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Difference between revisions of "34-173-61226"

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| State: Ohio
 
| State: Ohio
 
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| County: [[Wood_County,_Ohio|Wood]]
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| County: <County>
 
|-
 
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| Municipality: [[Plain_Township,_Wood_County,_Ohio|Plain Township]]
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| Municipality: [[Plain Township,_Wood_County,_Ohio|Plain Township]]
 
|-
 
|-
 
| Operator Name: [[ORPHAN WELL PROGRAM]]
 
| Operator Name: [[ORPHAN WELL PROGRAM]]

Revision as of 04:19, 15 August 2019

Well Details

Well ID: 34-173-61226
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Country: United States
State: Ohio
County: <County>
Municipality: Plain Township
Operator Name: ORPHAN WELL PROGRAM
Well Pad ID:
Farm/Lease Name: MCKEE
License Status: Final Restoration
License Date: 2009-07-21
Spud Date:
Spud Drilling Contractor:
Final Drill Date:
Well Total Depth:
Configuration: Vertical
Latitude: 41.387730148
Longitude: -83.69612888

For data sources see[1]

Well History

Well Status Well Status Date Comment
Oil and Gas 2009-03-02 KEN PIISPANEN INSPECTED WELL 2/18/2009. WELL HAS RODS AND TUBING IN PLACE. THE WELL HEAD HAS TWO OPENINGS WHERE PIPIES WERE ATTACHED AT ONE TIME. NO SIGN OF LEAKING OR CONTAMINATION AT THE WELL HEAD. WELL MAY BE PLUGGED AS PART OF THE PROJECT TO PLUG SEVERAL WELLS INCLUDE THE ONE TO THE EAST (PERMIT #61225).
APP 2009-07-21 Proposed Formations:, Issued Date:7/21/2009, Expired Date:7/21/2010 6:00:00 AM, Drilling unit acres:0, Proposed Well Type:OG, Proposed Well Class:
Plugged by Orphan Well Program 2009-07-27 Plugged by Orphan Well Program
Plugged/Abandoned 2009-07-27 KEN PIISPANEN INSPECTED WELL 2/18/2009. WELL HAS RODS AND TUBING IN PLACE. THE WELL HEAD HAS TWO OPENINGS WHERE PIPIES WERE ATTACHED AT ONE TIME. NO SIGN OF LEAKING OR CONTAMINATION AT THE WELL HEAD. WELL MAY BE PLUGGED AS PART OF THE PROJECT TO PLUG SEVERAL WELLS INCLUDE THE ONE TO THE EAST (PERMIT #61225).

I&O CN 2009 03 005

Construction Permit Expires 2010-07-21 KEN PIISPANEN INSPECTED WELL 2/18/2009. WELL HAS RODS AND TUBING IN PLACE. THE WELL HEAD HAS TWO OPENINGS WHERE PIPIES WERE ATTACHED AT ONE TIME. NO SIGN OF LEAKING OR CONTAMINATION AT THE WELL HEAD. WELL MAY BE PLUGGED AS PART OF THE PROJECT TO PLUG SEVERAL WELLS INCLUDE THE ONE TO THE EAST (PERMIT #61225).

I&O CN 2009 03 005

Record Last Modified 2019-06-14 KEN PIISPANEN INSPECTED WELL 2/18/2009. WELL HAS RODS AND TUBING IN PLACE. THE WELL HEAD HAS TWO OPENINGS WHERE PIPIES WERE ATTACHED AT ONE TIME. NO SIGN OF LEAKING OR CONTAMINATION AT THE WELL HEAD. WELL MAY BE PLUGGED AS PART OF THE PROJECT TO PLUG SEVERAL WELLS INCLUDE THE ONE TO THE EAST (PERMIT #61225).

I&O CN 2009 03 005

For data sources see[2]

Inspection Data

Inspections Performed

Inspection ID Inspection Date Inspection Type Inspection Result Inspection Comments
1248120179 2009-07-20 Orphan No Violations Operator Tony Krieder on site at McKee well #2. Brush and debris removed from around well head. Rods being removed from well. Pit being excavated for fluids. It appears as though the 6 inch outer casing is cemented into the well. Tony will finish removing rods and then remove tubing. Well will be circulated and bottom plug pumped into well. The 4 1/2 inch casing will then be removed (if possible) and the top plug pumped into well.
1248287449 2009-07-22 Orphan No Violations Nobody on site at time of inspection. Wellhead control device attached to 4 1/2 inch casing. It appears rods and tubing removed from well. Pit dug next to well for fluids. Plastic liner needed for pit before pumping fluids to pit.
1248367318 2009-07-23 Plug / Plug Back No Violations Old rods and tubing removed from well. Well cleaned out to depth of 1280 feet. Ran 2 inch tubing into well inside 4 inch casing and circulated fluids to tanks. Pumped 50 sacks of cement through 2 inch tubing for bottom plug and circulated fluids to tanks. Well produced oil and gas during circulation. Removed 2 inch tubing from well and will allow cement to set up. After cement sets up the well will be circulated again to try to remove remaining oil from well. Operator will then attempt to remove the 4 inch casing before pumping top cement plug.
1248726136 2009-07-27 Plug / Plug Back No Violations Cement set up at depth of 1000 feet from 5 yards of cement pumped on 7/23/09. Operator pulled entire string of 4 inch pipe from well (approximately 500 feet) on 7/24/09 and then pumped 8 yards of class A cement into well. Well did not circulate fluids to surface during this plugging. ODNR MRM inspector Sam Faust witnessed cementing of well on 7/24/09. Cement set up over weekend, then on 7/27/09 the top of cement was located at depth of 500 feet. Since well did not circulate fluids on 7/24/09, some of the cement went into the rock formation. The 13 yards of cement pumped into the well over the 2 days should have been sufficient to plug the well. Rather than pump more Class A cement, the decision was made to reverse grout the well with 9 sack grout. Cement grout was gravity fed into the well on the annular side of 500 feet of 2 inch tubing. Water was displaced through the 2 inch tubing and circulated to surface.
1248894769 2007-07-29 Orphan No Violations Well has been cut off 4 feet below ground elevation and ID plate attached to top of well. Most equipment removed from site. Pit will be backfilled and remaining epuipment removed from site
1248967291 2009-07-29 Orphan No Violations Well has been cut off 4 feet below ground and ID plate attached to top of well. Pit will be backfilled and remaining equipment removed from site.
1249388409 2009-08-03 Final Restoration No Violations Final restoration completed on site. Pit has been backfilled and area graded. All equipment removed. No contamination noted on ground. Site will be returned to agricultural production. Area where crop damage occurred as result of plugging activity is approximately 0.2 acres.

For data sources see[3]

References