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| County: [[Mahoning_County,_Ohio|Mahoning]] | | County: [[Mahoning_County,_Ohio|Mahoning]] | ||
|- | |- | ||
− | | Municipality: [[ | + | | Municipality: [[Goshen Township,_Mahoning_County,_Ohio|Goshen Township]] |
|- | |- | ||
| Operator Name: [[STEPHEN J SVETLAK LLC]] | | Operator Name: [[STEPHEN J SVETLAK LLC]] |
Well ID: 34-099-21690 | Loading map...
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Country: United States | |
State: Ohio | |
County: Mahoning | |
Municipality: Goshen Township | |
Operator Name: STEPHEN J SVETLAK LLC | |
Well Pad ID: | |
Farm/Lease Name: MCCRACKEN UNIT | |
License Status: Producing | |
License Date: 1984-06-05 | |
Spud Date: 1984-06-04 | |
Spud Drilling Contractor: PERKINS DRLG | |
Final Drill Date: 1984-06-16 | |
Well Total Depth: 5650 ft | |
Configuration: Vertical | |
Latitude: 40.917078169 | |
Longitude: -80.94023648 |
For data sources see[1]
Well Status | Well Status Date | Comment |
---|---|---|
Oil and Gas | 1983-12-22 | Issued Date 12/22/83 Expired Date 6/19/84 Acres 0045370 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 00000 Proposed Drill Depth 00000 |
CO | 1984-06-05 | 457 ALSID OIL & GAS GeoDate 6/5/84 |
Oil and Gas | 1984-06-05 | Issued Date 6/5/84 Expired Date 12/2/84 Acres 0045370 Tool Type RTAF Proposed Formation CLINTON Proposed Depth 05650 Proposed Drill Depth 05650 |
Original Spud | 1984-06-07 | R.I. 6-9-84 |
Completed | 1984-06-16 | R.I. 6-9-84 |
Reached Total Depth | 1984-06-16 | R.I. 6-9-84 |
CO | 1984-07-12 | 457 ALSID OIL & GAS GeoDate 12/22/83 |
Construction Permit Expires | 1984-12-02 | R.I. 6-9-84 |
Completion Report Received | 1985-06-17 | R.I. 6-9-84 |
Change of Owner | 2002-09-25 | Operator changed from 457, ALSID OIL & GAS to 6791, NORMAN D INVESTMENTS |
Change of Owner | 2005-03-14 | Operator changed from 6791, NORMAN D INVESTMENTS to 7773, SVETLAK STEPHEN J LLC |
Last Compliance Report | 2016-11-10 | R.I. 6-9-84 |
Record Last Modified | 2017-02-15 | R.I. 6-9-84 |
For data sources see[2]
Perforation Date | Interval Top (ft) | Interval Base (ft) | Number of Shots |
---|---|---|---|
1997-06-29 | 5490 | 5572 | 0 |
2006-09-11 | 5501 | 5571 | 38 |
For data sources see[3]
Stimulation Date | Chemical Agent | Chemical Agent Concentration (%) | Fracking Fluid Volume | Mass of Proppant Used (lb) | Fracking Company | Comments |
---|---|---|---|---|---|---|
N2 | 0 | 1830 Mscf | 82500 | FRAC;H2O,SAND,N2 |
For data sources see[4]
Period | Operator Name | Gas Quantity (mcf) | Oil Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ALSID OIL & GAS | 1429 | 317 | 365 |
1985 | ALSID OIL & GAS | 1587 | 476 | 0 |
1986 | ALSID OIL & GAS | 259 | 171 | 280 |
1987 | ALSID OIL & GAS | 181 | 49 | 365 |
1988 | ALSID OIL & GAS | 8 | 0 | 183 |
1990 | ALSID OIL & GAS | 0 | 0 | 0 |
1991 | ALSID OIL & GAS | 0 | 0 | 365 |
1992 | ALSID OIL & GAS | 0 | 0 | 365 |
1993 | ALSID OIL & GAS | 0 | 0 | 0 |
1994 | ALSID OIL & GAS | 0 | 61 | 0 |
1997 | ALSID OIL & GAS | 0 | 0 | 0 |
1998 | ALSID OIL & GAS | 0 | 0 | 365 |
1999 | ALSID OIL & GAS | 0 | 0 | 365 |
2000 | VANGUARD OIL & GAS LLC | 0 | 0 | 365 |
2001 | VANGUARD OIL & GAS LLC | 0 | 0 | 365 |
2002 | CONSORTIUM ENERGY LLC | 0 | 0 | 0 |
2003 | CONSORTIUM ENERGY LLC | 0 | 0 | 0 |
2014 | STEPHEN J SVETLAK LLC | 0 | 0 | 365 |
2015 | STEPHEN J SVETLAK LLC | 0 | 0 | 365 |
2016 | STEPHEN J SVETLAK LLC | 0 | 0 | 365 |
Period | Operator Name | Waste Type | Quantity (bbl) | Production Days |
---|---|---|---|---|
1984 | ALSID OIL & GAS | Brine | 0 | 365 |
1985 | ALSID OIL & GAS | Brine | 816 | 0 |
1986 | ALSID OIL & GAS | Brine | 210 | 280 |
1987 | ALSID OIL & GAS | Brine | 93 | 365 |
1988 | ALSID OIL & GAS | Brine | 0 | 183 |
1990 | ALSID OIL & GAS | Brine | 105 | 0 |
1991 | ALSID OIL & GAS | Brine | 0 | 365 |
1992 | ALSID OIL & GAS | Brine | 0 | 365 |
1993 | ALSID OIL & GAS | Brine | 0 | 0 |
1994 | ALSID OIL & GAS | Brine | 20 | 0 |
1997 | ALSID OIL & GAS | Brine | 0 | 0 |
1998 | ALSID OIL & GAS | Brine | 0 | 365 |
1999 | ALSID OIL & GAS | Brine | 0 | 365 |
2000 | VANGUARD OIL & GAS LLC | Brine | 0 | 365 |
2001 | VANGUARD OIL & GAS LLC | Brine | 0 | 365 |
2002 | CONSORTIUM ENERGY LLC | Brine | 0 | 0 |
2003 | CONSORTIUM ENERGY LLC | Brine | 0 | 0 |
2014 | STEPHEN J SVETLAK LLC | Brine | 0 | 365 |
2015 | STEPHEN J SVETLAK LLC | Brine | 0 | 365 |
2016 | STEPHEN J SVETLAK LLC | Brine | 0 | 365 |
Inspection ID | Inspection Date | Inspection Type | Inspection Result | Inspection Comments |
---|---|---|---|---|
000PL12988 | Preliminary Restoration | No Violations | Preliminary Restoration done information from Data Point | |
0697369713 | 2014-09-22 | Production Wells | No Violations | I performed a follow up inspection on the above location. On 4/1/2013, there was a Compliance Notice issued on this well. As of this date, 9/22/2014 this well is shut in. The 4 wellhead and flow line valves are shut. This well has not been swabbed. Last recorded production was 2003. Well shall be plugged. |
1208100939 | 2016-09-07 | Annular Disposal | No Violations | I performed a TAAD inspection of the wellhead and the tank battery. The well is equipped with 4.5 casing. No visual signs of annular disposal was present. No production equipment at this location. |
1246645400 | 2010-11-22 | Production Wells | No Violations | I performed a TAAD inspection of the wellhead and the tank battery. I GPSd both the tank battery and the wellhead. I inspected around the wellhead and found no signs of annular disposed fluids. The tank battery area was set up for gas/stock tank. No visual signs of annular disposal was present. There were no violations at this time. |
1365428888 | 2013-04-01 | Production Wells | Violations Noted | I performed a status check on the above location. The tank battery has one 210 barrel tank no separator. This is a 4.5 swab well all flow line values are shut. The last reported production was in 1993. Well should be plugged. This well shares the same tank battery as (34099216910000) McCracken #1. |
1381931636 | 2013-09-01 | Production Wells | No Violations | I performed a follow up inspection on the above location. On 4/1/2013 I issued a Compliance Notice and on 9/25/2013 a Chief Order for Failure to Maintain Liability Insurance. Order No. 2013-136. |
1434653448 | 2014-06-18 | Production Wells | No Violations | I performed a follow up inspection on this well. A Compliance Notice was issued (1365428888) on 4/1/2013 to plug this well by 6/1/2013 and a Chiefs Order was issued on 3/24/2015 ( 2015-123). Upon my inspection I found the well to be equipped with 4.5 casing with a 4 gate valve on the well casing and a 2 flow line. There is a 2 valve on the flow line. This valve is closed. I notice no sign of any activity at the wellhead. The tank battery is equipped with one 210 barrel tank. There is no separator or meter at the location. At present, this well is incapable of production. |
1494862408 | 2017-05-16 | Production Wells | No Violations | I performed an inspection on the above location. The well is equipped with 4.5 casing with a 4 frac valve. There is one 210 barrel tank no other production equipment is on location, it is shared with (3409921691) McCracken #1. There was a Compliance Notice Issued (#1365428888) on 4/1/2013 and also a Chiefs Order 2015-123 requiring the well to be plugged. There is no ID sign posted at the well or at the tank battery. |
1510170779 | 2017-10-08 | Production Wells | No Violations | I performed a Chief Order ( 2015-123 ) follow up inspection on the above well. The well is equipped with a 4.5 valve. The 2 valve on the flow line is in the closed position. At this time the well is not plugged. |
1516708516 | 2018-01-22 | Production Wells | No Violations | I performed an inspection on the above location. The well is equipped with 4.5 casing with a 4 frac valve. There is one 210 barrel tank no other production equipment is on location, it is shared with (3409921691) McCracken #1. There was a Compliance Notice Issued (#1365428888) on 4/1/2013 and also a Chiefs Order 2015-123 requiring the well to be plugged. There is no ID sign posted at the well or at the tank battery. At this date ( 01/22/2018 ) the well is not plugged. |
1792776493 | 2005-11-16 | Annular Disposal | No Violations | The AD is not hooked up or in use. The tank batttery is shared with permit 1691 and consists of 1-210 bbl storage tank, 1-50 bbl salt water tank and a dike. |
Inspection ID | Violation ID | Violation Date | Violation Code | Violation Comments |
---|---|---|---|---|
1365428888 | US-OH-110727 | 2013-04-11 | Failure to legibly identify well | |
1365428888 | US-OH-110728 | 2013-04-11 | Well shall be plugged |
For data sources see[9]