, well is producing, good IDs, current chart in meter.
0411036982 2010-01-27 Production Wells No Violations Inspection found leak in sales line still not fixed - well not producing.
0764200856 2013-11-04 Plug / Plug Back No Violations Crew was rigging up over well at the time of inspection. We discussed the packer in the well and possible methods of plugging this well.
1104167746 2004-12-27 Production Wells No Violations Inspection this day found well in production, tank down on Yaegers - 100 bbl, current chart in meter, IDs say 9033 which is the shallow well and should be 9081 - turning production in on correct one. Landowner getting house gas
1109438284 2015-09-29 Final Restoration No Violations Location has met 1509.072 B requirements.
1185823730 2013-11-06 Plug / Plug Back No Violations Received phone call from Mr. Donnie Strange stating that they had ripped 4.5 in. casing at a depth of 3069 ft. They plan to run tubing back down and set a 300 ft. plug where they ripped. When I arrived on site, all of the 4.5 in casing had been pulled and hauled off. Crew was getting ready to run tubing back down.
1207976988 2009-12-07 Production Wells Violations Noted

- talked to the men and they knew about it and had a plan to fix so will give a couple weeks to correct problems on this well. Plug or produce. Fix erosion on lease road.

1315333004 2011-09-06 Production Wells Violations Noted Inspection this day found well with jack, not capable of producing. Jack has no motor, lines not connected to sales line. Tank has good IDs, no chart in meter. Annual production shows well has not produced since 2007. Sales line to tank (which is on Mr. Whiteds land) is not buried, Mr. Mike Whited says that is a requirement of his lease and wants line buried or removed. Well needs plugged or produced, put in TI, IDs needed at well, annual production should be submitted by now for 2010.
1374368194 2005-02-01 Preliminary Restoration No Violations Drill site has been reclaimed
1383896920 2013-11-07 Plug / Plug Back No Violations Berrys well service had ripped pipe at 3050. They pulled all 4.5 casing out and ran 2.375upset tubing back to depth of 2989. Cemenco set cement plugs and J&L Water service supplied water. They set plug at 2989-2689 for the Big Lime plug. The set plug of 66 sacks at 14.1Lb/Gal. Berea plug was set 1790-1629 and ran 36 sacks at 14.1LB/Gal. Then set plug at Bottom of surface 1567-1367. They ran 45 sacks of cement at 14.1 Lb/Gal. The Top Plug was set at 100-0. They ran 25 sacks at 14.1 Lb/ Gal after setting a bridge plug at 350. None of the plugs circulated. The cement did not fall back.
1538105052 2013-11-05 Plug / Plug Back No Violations Witnessed wireline operations on this plug job. Tubing was shot off at 4756 ft. Well started unloading gas and fluid. Cementers hooked up their pump truck and pumped down the tubing to circulate gas out. After that, a 35 sack plug was pumped down hole.
1597439749 2011-09-06 Production Wells No Violations FOLLOW UP TO NOV # 1315333004 Inspection this day found well with jack, not capable of producing. Jack has no motor, lines not connected to sales line. Tank has good IDs, no chart in meter. Annual production shows well has not produced since 2007. Sales line to tank (which is on Mr. Whiteds land) is not buried, Mr. Mike Whited says that is a requirement of his lease and wants line buried or removed. Well needs plugged or produced, put in TI, IDs needed at well, annual production should be submitted by now for 2010.
2122552789 2018-09-07 Field Inspected, Well Not Found No Violations On this day, I am conducting an inspection per request of landowner Jeff Kephart. I was accompanied by Mr. Kephart during the inspection. He inquired about building a new household near the previously plugged well.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
1207976988 US-OH-105438 2009-12-11 Well shall be plugged
1315333004 US-OH-108971 2011-09-07 Failure to properly bury pipeline
1315333004 US-OH-108972 2011-09-07 Failure to legibly identify well
1315333004 US-OH-108973 2011-09-07 Nonproduction; well shall be plugged or placed in temporary inactive status
1315333004 US-OH-108974 2011-09-07 Statement of annual production not filed

For data sources see[9]

References