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Difference between revisions of "34-007-20988"

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| County: [[Ashtabula_County,_Ohio|Ashtabula]]
 
| County: [[Ashtabula_County,_Ohio|Ashtabula]]
 
|-
 
|-
| Municipality: [[Trumbull_Township,_Ashtabula_County,_Ohio|Trumbull Township]]
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| Municipality: [[Trumbull Township,_Ashtabula_County,_Ohio|Trumbull Township]]
 
|-
 
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| Operator Name: [[BIG SKY ENERGY INC]]
 
| Operator Name: [[BIG SKY ENERGY INC]]

Revision as of 03:51, 14 August 2019

Well Details

Well ID: 34-007-20988
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Country: United States
State: Ohio
County: Ashtabula
Municipality: Trumbull Township
Operator Name: BIG SKY ENERGY INC
Well Pad ID:
Farm/Lease Name: FORBES L& L
License Status: Producing
License Date: 1978-10-04
Spud Date: 1978-11-13
Spud Drilling Contractor:
Final Drill Date: 1978-11-19
Well Total Depth: 3530 ft
Configuration: Vertical
Latitude: 41.650936830
Longitude: -80.91704042

For data sources see[1]

Well History

Well Status Well Status Date Comment
CO 1978-10-04 300 PETROLEUM ENERGY PROD COR GeoDate 10/4/78
Original Spud 1978-11-13 UPDATED LOCATION TO SURVEYOR COORDINATES ALE 12/14/2016.
Completed 1978-11-19 UPDATED LOCATION TO SURVEYOR COORDINATES ALE 12/14/2016.
Reached Total Depth 1978-11-19 UPDATED LOCATION TO SURVEYOR COORDINATES ALE 12/14/2016.
CO 1991-10-09 201 GREEN GAS CO GeoDate 10/4/78
Change of Owner 1991-11-05 Operator changed from 201, GREEN GAS CO to 1453, GREEN ENERGY INC
Change of Owner 2001-02-07 Operator changed from 1453, GREEN ENERGY INC to 1333, BARR ROBT/dba BIG SKY PET
Record Last Modified 2017-02-10 UPDATED LOCATION TO SURVEYOR COORDINATES ALE 12/14/2016.

For data sources see[2]

Perforation Treatments

Perforation Date Interval Top (ft) Interval Base (ft) Number of Shots
2006-09-11 3305 3358 0

For data sources see[3]

Stimulations Data

Stimulation Date Chemical Agent Chemical Agent Concentration (%) Fracking Fluid Volume Mass of Proppant Used (lb) Fracking Company Comments
H2O 0 860 Bbl 90000

For data sources see[4]

Production Data

Period Operator Name Gas Quantity (mcf) Oil Quantity (bbl) Production Days
1985 EVERFLOW EASTERN PTNS L P 1474 0 214
1986 EVERFLOW EASTERN PTNS L P 1107 0 365
1987 EVERFLOW EASTERN PTNS L P 0 0 365
1988 EVERFLOW EASTERN PTNS L P 0 0 365
1989 EVERFLOW EASTERN PTNS L P 0 0 365
1990 EVERFLOW EASTERN PTNS L P 0 0 365
1991 GREEN ENERGY INC 0 0 365
1992 GREEN ENERGY INC 1881 0 323
1993 GREEN ENERGY INC 2789 0 365
1994 GREEN ENERGY INC 1591 0 365
1995 GREEN ENERGY INC 50 0 150
1996 GREEN ENERGY INC 16 0 61
1997 GREEN ENERGY INC 22 0 365
1998 GREEN ENERGY INC 15 0 61
1999 GREEN ENERGY INC 21 0 61
2000 GREEN ENERGY INC 19 0 61
2001 BIG SKY ENERGY INC 0 0 0
2002 BIG SKY ENERGY INC 0 0 365
2003 BIG SKY ENERGY INC 0 0 0
2004 BIG SKY ENERGY INC 0 0 0
2005 BIG SKY ENERGY INC 0 0 0
2006 BIG SKY ENERGY INC 0 0 365
2007 BIG SKY ENERGY INC 0 0 0
2008 BIG SKY ENERGY INC 0 0 0
2009 BIG SKY ENERGY INC 0 0 365
2010 BIG SKY ENERGY INC 0 0 0
2011 BIG SKY ENERGY INC 0 0 0
2012 BIG SKY ENERGY INC 0 0 0
2013 BIG SKY ENERGY INC 0 0 250
2014 BIG SKY ENERGY INC 0 0 0
2016 BIG SKY ENERGY INC 0 0 0
2017 BIG SKY ENERGY INC 0 0 0

For data sources see[5] [6]

Waste Data

Period Operator Name Waste Type Quantity (bbl) Production Days
1985 EVERFLOW EASTERN PTNS L P Brine 102 214
1986 EVERFLOW EASTERN PTNS L P Brine 0 365
1987 EVERFLOW EASTERN PTNS L P Brine 0 365
1988 EVERFLOW EASTERN PTNS L P Brine 0 365
1989 EVERFLOW EASTERN PTNS L P Brine 0 365
1990 EVERFLOW EASTERN PTNS L P Brine 0 365
1991 GREEN ENERGY INC Brine 173 365
1992 GREEN ENERGY INC Brine 463 323
1993 GREEN ENERGY INC Brine 517 365
1994 GREEN ENERGY INC Brine 61 365
1995 GREEN ENERGY INC Brine 0 150
1996 GREEN ENERGY INC Brine 0 61
1997 GREEN ENERGY INC Brine 0 365
1998 GREEN ENERGY INC Brine 0 61
1999 GREEN ENERGY INC Brine 0 61
2000 GREEN ENERGY INC Brine 0 61
2001 BIG SKY ENERGY INC Brine 0 0
2002 BIG SKY ENERGY INC Brine 0 365
2003 BIG SKY ENERGY INC Brine 0 0
2004 BIG SKY ENERGY INC Brine 0
2005 BIG SKY ENERGY INC Brine 0 0
2006 BIG SKY ENERGY INC Brine 0 365
2007 BIG SKY ENERGY INC Brine 0 0
2008 BIG SKY ENERGY INC Brine 0 0
2009 BIG SKY ENERGY INC Brine 0 365
2010 BIG SKY ENERGY INC Brine 0
2011 BIG SKY ENERGY INC Brine 0 0
2012 BIG SKY ENERGY INC Brine 0 0
2013 BIG SKY ENERGY INC Brine 0 250
2014 BIG SKY ENERGY INC Brine 0 0
2016 BIG SKY ENERGY INC Brine 0 0
2017 BIG SKY ENERGY INC Brine 0 0

For data sources see[7] [8]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
0122661702 2015-10-02 Production Wells No Violations I was on site to take photos per request from Supervisor Hill.
0211133937 2016-11-25 Plug / Plug Back No Violations I arrived on site to find Charles Mosio and one crewman in the prcess in repairing the transmission on the drawworks.
0306255610 2016-11-18 Plug / Plug Back No Violations I arrived on site to find they were able to attach the overshot to what they believed was 1.5 inch tubing. They made several attempts to pull the tubing string but it was hung in the production casing. The transmission began to overheat to the point they could not pull any tension on the tubing string. I then left the site.
0405118391 2018-02-07 Production Wells No Violations I inspected this producing well as a follow-up to Chiefs Order #14-133, dated May 15, 2014 which had directed the owner to plug the well within 30 days of the date of the Order. At the time of this inspection, I noted the following. The service rig that had been positioned at the well for plugging activity remained at the site. There was no longer tubing left in the slips. The site otherwise appeared unchanged, with pipe trailer and tracked dozer left on site. I contacted contractor Charles Mosio who reported that no work had taken place since the tubing had become hung in the hole in the early fall of 2017. He reports that in addition to the stuck tubing, mechanical problems with the rig have delayed completion of the plugging and abandonment. He did not have an estimate on when the work would resume.
0420188061 2017-02-01 Plug / Plug Back No Violations My inspection found no activity for completion in plugging this well at this time.
0435683266 2016-12-29 Plug / Plug Back No Violations My inspection of this well found there was no activity at the well.
0455599272 2016-12-16 Plug / Plug Back No Violations My inspection of this well found there no activity at this time.
0537602927 2013-05-01 Production Wells No Violations Myself and Supervisor Hill inspected well . The inspection found the 210 barrel steel producton tank has been emptied of all the fluids . There has been no action from the company to plug the well .
0578892600 2016-11-09 Plug / Plug Back No Violations I arrived on site to find the rig crew was able to pull free of the tubing to find after the tubing with the overshot was recovered the jaws in the overshot had shattered. They were unable to recover any tubing from the well. They replaced the jaws in the overshot and then run back into the well with the overshot on the two inch tubing. They were able to attach the overshot onto the lost tubing only to find it was still hung in the well. They pulled tension on the tubing and then set it in the tubing slips. They left tension on the tubing and left the site.
0784863882 2017-09-21 Production Wells No Violations I inspected this producing well as a follow-up to Chiefs Order #14-133, dated May 15, 2014 which had directed the owner to plug the well within 30 days of the date of the Order. At the time of this inspection I observed the following: a service rig appears to have been abandoned at the wellhead, in mid-plugging process with 2.375-inch tubing in the hole and sitting in the slips. The production casing is packed off with no discernible leaks. The wellhead area, including the service rig, had become overgrown with vegetation, The tank battery is largely obscured by dense vegetation. Other idle tools and equipment left at the site include a pipe trailer with several joints of 2.375-inch tubing, another pipe trailer with several joints of 1.625-inch tubing, and a small tracked bulldozer.
0785677022 2017-01-18 Plug / Plug Back No Violations My inspection found there was no activity for plugging this well at the time of my inspection. The service rig was still rigged up over the well bore.
0792753657 2016-11-17 Plug / Plug Back No Violations I arrived on site to find Charles Mosio and one crewman rigging up the sand line to run into the production casing. They run into the well to a depth of 2627 feet when they tagged an obstruction. They then pulled the sand line from the well. They began running the two inch tubing with the overshot into the production casing. They run the tubing with the overshot into the well till they set down on the obstruction. They were attempting to attach the overshot to the obstruction when I left the site.
0816099676 2016-12-05 Plug / Plug Back No Violations I met Rob Lowe on site. Rob took a gps reading of the well casing location. The service rig was rigged up over the well. The draw works transmission was partially taken apart.
0848888368 2005-03-23 Production Wells No Violations no violations .
0868905758 2012-09-09 Production Wells Violations Noted Complaintant [ Karen Forbes , landowner ] . My inspection found tank battery contained one 210 barrel steel production tank , one separator , there is vegetation growing inside dike area to point access is at a minimum . Further inspection of wellhead and well site area found tubing in production casing with valve which is shut-in , also well is dissconnected from flowline . There is three joints of tubing lying on ground near wellhead . Division records showed 0 production was reported since 2001 . Well is idle at this time . I contacted Bob Barr Jr. and advised him of corrective action needed to comply , He told me Karen had taken them to court to obtain ownership of well and he was under the understanding they turned well over to her . I then advised him Karen had told me a similar story but had refused to take ownership of well , Bob then told me he would put well into production . REMEDIAL WORK REQUIRED TO COMPLY : PLUG OR PRODUCE WELL .
1192718057 2016-08-26 Production Wells No Violations On site with DOGRM Inspection Mike Dinsmore, no action has taken place by the owner of the well to plug the well.
1370476422 2016-11-07 Plug / Plug Back No Violations I arrived on site to find Charles Mosio and one crewman trying to pull the hung tubing in the well. They were unsuccessful in retrieving the hung tubing. Charles then pulled tension on the string of tubing and set it in the tubing slips. Charles was loading the well with fresh water when I left the site. Charles was going to load the well with fresh water and leave it overnight with tension on the tubing string.
1376066616 2013-07-05 Production Wells No Violations Inspection of the well found there has not been any action from the company to plug the well . The company has not yet applied for a plugging permit for this well .
1393158732 2014-05-07 Production Wells No Violations My inspection found there has been no action to plug this well pursuant to chiefs order # 2014-133 .
1414595248 2014-10-28 Production Wells No Violations I was on location for a follow---
1463483848 2016-05-13 Production Wells No Violations Myself and Tom Hill inspected this well to find there has been no action from the company to plug and abandon the well since the last inspection on 10-2-2016.
1485014124 2016-11-04 Plug / Plug Back No Violations I arrived on site to find a service rig rigged up over the well bore. Charles Mosio and one crewman was preparing to start pulling the tubing from the well. They pulled one joint of two inch tubing to find the production casing was open. They then rigged up a impression block onto the two tubing. They went into the production casing to a depth of 140 feet when they set down on an obstruction. They then pulled the tubing with the impression block. The impression showed they had set down on a collar on 1.5 inch tubing. I took one photo of the impression block. They then rigged up the overshot onto the tubing and run into the production casing till they set down on the 1.5 inch tubing. They set down several times when they were able to attach the overshot to the 1.5 inch tubing. They started to pull the tubing with the overshot to find the tubing was hung in the well. They attempted to turn the tubing with the power tongs when the power tongs failed to work. They were in the process in trying to repair the power tongs when I left the site.
1485098596 2016-11-10 Plug / Plug Back No Violations I arrived on site to find the tubing was still hung in the production casing. The company was in the process in loading the well with fresh water.
1485101616 2016-11-14 Plug / Plug Back No Violations I arrived on site to find the company was able to retrieve one joint of 1.5 inch tubing. They then run the two inch tubing which was open ended. They run 160 feet into well and set down on the 1.5 inch tubing. They the run the sand line into the tubing to about 2000 feet when they come upon a very bad kink in the sand line. They were in the process in repairing the sand line when I left the site.
1490714922 2017-01-26 Plug / Plug Back No Violations My inspection found there was no activity for completion of plugging this well at this time.
1520959005 2018-03-08 Production Wells No Violations I inspected this well as a follow-up to Chiefs Order #14-133, dated May 15, 2014 which had directed the owner to plug the well within 30 days of the date of the Order. At the time of this inspection the service rig was still located at the wellhead. The 2.375-inch tubing that was identified in previous inspections as being in the slips, was gone. Plugging operations have not been completed on this well and the site not reclaimed. The 210 BBL production tank and mechanical separator remain on location. Other equipment left at the site, include a pipe trailer with several joints of 2.375-inch tubing, a pipe trailer with several joints of 1.625-inch tubing, and a small tracked bulldozer.
1537112794 2015-03-19 Production Wells No Violations My inspection of this well found there has been no action to plug this well pursuant to Chiefs Order # 2014-133.
1955562839 2017-09-12 Plug / Plug Back No Violations On location to follow-up on Chiefs order 2014-133 and Court Order to plug the well. At the time of my inspection Big Sky Energy Incs service rig remains over the hole with tubing hanging in the hole and from the mast. The well is open to atmosphere, it is not packed off. Plugging operations remain incomplete. Operator has a parted fishing tool and tubing down hole that has not been removed from the hole. Two pipe trailers and a dozer were also on location. Permit to plug expired 08/18/2017, the operator will need to apply for a new permit before plugging operations can resume. A 210 production tank and a mechanical separator remain in the tank battery. Site conditions were dry.
1966682716 2017-07-14 Plug / Plug Back No Violations At the time of my inspection a service rig is still staged over the well. There is a string of tubing in the well, held suspend by the rig. Tongs are hanging next to the tubing. Well is open to atmosphere. Two pipe trailers are staged to the east of the well. Model 70 dozer is on location. The water truck has been removed since last inspection, The 210 barrel production tank is still on location. Well remains unplugged.
2023486498 2016-11-16 Plug / Plug Back No Violations I arrived on site to find Charles Mosio and one crewman pulling the 1.5 inch tubing from the well. They pulled a total of 77 joints of 1.5 inch tubing from the well. They tallied the 1.5 inch tubing to find they had recovered 2640 feet of tubing. The bottom joint had no threads on it. Myself and the rig crew then left the site.
2023654799 2016-11-15 Plug / Plug Back No Violations I arrived on site to find Bob Barr Sr. running the service rig. They pulled the tubing from the well and attached the overshot the two inch tubing. They then run into the production casing with the two inch tubing with the overshot. They set down on the 1.5 inch tubing and was able to attach the overshot to the lost tubing. The tubing was still hung in the production casing. They then pulled tension on the string of tubing an attempted to unscrew the 1.5 inch tubing. They pulled on the tubing string to find the string was free. They pulled the tubing with the overshot to find they had recovered the 1.5 inch tubing. There was a homemade overshot attached to the 1.5 inch tubing string. They removed the overshot from the 1.5 inch tubing. I took 5 photos of the homemade overshot. They were beginning to pull the 1.5 inch tubing when I left the site.
2077927897 2016-12-27 Plug / Plug Back No Violations There was no activity at this well at the time of my inspection.
2078426313 2014-10-16 Production Wells No Violations My inspection of this well found there has been no action to plug this well pursuant to Chiefs Order # 2014-133. I spoke with Bob Barr Sr. , he told me there is no current plan to plug this well due to financial difficultys.

Violations Commited

Inspection ID Violation ID Violation Date Violation Code Violation Comments
0868905758 US-OH-129886 2013-08-27 Defective casing, leaking well

For data sources see[9]

References