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| County: [[Athens_County,_Ohio|Athens]] | | County: [[Athens_County,_Ohio|Athens]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Trimble Township,_Athens_County,_Ohio|Trimble Township]] |
|- | |- | ||
| Operator Name: [[ROULETTE ENERGY LLC]] | | Operator Name: [[ROULETTE ENERGY LLC]] |
Well ID: 34-009-23049 | Loading map...
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Country: United States | |
State: Ohio | |
County: Athens | |
Municipality: Trimble Township | |
Operator Name: ROULETTE ENERGY LLC | |
Well Pad ID: | |
Farm/Lease Name: SUNDAY CREEK COAL CO | |
License Status: Producing | |
License Date: 1984-05-18 | |
Spud Date: 1984-09-18 | |
Spud Drilling Contractor: BOWMAN DRILLING | |
Final Drill Date: 1984-10-20 | |
Well Total Depth: 3818 ft | |
Configuration: Vertical | |
Latitude: 39.504459814 | |
Longitude: -82.13213239 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1984-05-18 | Issued Date 5/18/84 Expired Date 11/14/84 Acres 0266000 Tool Type CT Proposed Formation CLINTON Proposed Depth 03818 Proposed Drill Depth 03818 |
Original Spud | 1984-09-18 | |
Completed | 1984-10-20 | |
Reached Total Depth | 1984-10-20 | |
Construction Permit Expires | 1984-11-14 | |
CO | 1984-11-15 | 133 QUAKER STATE OIL REF CORP GeoDate 5/18/84 |
Completion Report Received | 1985-01-18 | |
CO | 1995-10-18 | 182 BELDEN & BLAKE CO GeoDate 5/18/84 |
Change of Owner | 2002-08-06 | Operator changed from 182, BELDEN & BLAKE CORPORATION to 1966, PETROX INC |
Change of Owner | 2015-08-05 | Operator changed from 1966, PETROX, INC to 8373, ROULETTE ENERGY LLC |
Last Compliance Report | 2016-05-06 | |
Record Last Modified | 2017-02-15 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 3770 | 3802 | 0 |
2006-09-11 | 3771 | 3786 | 31 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
H2O | 0 | 2640 Bbl | 44000 | FRAC: H2O,SAND |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | QUAKER STATE OIL REF CORP | 6185 | 1348 | 365 |
1986 | QUAKER STATE OIL REF CORP | 6441 | 1021 | 365 |
1987 | QUAKER STATE OIL REF CORP | 4595 | 635 | 365 |
1988 | QUAKER STATE OIL REF CORP | 3088 | 478 | 365 |
1989 | QUAKER STATE OIL REF CORP | 2411 | 453 | 365 |
1990 | QUAKER STATE OIL REF CORP | 2169 | 339 | 365 |
1991 | QUAKER STATE OIL REF CORP | 1392 | 228 | 365 |
1992 | QUAKER STATE OIL REF CORP | 1101 | 210 | 365 |
1993 | QUAKER STATE OIL REF CORP | 1137 | 193 | 365 |
1994 | QUAKER STATE OIL REF CORP | 801 | 156 | 365 |
1995 | BELDEN & BLAKE CORPORATION | 263 | 0 | 123 |
1996 | BELDEN & BLAKE CORPORATION | 620 | 0 | 341 |
1997 | BELDEN & BLAKE CORPORATION | 676 | 275 | 295 |
1998 | BELDEN & BLAKE CORPORATION | 1158 | 36 | 241 |
1999 | BELDEN & BLAKE CORPORATION | 1458 | 0 | 271 |
2000 | BELDEN & BLAKE CORPORATION | 1372 | 9 | 342 |
2001 | BELDEN & BLAKE CORPORATION | 2435 | 0 | 346 |
2002 | PETROX, INC | 274 | 0 | 365 |
2003 | PETROX, INC | 1282 | 31 | 365 |
2004 | PETROX, INC | 654 | 70 | 365 |
2005 | PETROX, INC | 516 | 37 | 365 |
2006 | PETROX, INC | 449 | 28 | 365 |
2007 | PETROX, INC | 398 | 15 | 365 |
2008 | PETROX, INC | 312 | 15 | 365 |
2009 | PETROX, INC | 457 | 136 | 365 |
2010 | PETROX, INC | 410 | 187 | 365 |
2011 | PETROX, INC | 321 | 123 | 365 |
2012 | PETROX, INC | 220 | 94 | 366 |
2013 | PETROX, INC | 267 | 125 | 365 |
2014 | PETROX, INC | 170 | 80 | 365 |
2015 | PETROX, INC | 82 | 38 | 240 |
2016 | ROULETTE ENERGY LLC | 226 | 77 | 365 |
2017 | ROULETTE ENERGY LLC | 146 | 12 | 365 |
2018 | ROULETTE ENERGY LLC | 126 | 12 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1985 | QUAKER STATE OIL REF CORP | Brine | 815 | 365 |
1986 | QUAKER STATE OIL REF CORP | Brine | 1460 | 365 |
1987 | QUAKER STATE OIL REF CORP | Brine | 698 | 365 |
1988 | QUAKER STATE OIL REF CORP | Brine | 711 | 365 |
1989 | QUAKER STATE OIL REF CORP | Brine | 600 | 365 |
1990 | QUAKER STATE OIL REF CORP | Brine | 400 | 365 |
1991 | QUAKER STATE OIL REF CORP | Brine | 267 | 365 |
1992 | QUAKER STATE OIL REF CORP | Brine | 217 | 365 |
1993 | QUAKER STATE OIL REF CORP | Brine | 1390 | 365 |
1994 | QUAKER STATE OIL REF CORP | Brine | 1961 | 365 |
1995 | BELDEN & BLAKE CORPORATION | Brine | 0 | 123 |
1996 | BELDEN & BLAKE CORPORATION | Brine | 694 | 341 |
1997 | BELDEN & BLAKE CORPORATION | Brine | 560 | 295 |
1998 | BELDEN & BLAKE CORPORATION | Brine | 346 | 241 |
1999 | BELDEN & BLAKE CORPORATION | Brine | 488 | 271 |
2000 | BELDEN & BLAKE CORPORATION | Brine | 492 | 342 |
2001 | BELDEN & BLAKE CORPORATION | Brine | 232 | 346 |
2002 | BELDEN & BLAKE CORPORATION | Brine | 0 | 0 |
2003 | PETROX, INC | Brine | 1049 | 365 |
2004 | PETROX, INC | Brine | 586 | 365 |
2005 | PETROX, INC | Brine | 366 | 365 |
2006 | PETROX, INC | Brine | 91 | 365 |
2007 | PETROX, INC | Brine | 365 | |
2008 | PETROX, INC | Brine | 116 | 365 |
2009 | PETROX, INC | Brine | 201 | 365 |
2010 | PETROX, INC | Brine | 114 | 365 |
2011 | PETROX, INC | Brine | 26 | 365 |
2012 | PETROX, INC | Brine | 18 | 366 |
2013 | PETROX, INC | Brine | 23 | 365 |
2014 | PETROX, INC | Brine | 36 | 365 |
2015 | PETROX, INC | Brine | 1 | 240 |
2016 | ROULETTE ENERGY LLC | Brine | 15 | 365 |
2017 | ROULETTE ENERGY LLC | Brine | 0 | 365 |
2018 | ROULETTE ENERGY LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
0984432832 | 2005-02-24 | Annular Disposal | No Violations | The well is not equipped for annular disposal. There were no violations at the time of inspection. |
1178082288 | 2016-03-24 | Temporary Abandoned Annular Disposal | No Violations | Visual inspection of well head found no AD hook up was present. AD is not in use. |
1552077665 | 2007-09-28 | Annular Disposal | No Violations | The well was not equipped for annular disposal. |
2139212089 | 2016-03-24 | Production Wells | No Violations | Pumping unit had no electric motor. The electric line was severed in several spot along the path to the well. Production and 4 1/2 valves were open. One side of the 4 1/2 was open and gas could be seen ventiing into the air. Will find out the pumpers name and have them place a cap on the 2. |
For data sources see[9]